ML17342B101

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Forwards mgt-on-shift Weekly Summary Rept,Per NRC 871019 Order
ML17342B101
Person / Time
Site: Turkey Point  
Issue date: 01/20/1988
From: Woody C
FLORIDA POWER & LIGHT CO.
To: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
L-88-32, NUDOCS 8802020256
Download: ML17342B101 (47)


Text

REGULA Y INFORMATION DIBTRIBUTI YSTEi I (RIDS)

ACCESSION NBR: 8802020256 DOC. DATE: 88/01/20 NOTARIZED:

NO FACIL: 50-250 Turkey Point Planti Unit 3i Florida Pacer and Light C 50-251 Turkey Point Planti Unit 4i Florida Power and Light C

AUTH. NAME AUTHOR AFFILIATION MQODYi C. Q.

Florida Power

8. Light Co.

REC IP. NAME RECIPIENT AFFILIATION GRACEi J. N.

Region 2i Ofc of the Director

SUBJECT:

Foreards mgt-on-shift meekly summary rept'er NRC 871019 ord er.

1 DISTRIBUTION CODE:

D036D COPIEB RECEIVED: LTR

~

ENCL +

SIZE:

TITLE: Turkey Point Management Onshift Program NOTES:

DOCKET 0 05000250 05000251 REC IP IENT ID CODE/NAME DRP/ADR-2 PD2-2 PD INTERNAL:

AEOD NRR DEPY NRR MORIBBEAUiD NRR/ADT NRR/DOEA DIR NRR/PMAS/ILRB OGC/HDS2 RGN2 FILE EXTERNAL:

LPDR NSIC CQP IES LTTR ENCL REC IP IENT ID CODE/NAME NRR/DRP-1/2 EDISON' DEDRO NRR DIR NRR/ADP NRR/DLPG/PEG NRR/DRIS DIR CMEBER Ni J REG FIL 01 NRC PDR COPIES LTTR ENCL TOTAL NUMBER OF COP IEB REQUIRED:

LTTR 23 ENCL

l

P.

X 14000, JUNO BEACH, FL 33408 0420 JANUARY 2 0 1988 L-88-32 Dr. J. Nelson Grace Regional Administrator, Region II U.S. Nuclear Regulatory Commission 101 Marietta Street, N. W., Suite 2900 Atlanta, Georgia 30323 Re:

Turkey Point Units 3 and 4

Docket Nos.

50-250 and 50-251 Mana ement-on-Shift Weekl Re ort

Dear Dr. Grace:

Pursuant to the Nuclear Regulatory Commission Order dated October 19,

1987, the attached summary of Management-on-Shift (MOS) reports is submitted.

Should there be any questions on this information, please contact us

~

Very truly yours, C.

O.

W Execut'ice President COW/SDF/pw Attachment cc:

J.

Lieberman, Director, Office of Enforcement, USNRC D.

G. McDonald, Project Manager,

NRR, USNRC Senior Resident Inspector, USNRC< Turkey Point Plant R. E. Talion, President, FPL aaoaOZO-5S S5OOO25O 8oi20 pDR
  • DOCK O pDR R.

PEOPLE...EENYING PEOPLE ~a~(

MA GEMENT ON SHIFT MOS)

WEEKLY

SUMMARY

REPORT WEEK $7+R7ING.

JcI~U<~/ ll, 1988 PAGE 1

OF 2

Four MOS observers were on shift:

Lamar L.

McLaughlin,. St.

Lucie Plant (01/11-17/88, Days);

Peter L. Walker, Westinghouse Electric Corporation (01/11-18/88, Nights);

Lee 'C.

Huenniger, Turkey Point Startup Department Superintendent (01/11-16/88, Split) and Jesus

Arias, Turkey Point Regulation and Compliance Supervisor (01/16-18/88, Split).

While on shift these MOS observers reported potential safety

problems, questionable work practices, areas for improvement,
comments, and general recommendations.

During this reporting period Unit 4 remained at full power except for routine main turbine valve operability and turbine trip tests.

Unit 3 was ramped to full power but had to be shutdown to Hot Standby (Mode 3) because of an unretrievable dropped rod (two rods were dropped during the attempt to retrieve the initial dropped rod).

A Control Rod Drive Mechanism (CRDM) housing seal weld leak was identified.

Unit 3

was cooled down to cold shutdown (Mode 5) in order to effect repairs.

No immediate safety problems were observed.

The following questionable work practices were observed:

During maintehance on the "3B" Boric Acid Transfer Pump the strip heaters were not deenergized (not on the clearance) which was a potential shock/burn hazard.

Security guards were observed to key their radios in restricted areas (may have caused some spurious alarms).

This requirement will be reviewed with all security personnel.

Some improvements were recommended by the MOS observers:

Affix lights or fencing around the Hydrogen trailer by the Unit 1

& 2 discharge.

Update phone numbers on security signs and replace any that are missing.

Review the processing of Plant Work Orders (PWOs) in order to improve the system.

ATTACHMENT:

MOS DAILY REPORTS

MAN GEMENT ON SHIFT (MOS)

I WEEKLY

SUMMARY

REPORT WEEK STARTING:

Januar ll, 1988 PAGE 2

OF 0

Establish a central location to maintain keys to all panels, breakers and buildings.

V Improve Plant Work Order response time specifically for A-1 type work.

o Ensure RCO log entries are made for significant transients such as the Unit 3 pressure reduction problem.

o Maintenance personnel need to improve their awareness of how the work on plant equipment can affect plant status.

Improve communications within Mechanical Maintenance concerning shift turnover of vital equipment.

o Repair leaks on Fire Protection System.

o Replace chicken wire removed from old drawing update trailer or install lighting.

o Ensure testing procedures are completed before placing equipment in service.

Several recommendations were made by the MOS observers:

Develop a

means to reduce operator confusion concerning Technical Specification LCOs for valves.

0 0

0 0

Evaluate the backup Nitrogen Systems for the Auxiliary Feedwater

.System (AFW) and the Main Steam Isolation Valves (MSIVs) to determine if improvements are needed.

Remove or repair a water cooler that is tied to the turbine deck railing.

Replace several temporary "No Smoking" signs with permanent ones and control them by an appropriate procedure.

Repair PCV-455B at first opportunity.

Determine root cause'f Pressurizer pressure tr'ansient.

ATTACHMENT:

MOS DAILY REPORTS

0;ADM-019 anagement on Shift (MO MOS DAILYREPORT Pig@

To:

Operations Superintendent-Nuclear Date:

0 From:

Lamar McLaughlin (M

6seruer)

Shift:

~x Day Q -Night h.

Plant evolutions observed Unit 3 power increased to 100%; Unit 4 at 100% power Review of Main Steam Isolation Valve Nitrogen Backup System (See 12/20/87 MOS Report).

Prints PC/M 85-135

- System walkdown

- JPE letter JPE-PTPO-87-2175 3-OSP-72.2

- Discussed briefly system with system engineer and NPO Control Room operations Unit 4 746 A (Component Cooling Vater Manual Isolation Valve) stuck open.

The operators'ave determined a

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO fs in effect since 1000 this morning.

This could be a conservative approach since they believe the valve is stuck open.

B.

Immediate safety problems None Questionable work practices None Area(s) for improvement None noted 0 NOS. I l&ll/I7 01/11/SS

0-ADM-019 management on Shift (MOI~

MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments The Nitrogen backup system for the Main Steam Isolation Valves appears to have problems that make the system difficult to operate.

The primary problem is leakage out of the system and check valve leakage.

These problems manifest themselves as excessive bottle changing and Temporary System Alterations to Surveillance Test procedures.

Recommendations will be made after further discussion with appropriate plant and engineering personnel.

A review of Nitrogen usage will be done tf data exists.

Recommendations None at this time Completed By:

ar McLau hlin seroer Date:

01 11/88 Reviewed By:

Management Review By:

p rations uperi ntendent-Nuclear

/~t,l8t'ate:

l /2-

~ate MANAGEMENTINITIALRESPONSE

~ KOS. I UI%7m Ol/11/88

0-ADM-019 Management on Shift (MO MOS DAILYREPORT Page ro Operations Superintendent

- Nuclear Date:

01 11-12 E8 From:

seroer)

Shift:

Q Day Qx Night h.

Plant evolutions observed Unit 3 Chemistry problem (action level

1) due to fluorides in steam Generators

- Resolved by demineralizers

- Not currently in action item.

Containment activity (particulate) continues to increase.

At the same time, pressurizer level channel Ll-3-461 was taken out of service (8%

high) and its bistables tripped.

A small amount (0.2179GPM) of reactor coolant leakage was also calculated.

Unit 4

valve 746 reach rod was repaired

- 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO cleared.

"4C" Charging Pump Pulsation Damper was worked on - Pump was

tested, but would not provide enough flow to keep up with 45 GPH letdown.

Pump is still out of service.

C.

D.

Immediate safety problems None Questionable work practices None hrea{s) for improvement None E.

Professionalism, Summary of Shift, Comments This observer was pleased to note no extraneous noises over the plant page..

Recommendations None Completed By:

P.L. Walker seroer Date 01/12/88 Reviewed By:

Management Review By:

perations uperinten nt-Nuclear

/ 6 at ate

0-ADM-019 management on Shift (MO+

MOS DA!LYREPORT Page To:

Operations Superintendent

- Nuclear Date:

01/11-12/88 From:

L. Huenniger (M

bseruer)

Shift:

0 Day Qx Night A.

Plant evolutions observed 1300 afternoon planning meeting 1515 Operations PSN turnover 1545 Operations/Maintenance shift meeting 100o'o plant operations 2315 Electrical Department turnover meeting 2345 Operations/Maintenance shift meeting B.

Immediate safety problems None C.

Questionable work practices n3Bn Boric Acid pump was being worked by Maintenance on peak shift.

The pump breaker was on the clearance, but the strip heaters on the dog house were not.

The house was removed and heaters exposed.

This presents a potential for electrical shock or burns to personnel.

D.

Area(s) for improvement South Control Room toilet is out of service with sign on the door.

It is a convenience item and one of showing plant support for operators and Control Room conditions.

Additionally the deep sink in the Control Room is leaking up to two GPM

- can't be shut off with faucet - water is in short supply - Plant Work Order was written last night.

The Hydrogen trailer by I 6 2 discharge has no lights under or fencing around it.

Suggest a light be permanently affixed to the nearby station for meeting this requirement.

Professionalism, Summary of Shift, Comments An NRC letter dated December 22, 1987 was read by the PSN at the shift turnover meeting in the Control Room.'his letter dealt with formal communications and led to a heated discussion between operators and the PSN.

This letter stirred much resentment and created a negative effect by people who have been under the gun for a long time and the resulting stress it carries with it.

This correspondence needed to be more specific, not such a sweeping statement of condemnation.

Attached - the Nuclear Newsletter under regulatory matters

- says visit was favorable, then the December 22, 1987 letter really let the air out of our sails.

01/11-12/88

O'-ADM-OI9 j

anagement on Shift (MOB MOS DAILYREPORT Page lt is my understanding that a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO was agreed upon between PTN licensing and the NRC concerning manual RHR valve 4-746A.

The reading of the Technical Specification left some Control Room operations personnel unsure as to what controlling condition applied.

A decision should be reached, put in writing or on a computer such that the PSN has only to input valve number and the predetermined Technical Specification will be identified and followed.

Completed By:

bseruer D

Reviewed By:

Management Review By:

perations uperi ntendent-Nuclear Date:

I r2.

MANAGEMENTINITIALRESPONSE a@OS.I OIN7%0 01/11-12/88

0-ADM-Oi9

~management on Shift (MO MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear, Date; 01/12/88 From:

A.

Lamar McLau hlin

(

bseruer Plant evolutions observed Shift:

Qx Day Q Night Morning plant status meeting Control Room shift meeting (morning)

Discussed status of Main Steam Isolation Valve (MSIV) Nitrogen Backup System with Technical, Startup, Operations and Site Engineering.

Due to containment particulate activity increase, the containment was tnspected by plant personnel for leakage.

Some water was found.

Evaluation of this leakage is in progress.

Control Room shift briefing (afternoon)

- Downpower planned for peak shift for Turbine Valve Testing B.

Immediate safety problems None observed C.

Questionable work practices None observed D.

Area(s) for improvement None Professionalism, Summary of Shift, Comments Nitrogen Backup System

- Operators're no longer having difficulty maintaining nitrogen bottle pressure.

- The Nitrogen System valves for the MSIVs are leaking such that additional isolation is required to perform periodic testing (See OTSC 5656).

- Technical is considering adding the MSIV Nitrogen System to the scope of the Request for Engineering Assistance (REA) for the Auxiliary Feedwater System (AFW) Nitrogen System work.

Control Room operators are attempting to clear past due surveillances.

This was discussed in the afternoon shift briefing.

The list should be reduced as much as possible.

1 NUB. I IVQI&7 01/12/88

'0-ADM-019 Ianagement on Shift (MOQ MOS DAILYREPORT Pase F.

Recommendations Recommend that Technical include the MSIV Nitrogen Backup System problems in the scope of the REA for AFW Nitrogen System.

Recommend that Site Engineering review NCR-0837-87 test results again to ensure that the test that was performed adequately addressed the deficiency description.

Completed By:

bseruer Dt:~

Reviewed By:

Management Review By:

perations uperi ntendent-Nuclear

/ g)3&'te MANAGEMENTINITIALRESPONSE ll&i.I 0 IIQ1M 01/12/88

0-ADM-019 anagement on Shift(MO MOS DAILYREPORT Page

'ro:

Operations Superintendent

- Nuclear Date:

01/12-13/88 From:

A.

6server)

Plant evolutions observed Shift:

Q Day px Night Unit 3:

RCS leak continues - slow increase in containment particulate.

When Shutdown Bank Operability Test (OP-1604.1) was attempted, a shutdown bank A rod dropped completely into the core, Turbine ran back (NIS rate) to approximately 709b, Quadrant Power Tilt Ratio (QPTR) was calculated to be approximately 11'S (111%).

Reactor Engineering requested power be decreased to less than 50% after rod was found to be irretrievable.

Unit stable at approximately 50%

and awaiting further decisions during day shift.

Unit 4:

Downpower to 40'k

- Repaired trip breaker, tested per 4-OSP-49.1

- Performed Turbine Valves Operability Test 4-OSP-089, section 7.3

- Performed Turbine Trip test

- Escalated back to 100o'o at 3 MWE/minute rate

- Unit steady at 100o/a power B.

C.

D.

Immediate safety problems None Questionable work practices None Area(s) for improvement None Professionalism, Summary of Shift,,Comments During the last 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, the Operations staff performed well while doing a

very complex series of operations, and recovering from the rod drop transient.

I was especially interested in the communications, which were done in a professional manner.

Recommendations None Completed By:

P.L. Walker server Date.

01/13/88 Reviewed By:

Management Review By:

perations uperintendent-uclear

/ I/JK ate Date:

/

ate all(ki I ollQ7iea 01/12-13/88

0-ADM-019 anagement on Shift (MO MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date:

01/1"-13 88 From:

L. H'~ennin

'.r (M

6seroer)

ShiA.;

Q Day Qx Night Plant evolutions observed 1:00 p.m. plant planning meeting 3:45 p.m. Operations/Maintenance turnover meeting 11:15 p.m. Mechanical/Maintenance turnover Load reduction - 100% to 40oo power (4-GOP-103)

Turbine Valve Test (4-OSP-089)

Replacement of relay by IGC and preparation by Operations (4-OSP.1)

B.

immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement None 01/12-13/88

0-ADM-019 elianagement on Shift (MO MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments l.

I observed three Operations/Maintenance turnovers in the Control Room during the past two days.

Each Maintenance Department representative had in hand the Plan of the Day.

Z.

Two in-shop turnovers were conducted in which on going work activities and the Plan of the Day were passed on to the on-coming shift. All the supervisors and foreman I talked to expressed a feeling of having a

better status of plant needs.

They thought having Maintenance at the Operations/Maintenance turnover meetings gave them an update to the current operations needs.

3.

A general feeling I got was the Maintenance people were providing better operations support than my previous Management on Shift days.

This was observed by two foreman receiving operations calls during our conversation, excusing themselves, then directing their people on a real time basks to take care of the operations needs.

Their attitute was more suportfve and a willingness to do so.

4 The peak shift with mid shift holdover, did a very professional job of bringing down the unit, coordinating the valve test, taking out the reactor trip breaker for IGC relay replacement, performing the Turbine Trip Test and increasing to full power operation.

Recommendations The water cooler on the turbine deck by ¹3 generator exciter switch gear is rusted out and tied to the rail by a rope. It should be replaced or removed, it gives a run down appearance to a very visible area.

Completed By:

L. Huennin er seruer Date: '1/I".'88 Reviewed By:

y7 perations uperintendent-Nuclear Date: <<8 P

Management Review By:

ate aQUb.l el%7'ee 01/12-13/88

0 ADM-019 anagement on Shift (MOS MOS DAILYREPORT Page To Operations Superintendent

- Nuclear Date:

01/13/88 From:

Lamar McLau hlfn server)

Shift:

gx Day Q Night h.

Plant evolutions observed Morning plant status meeting Control Room shift briefing Unit 3 power reduced to 10 8 amps.

Trouble shooting N-9 dropped rod.

Emergency drill practice in progress on Unit 4 Toured Turbine Building While shutting down Unit 3 control rods dropped

- Unit 3 was manually tripped

- The required NRC notification was made B.

C.

Immediate safety problems None Questionable work practices None E.

brea(s) for improvement None observed Professionalism, Summary of Shift, Comments Attended ERT meeting for control rod N-9 and LT-461.

The meeting was effectively run and directed towards the pre-planning of work activities during the reactor downpower (10 8 amps power at the time).

-, Work items that needed to be completed prior to return to power were identified.

- A game plan for troubleshooting rod N-9 was discussed.

This troubleshooting was aimed at isolating an open fn the coil circuit.

- A discussion of LT-461 problems reviewed suspected problem areas fn the reference leg system for this transmitter.

The three rods that dropped are all fn the same area of the head.

The present plans are to investigate this area of the head and if a leak fs found fn this area, an immediate cooldown will be done.

If leakage fs not found fn thfs area the Reactor Coolant System (RCS) willbe kept pressurized and a leak search willcontinue.

Reviewed the reportabflfty for the initial dropped rod event.

This event was properly reported under 10 CFR 72 b (2)ff.

a N(L>,I I &Ills A1 /1 3/RA

0-ADM-019 Management on Shift (MC MOS DAILYREPORT Page F.

Recommendattons None Completed By:

La ar )1 L u hlin server Date:

01/13/88 I

Reviewed By;

'anagement Review By:

Operations Superintendent-Nuclear Iq 88 Date:

~ate MANAGEMENTINITIALRESPONSE 0/13/88

~ il(Li.lelenaee

0-ADM-019

~Management on Shift(M MOS DAILYREPORT Page To:

Operations Superintendent - Nuclear Date:.

01 13-14 88 From:

server)

Shift:

Q Day px ¹ight h.

Plant evolutions observed Unit 3: Hot standby, degassing Unit 4:

100% steady state B.

Immediate safety problems None C.

Questionable work practices.

None D.

brea(s) for improvement None E.

Professionalism, Summary of Shift, Comments None Recommendations None Completed By:

p server Dt:~

Reviewed By:

Management Review By:

rations uperi ntendent-uclear

/ I l'I lR Dat:

r SE

( (((~lsd ail@i.t Ill%7(aa 01/13-14/88

0 ADM-019 Management on Shift (MOSQ

~

MOS DAILYREPORT Pege To:

Operations Superintendent

- Nuclear Date:

01/13-14/88 From:

L.C; Huenniger (M

bseruer Shift:

p Day

'x Night A.

Plant evolutions observed 1:00 p.m. plant planning meeting 3:15 p.m. Haintenance day-to-peak turnover 3:45 p.m. Operations/hiaintenance turnover meeting.

VCT gas space concentration control (3-OP-047.1).

IGC taking voltage readings on control rod drive cabinets in 3B Motor Control Center (hiCC).

11:15 p.m. IAC peak-to-mid shift turnover B.

immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement None E.

Professionalism, Summary of Shift, Comments The Plan of the Day continues to be used at turnover by the Maintenance Department.

Today, with emergency drill. several supervisors and foremen were filling spots temporarily, but conducted normal turnover, including use of the Plan of the Day per maintenance direction.

hiuch interest as to cause of tJnit 3 shutdown, length of time down, and what must be done to 'return the unit to the line was exhibited by many plant people this shift.

~ MO> I I'Vllli01 01/13-14/88

0-ADM-OI9

~Management on Shift (Ml MOS DAILYREPORT Page Recommendations Three temporary "No Smoking" signs with red plastic flags, a wood

post, and clamp with "No Smoking" hand written on them should be replaced by professionally painted signs.

Two flags are located at top of stairs to ¹3 condensate pit and one flag by Hydrogen Gas dryer

¹3 unit.

These flags, in the future, could be controlled by AP-103.36 "Control of Operator Aids and Temporary Information Tags".

This would insure periodic review and a removal when no longer required.

Completed By:

L.C. Huenni er bseruer Date..01/14/88 Reviewed By:

'erations uperi ntendent-Nuclear Management Review By:

Date:

/ii/

N'te MANAGEMENTINITIALRESPONSE alt0$.1 01%7+a 01/13-14/88

6-ADM-019 f

anagement on Shift (M0 MOS DAILYREPORT Page To:

Operations Superintendent-Nuclear Date:

Ol 14 88 From:

A.

(M server)

Plant evolutions observed Shift:

Qx Day Q Night B.

C.

t'orning Plant Staff fleeting 7:45 shift briefing in Control Room Unit 3 degassing of hydrogen in preparation for cooldown; Unit 4 is at 100>> power.

Toured Turbine Building area and diesel rooms Toured intake area Af.ernoon Staff tteeting Afternoon shif. briefing in Control Room and Control Room Operations.

Security event occurred - storm drain protection not in place Unit 4 had a problem with a 4KV transformer (auxiliary).

Transferred power.o startup transformer.

Troubleshooting efforts underway.

Ineediate safety prob1ems None guestionable work practices None D.

E.

F.

Area(s) for improvemnt None Professiona1ism, Sumary of Shift, Coaments

't was determined that control rods L-9 and t1-10 dropped during shutdown yesterday due to fuses being pulled.

These are the same fuses that supply rod N-9.

Recoarnendations None CompletedBy:

Lamar tlcLau hlin server 0 t:

D //8 Reviewed By; Management Review By:

perations uperi ntendent-uclear ate Date:

IS'te

0-ADM-019 Planagement on Shift (MOQ MOS DAILYREPORT Page ro:

Operations Superintendent-Nuclear Date:

Ol 14-15/80 From:

p server)

Shift:

Q Day Qx Night A.

Plant evolutions observed B.

C.

0.

Unit 3:

Volume Control Tank purge - gas decay tank release.

Hydrogen down to desired level prior to cooldown.

Initiated cooldown.

Unit 4: Steady state - 100~'ower.

Imediate safety problems Noni 2 guestionable work practices None Area(s) for improvement Hone E.

Professionalism, Sunrnary of Shift, Comments Yesterday

( 14 )an. 88),

I received a request from an instrumentation and control technician which expressed concern for the ef ectiveness of recent changes in policy aimed at improving the overall condition of eouipment in the plant.

I passed the request on to the DOS coordinator for his attention.

Today

( 15 Jan.

88),

I discussed the issue with the individual and informed hin that a review had been initiated.

F.

Recomnendations None Completed By:

P.

L. Balker server Date:

01/15/88 Reviewed By:

Management Review By:

allOb I allll7%a perations uperi ntendent-Nuclear 01/14-15/88 ate Date:

/ r5 I7

Q-ADM-019 Management On Shift (MO

)

~

MOS DAILYREPORT To:

Operations Superintendent

- Nuclear Date:

01/14-15/88 From:

L,C. Huenniger (I bseruer)

Shift:

P Day Cxl Night A.

Plant evolutions observed B.

1:00 P.H. operations/maintenance planning meeting 3: 15 P.H.

I&C day-to-peak turnover

- Electrical Department troubleshooting ground on fire horns.

- Operations evaluation and isolation" of salt water leak on 3B turbine plant cooling water system.

Bushing rusted through allowing separation of isolation valve 3-50-579B from header.

Line is outlet sensing line to FI-3-1406 ll:15 P.M. mechanical maintenance turnover peak-to-mids.

ll:45 P.H. operations/maintenance turnover meeting.

Itmediate safety problems None C.

Questionable work practices None 0.

Area(s) for improvement Security signs on fences for both units to the steam platforms, blowdown areas, condensate

areas, feedwater platform, and the common Diesel House have signs with wrong (old) phone numbers.

These signs are 20" X 24" orange with black letters stating "Security Barrier - Caution - prior to removing or cutting any portion of this barrier security must be notified at PAX 398 Bell 4405."

Neither of these numbers will connect you with security.

Signs need to have correct phone number attached over incorrect numbers, and those loose and on the ground need to be refastened to the fences.

~ NlPi I I'~lil1 01/14-15/88

0-ADM-019 Management on Shift (MO MOB DAILYREPORT Page E.

F.

Professionalism, Sunrnary of Shift, Cerements Operations peak shift turbine operators and Nuclear Watch Engineer did a professional job in evaluating and isolating the 38 turbine plant salt water line to stop the header leak quickly.

The drain valve was opened to prevent any, leakage flow past the butterfly valves to be removed by system low point which will allow maintenance to repair on midshift.

tlechanical maintenance turnover at 11: 15 P.H.

was very thorough reviewing many PWO's, the priority, reason for holdup, and status of ongoing work was reviewed.

The plan of the day was passed on from peak-to-mid shift.

Recoamendations Hone CompletedBy:

L.C. Huenni er server Date Ol/15/88 Reviewed By:

Management Review By:

1M' Ulalt'ae peratio'ns uperi ntendent-Nuc ear ate Date:

/ /5 01/14-15/88 ate

6-ADM-019 management on Shifi, (MO MOS DAlLYREPORT Palo To:

Operations Superintendent

- Nuc]ear Date:

01 15 88 From:

Lamar McLau hlin bseruer)

Shift:

g Day p ¹ight h.

Plant evolutions observed Morning plant status meeting Control Room 7:45 shift briefing Unit 3 plant cooldown Afternoon plant status meeting Unit 3 containment atmosphere is cleaned up such that respiratory protection is no longer required in general areas.

B.

C.

D.

Immediate safety problems None Questionable work practices None brea(s) for improvement Will make recommendations tomorrow after discussing pressure event with the operators that were on shift at the time.

Professionalism, Summary of Shift, Comments RCS pressure reduction After the shift turnover meeting (7:45) I noticed an unusual trend on pressurizer

pressure, (approximately 350 PSI drop in 12 minutes, then increase).

This decrease had happened on the previous shift (about 7:15 a.m.) and was stored on Safety Assessment System (SAS).'hecked cooldown procedure to see where the accumulators should be isolated (700 to 1000 PSI) from RCO to see if there were any pressure/temperature problems.

No problem found.

Notified APSN and PSN to ensure they were aware of the event.

Requested a pressurizer level trend to see if accumulators had injected into RCS.

Information was not conclusive, subsequently received accumulator trends that appear to show discharge to the RCS.

Suggested that PSN and APSN look at reportability of the event.

They contacted the regulatory and compliance group for support.

NRC notified within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of verification of accumulator discharge.

Cable found smoking in a manhole.

This was subsequently extinguished.

  • aiu.i iuu>ev 01/15/88

~0-ADM-019 anagement on Shift (MO MOS DAlLY.REPORT Recommendatfons None Completed By:

Reviewed By:

Management Review By:

M dseroer P

Operations Superintendent-Nuclear M-Dt:~

MANAGEMENTINITIALRESPONSE 01/15/88

6-ADM-oi9

+Management on Shift (M(

MOS DAILYREPORT Page To:

Operations Superintendent

- Nuclear Date; 01/15-16/88 From:

h.

L Walker server Plant evolutions observed Shift Q

Day g Night Unit 3:

Uneventful cooldown/depressurization to Mode 5.

Stable, drained to approximately 10%

in pressurizer, missile shield removed.

Equipment hatch open, guards posted.

Unit 4:

Stable at 100% power.

B.

C.

D.

Immediate safety problems None Questionable wort practices None brea(s) for improvement None Professionalism, Summary of Shift, Comments Unit 3 operators did well to switch from cold calibrated pressurize level indicator to one of the functional hot calibrated level channels

- the cold calibrated sensor uses the same reference leg as the faulty LT-461, but had not been tagged as defective.

During the midnight shift turnover, two training briefs were well read and interpreted by the PSN.

Recommendations None Completed By:

P.L V ker server Date:

01 06/88 Reviewed By:

Management Review By:

perations uperi ntendent-uclear

/>0 Date:

/ // E

0-ADM-019 management on Shift (MO MOS DAILYREPORT Page To:

Operations Superintendent-Nuclear Date:

From:

6server Shift:

p Day Qx Night A.

Plant evolutions observed 3:15 p.m. Mechanical Maintenance day to peak turnover Pire and fire team response to site support Unit 4 100% power operation Unit 3 RCS cooldown operation 11:15 p.m. IGC peak to mid turnover 11:45 p.m. Operation/Maintenance turnover B.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement PWO time response

- specifically to A-1 type work.

Problems:

'(See F.

for recommendation) a.

b.

C.

d.

e.

g.

h.

i.

PWOS not classified timely Not PSN approved timely Not entered into computer timely WA number not assigned for quick identification Receiver not checking computer often enough to start PWO package development.

QC signature not obtained timely No set method (standardized) for all shifts to follow Inputers in Control Room - not given computer training Lack of followup phone call on hot items to determine priority within a priority.

Hot items identified - not followed up timely with WA number on PWO and phone call to designated person.

O.ADM-019 anagement on Shift (Mo

)

MOS DAILYREPORT Page Professionalism, ummary o t,

ommenta l.

The fire team responded quickly - had appropriate gear, worked well with all departments involved.

This was a small, but not normal situation in that a trace of smoke was coming from a conduit in a open manhole.

Thermography was used to locate covered

manhole, Construction/Plant forces opened manhole - fire team lead way to determining source.

Operation personnel assisted in isolation of the feed, once the probable feed was indentified.

Plant Electrical forces willsecure source and render it safe.

2.

One problem was identified from the fire in the manhole.

Once source of supply was properly identified, the breaker could not be opened to confirm suspicion due to a

lock on distribultion center door.

Considerable time was expended until a

key was found and lock removed.

3.

The peak maintenance crews had a

good work plan for the shift.

They accomplished the polar crane mechanical

checkout, moved the missile shields to the top of the pressurizer, defeated the personnel hatch inte~ locks and opened equipment hatch.

A real good effort.

h Recommendations (See E. 2.)

All panels,

breakers, buildings should have a

key for entry at a

centralized location such that entry could be made without cutting locks or destroying doors.

I suggest a key storage facility be maintained at a central location and keys identified. by panel or building location.

A place that is manned 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> per day and controlled such as security, might be a good group to act as custodian.

(See D.)

A meeting of Operations

Planner, Scheduling, Maintenance, Generating Equipment Management Systems (GEMS),

and OC representative meet to coordinate details.

The basics are in place, a couple of people I talked to have ideas for improvement.

- Proceduralize outcome of meeting by incorporating a

standard method for all shifts to follow.

Example, 0-ADM-010 activity planning and coordination, hot items (the subject) is already there

- needs expansion and more direction/detail.

- Provide PSN, APSN, and NWE computer training or detailed menu to follow. (PWO inputing).

- Provide how backup method will flow should computer system fail.

(Manual on similar method needs to be established and documented).

The R-14 PWO of 01/14/88 took aproximately six hours to get to the field from origination.

Numerous small items that collectively used too much time and can be improved on by the ideas of those I talked to should be

- utilized.

Completed By:

Date:

01/16/88 Reviewed By:

perations Superintendent-uclear Management Review By:

ate ate ate

'P

0 ADM-oie management on ShiFt (MO MOS DAlLYREPORT PIgt To:

Operations Superintendent

- Nuclear Date:

01 16 88 From:

A.

Lamar McLau hlin bseruer Plant evolutions observed Shift:

g Day Q Night 0

7:00 a.m. plant staff meeting 7:45 Control Room shift meeting Discussed with Control Room'operators the RCS pressure event of 01/15/88.

Unit 3 on Residual Heat Removal (RHR) - Unit 4 is at 100%

LT-461 (pressurizer level) was found to have a leaking bypass value.

B.

Immediate safety problems None C.

Questionable wort practices None D.

Area(s) f'r improvement Logging of RCS pressure event

- This event should have been logged in the RCO log.

An entry such as "RCS pressure transient occurred.

RCS pressure recovered.

Investigating."

would have been appropriate.

It is not my intent that every annunciator have a log entry, but I do feel a description of a

~si nificant transient like this should be entered even if the root cause is not known.

Professionalism, Summary of Shift, Comments RCS Pressure reduction event.

- Discussed the event with the off-going RCO.

He took accountability for initiation of the event.

The root cause appears to be an error in the adjustment of the spray valve just before or during the shift turnover.

The spray valve in use had a plant work order written against it due to valve response characteristics.

The shift turnover was in progress.

These two factors probably contributed in making this event occur.

- Discussed with the operators the logging of an event like this.

Early entries were not made although subsequent entries were made in the APSN log. This item is identified as an area for improvement.

- Reviewed the Shift Technical Advisor (STA) report of abnormal occurrences and determined that the first indication that a problem existed was the accumulator alarm actuations (RCO statement).

These alarms show that accumulator discharge had occurred.

The operator took manual control of pressurizer spray and ensured heaters were energized to recover pressure.

4U(hv I larUllaf

D

.0-ADM-019

~ Management on Shift (M)

MOS DAILYREPORT Page Recommendations Recommend that this event be reviewed by other operators via routine in-house review system.

This event could have been more complicated had the accumulators been isolated at initiation.

Recommend that Operations Department address the event logging area for improvement.

It is not clear who should have logged this event considering time of the event (shift turnover).

Repair PCV-455B at first opportunity.

Completed By:

Lamar McLau hlin seroer Reviewed By:

perations uperintendent-Nuclear Date:

01/16/88 Management Review By:

te VP MANAGEMENTINITIALRESPONSE 01/16/88

0-ADM-019 anagement on Shift (Mo MOS DAILYREPORT Page ro Operations Superintendent

- Nuclear Date:

From:

P.L. Walker bseruer Shih:

Q Day g Night A.

Plant evolutions observed Unit 3:

Stable ln cold shutdown

- Maintenance work continuing ln containment.

Unit 4:

100% steady state power production.

Observed 2230 and 2315 shift turnover discussions.

Toured Auxiliary Building.

Immediate safety problems None C.

Questionable work practices None D.

Area(s) for improvement None E.

Professionalism, Summary of Shift, Comments Very smooth, quiet shift. No problems, no great challenges.

F.

Recommendations None Completed By:

P.L. Walker Date:

0 1/17/88 server

~/'

Reviewed By: G

. 8 8

perations uperi nten nt-uc ear Management Reviewer By:

/IS

/

Vl 1ft

~ II%I I OINT'

0-ADM-019 management on Shift (MC MOS DA1LYREPORT Page To:

Operations Superintendent-Nuclear

- Date:

01/16-17/88 From:

Jesus Arias, Jr.

seroer Shift; p

Day px Night A.

Plant evolutions observed Outage meeting Shift turnover meetings Placing CV-4-1510A back in service Shift briefings B.

Immediate safety problems None C.

Questionable work practices None D.

brea(s) for improvement IGC Technician came over to the Control Room to work on relay TC-4-408D-I.

Upon questioning by Control Room personnel and Shift Technical Advisor (STA) of possible effects of his work, he could not answer.

He was asked to go back to the shop and get more familiar with the work planned and possible effects.

He then came back (approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> later) and had a good understanding of the relay function and effects of his work.

"4Cn Charging Pump was discussed at the 1:00 p.m. meeting as needing further work (could not hold a 45 gpm orifice) but this work was not turned over to peak shift or mid shift in Mechanical Maintenance.

With the "4B" Charging Pump having an information tag to minimize use, the n4C" Charging Pump work becomes critical.

A1 I ~ c 16lhtl

i~

O.-ADM-or9 Management on Shift (M)

MOS DAILYREPORT Page Professionalism, Summary of Shift, Comments Overall, professionalism was adequate.

Shift briefings are thorough and well attended.

Some inform'ality still is noticed during shift briefings.

During the shifts there were several trainees in the Control Room.

RCOs and APSNs had good control of them.

During the peak shift, I witnessed the task of placing CV-4-1510A back in service.

There was good coordination, valving was done carefully and prudently.

Adequate supervision was devoted to this evolution.

Constant communications between Unit 4 RCO and other personnel (PSN, NWE, and TOs) was efficient.

A difficult evolution was handled smoothly.

Shift briefings are not necessarily following the Daily Work List.

Recommendations 16C personnel should be knowledgeable of work and its effects.

A few more minutes at the shop'will expedite the work and prevent mistakes.

Review Daily Work List during shift briefings for work scheduled for the shift. (Priorities may change).

Operations management should review the pressurizer pressure transient of 01/15/88.

What was known

then, may be important.

Did not get a clear description of root cause.

Completed By:

Jesus Arias Jr.

server Date:

01/17/88 Reviewed By:

perations uperinten nt-uc ear oat:

Management Review By:

VP

0-ADM-019

~ I management on Shift (MO MOS DAILYREPORT Page TQ:

Operations Superintendent

- Nuclear Date:

01/17/ee From:

h.

server Plant evolutions observed Shift:

g Day Q Night B.

C.

D.

7:00 a.m. plant staff meeting 7:45 a.m. Control Room shift briefing Control Room operations Toured intake and Turbine Building areas 3:45 p.m. Control Room shift briefing Immediate safety problems None Questionable work practices None brea(s) for improvement None Professionalism, Summary of Shift, Comments Over the past few days, in the Control Room briefings, the operators have been kept up to date on the RCS leak.

Discussions/presentations have been given that describe the location and extent of the leak, locations of the limited boric acid deposits and plant/descriptions of the weld repair process..

I feel these discussions are effective in promoting a team atmosphere.

F.

Recommendations None Completed By:

Lamar McLau hlin server Date:

01/17/88 Reviewed By:

Management Review By:

perations uperinten nt-uc ar Date:

i /

8-ADM-019 Management on Shift (MQ)

MOS DAILYREPORT Page ro:

Operations Superintendent

- Nuclear Date:

01 17-18 88 From:

server Shift:

Q Day g Night h.

Plant evolutions observed Unit 3:

Cold shutdown - 10% level in Pressurizer.

Evaluation team inside containment looking at leak.

Videotapes shown to Operations in humain Control Room.

Unit 4:

100% power - no transients B.

ImmedIate safety problems None C.

Questionable work practices None D.

brea(s) for improvement None Professionalism, Summary of Shift, Comments Quiet shift Recommendations None Completed By:

server Date:

01 18 88 Reviewed By:

Management Review By:

l'erations uperi ntendent-uclexr

0;ADM-019

~ ~

Management on Shift (MOS)

MOS DAILYREPORT Page To Operations Superintendent

- Nuclear Date:

01 17-18 88 From:

Jesus Arias Jr.

(M bseruer)

Shift:

Q Day Qx Night A.

Plane evolutions observed Shift turnover Sh ift briefings Plant tours B.

C.

Immediate safety problems None Questionable work practices Security guards continue the practice of keying radios at the turbine deck in the proximity of the steam generator and steam line pressure transmitters.

At 1134, a Digital Data Processing System alarm was noticed on "4C" Steam Generator (S/G) steam line differential pressure.

A guard was in the area using his radio.

During the night a second guard was seen using his radio in the same area.

The yellow signs posted in these areas are not preventing this practice.

When questioned,.

the guards responded that they had forgotten the restrictions.

D.

Area(s) for improvement During a plant tour, several leaks were noted on the fire protection system.

Some of the major ones are:

- Recirculation line to the Diesel Fire Pump has an elbow leak (thru-pipe) P WO ¹316509 dated 01/02/87.

- Raw Water Tank ¹I outlet valve 10-615 has a packing leak.

PWOs (1) WA861260858 dated 05/06/86.

(2) 026982 dated 04/09/87.

- Thread leak on recirculation line to Electric Fire

Pump, PWO

¹316958 dated 01/06/88.

Old drawing update trailer located east of the Technical Support Center has a section of chicken wire removed, and no lighting has been installed underneath.

In reviewing the Out of Service log, found an Appendix B sheet for testing of 3-2833 (Auxiliary Feed Water flow control valve).

This sheet is required by procedure to be signed off by the Inservice Testing Coordinator or the Shift Technical Advisor upon completion of post-maintenance testing arid provided to the Maintenance Supervisor for signature.

FCV-3-2833 was placed in service during the day shift after satisfactory testing per 3-OSP-75.10.

The Appendix B sheet was not signed off or pulled out accordingly.

a Mll'iI I'CWliI7 01/17-18/88

a 0-ADM-019 anagement on Shift (MO MOS DAlLYREPORT

, Page B.

Professionalism, Summary of Shift, Comments Shift members were acting in a professional manner.

Shift turnovers, board walkdowns and shift briefings were thorough, and the interchange was adequate.

Plant is clean and quiet.

Reactor Operator trainees stayed busy and with reasonable control by the RCOs.

Not a lot of activity to mention.

Hard hats, ear protection and footwear policies are being followed regularly.

Recommendations Devote 6OMe resources and attention to the leaks in the Fire Protection System.

Provide further guidance to security guards regarding the use of radios in the vicinity of steam pressure transmitters.

Replace chicken wire on trailer by the Technical Support Center.

Completed By:

Jesus Arias Jr.

server Date 01/18/88 Reviewed By:

Management Review By:

perations uperintendent-uclear Dat:

r it ate ni I~ ~ in/on

q.Q 45m