ML17328A244

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LER 89-014-00:on 891127,discovered That P-250 Computers Rod Sequence & Deviation Monitors Inoperable Since Computer Bootstrap on 891123.Caused by Inadequate Guideline to Conduct Computer Bootstrap.Program corrected.W/891221 Ltr
ML17328A244
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/21/1989
From: Blind A, Ross C
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-89-014-01, LER-89-14-1, NUDOCS 9001040148
Download: ML17328A244 (6)


Text

ACCELERATED D UTION DEMON TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9001040148 DOC.DATE: 89/12/21 NOTARIZED: NO . DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana & 05000315 .

AUTH. NAME AUTHOR AFFILIATION ROSS,C.A. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele BLIND,A.A. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION R

SUBJECT:

LER 89-014-00:on 891123,Tech Spec surveillance requirement missed due to deficient administrative guidance.

W/8 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1 1 PD3-1 PD "1 1 GIITTER,J. 1 ~ 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1. 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DET/ESGB 8D 1 1 NRR/DLPQ/LHFBll 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEABll 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 NRR/DST/SPLB8D1 1 1 Rg/~ST/SRXB 8E 1 1 NUDOCS-ABSTRACT 1 1 ~EG F 02 1 1 RES/DSIR/EIB 1 '

1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 R NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 D

D NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTEl CONTACT THE DOCUMENT CONTROL DESK ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEEDl FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 38 ENCL 38

Indiana Michigan Power Company Cook Nuclear Plant P.O. Box 458

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Bridgrnah. Vil 49106 616 465 5901 INDIANA NICHIGAItI POWER December. 21, 1989 United States Nuclear Regulatory Commission Document Control Desk Rockvi1 le, Maryland 20852 Operating License DPR-58 Docket No. 50-315 Document Control Manager:

In ac:cordance with the criteria established by 10 CFR 50.73 entitled L'censee Event Re ortin System, the following report is heing submitted:

89-014-00 S

incere1>>,'.A.

Blind Plant Manager AAB:clw Attachment cc: D.H. Williams, Jr.

A. B. Davis, Region III M.P. Alexich P.A. Barrett J.E. Borggren R.F. Kroeger NRC Resident Inspector J.G. Giitter, NRC R.C. Callen G. Charnoff, Esq.

Dottie Sherman, ANI Library D. Hahn INPO PNSRC rgA S.J. Brewer/B.P. Lauzau g g>>'gp>>

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NRC Form 384 US. NUCLEAR REOULATORY COI04ISSION (P4)3)

APPAOVED OMB NO. 31600104 EXPIAES: SI31IBS LICENSEE EVENT REPORT {LER)

FACILITY NAME (1I DOCKET NUMBER (2)

D. C. Cook Nuclear Plant - Unit One o 5 o o 031510F04

"""'echnical Specification Surveillance Requirement Hissed Due to Deficient Administrative Guidance EVENT DATE l6) LEA NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED ISI MONTH DAY YEAR YEAR ~: ssorsslsTIAL NUMBER (I@ NUMBER MONTH DAY YEAR FACILITYNAMES DOCKET NUMBERIS) 0 5 0 0 0 2 3 8 9 8 9 014 0 0 1 22 18 9 0 5 0 0 0 THIS REPORT IS SUBMITTED PUASUANT TO THE AEOUIREMENTS OF 10 CFR (I; ICnrce onr or morr of tnr foriowi'nPI 01)

OPERATING MODE ISI 20.402(b) 20.406(c) 50.73( ~ ) (2) (lv) 73.71(5)

POWER 20.406(e) (1) (I) 50M(c)((l 50.73(el l2)(v) 73.7((c) l

'EVEL p p 20 406( ~ )(Il(SI 50.38(c) (2) 60.73(el(2) (rill OTHER ISprCify in Aettieet INiow end In Trnt HRC Fpnn 20.406( ~ ) (1)(lll) X 50.73( ~ )(2)lll 50.73(e l(2) (rllll(AI 366AI 20A05(e l(1) (Ivl 50.73(e I (2((S) 60.73(el(2)(rllll(B) 20.405(e) (1)(vl 60.73(e I (2)(IllI 60,73( ~ ) (2)(el LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER AREA CODE CD A. Ross - Computer Science Superintendent 61 6 4 6 5 - 5 90 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13l

'%KNRKNY%o "~ y+ 6,

". ~n MANUFAC.

i~Q+. )i MANUFAC. rrr~'PORTABL CAUSE SYSTFM COMPONENT '3 c. CAUSE SYSTEM COMPONENT TURER TO NPRDS .

TURER TO NPRDS

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(+A!,74 &%M ETI%%l:

SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)

YES IIIyes, compirtr EXPECTED SUEMISSIOH DATEI NO ABSTRACT ILimit to f400 sprcn, I,r., epproximrtriy fifteen sinpir.specs typewritren IinNI (141 On November 77, 1989, with Un5.t One operating at 100 percent reactor thermal power, ie was discovered that the P-750 computers rod sequence and deviation monitors had been inoperable since a compueer bootstrap on November 73, 1989.

The inoperabilitv was unknown causing the required Technical Specification l,'T/S) increased surveillance eo not be per ormed. T/S 4.1.3.1.1 and 4,1.3.2 both require a four hour surveillance of rod position determination if the rod deviation or sequence monitors are inoperable. The normal operating twelve hcur T/S surveillances were completed with no out of specification rod positions during this event per5od. The P-250 Rod Monitor Program did not reactivate after the computer bootstrap because an operator failed to update one address point. The guidel5ne to update the computer is not explicit and contradictory causing the operator to not perform the update task properly.

To prevent this event from reoccurring, a detailed procedure to perform a post maintenance operabi.lie'v check of the P-250 computer will be wrieeen.

The bootstrap guide'ine has been revised to include information necessary to bootserap and update ehe computer correctl.y.

NRC Form 385 I& 83"

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NNC Form 35SA U.S. NUCLEASI hECULATONY COMMISSION 1043 I LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AFFROVEO OMS No. 3150&105 EXPIRES: b/31/Ie FACILITY NAME III OOCXET NUMSEh I2l LEh NUMSEh (~) ~ AOE ISI YEA/I 5SOUSNT/AL v " osvlSION HVM55% HQM so D. C. Cook Nuclear Plant: - Unit One 0 0 0 5 0 0 0 3 $ 5 8 9 1 4 0 0 4 oFO 4 TEXT /// more <<>>ce is soy/we/L oss ~ //OO/'>>/ HRC %%de 3/ELA's/ IITI FAILED COMPONENT IDENTIFICATION:

NONE PREVIOUS SIMILAR EVENTS:

NONE

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