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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
AC CRAP>TED Dl Bt 'Tl ON DEMO~ > TV '104 SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8906200200 DOC.DATE: 89/06/13 NOTARIZED: NO DOCKET I FACIL!50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION ARBUCKLE,J.D. Washington Public Power Supply System POWERS,C.M. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 89-016-00:on 890514,ESF sys actuation caused by inadvertent fuse removal & loss of power due to IFL/IT/PE.
W/8 1tr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 SAMWORTH,R 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ,D ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 IRM/DCTS/DAB 1 1 NRR/DEST/ADE 8H 1 1 NRR/DEST/ADS 7E 1 0 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 .1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB 8D 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/J)REPJRPB 10 2 2 NUDOCS-ABSTRACT 1 1 1 1 RES/DSIR/EIB 1 1 RES/DSR PRA 1 1 RGN5 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 FORD BLDG HOY I A 1 1 R L ST LOBBY WARD 1 1 LPDR 1 1 I
NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NIXIE 'IO ALL "RIDS" RECIPIENIS PIZASE HELP US IO RHXJCE WASTE! CONTACT 'IHE DOCUNEPZ CGNZRDL DESK, KXN Pl-37 (EXT. 20079) 'XO KZiZMZNATR RÃ3R NAME FBCH DISTEUBVTIGN LISTS H)R DOCUKWZS YOU DGNIT NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 43 ENCL 42
a~i WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99352 Docket No. 50-397 June 13, 1989 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO.89-016
Dear Sir:
Transmitted herewith is Licensee Event Report No.89-016 for the WNP-2 Plant.
This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Very truly yours,
. Powers (M/D 927M)
WNP-2 Plant Manager CMP:lg
Enclosure:
Licensee Event Report No.89-016 cc: Mr. John B. Martin, NRC - Region V Mr. C.J . Bosted, NRC Site (M/D 901A)
INPO Records Center - Atlanta, GA Ms. Dottie Sherman, ANI Mr. D.L. Williams, BPA (M/D 399) 8906200200 890613 PDR ADOCK 05000397 8 PDC
NRC Form 385 V.S. NUCLEAR AEGULATORY COMMISSION (94)3)
APPRDYED DMB No 3)504)104 LICENSEE EVENT REPORT (LER) EXPIRES SI31I88 FAC ILI'TY NAME (I I DOCKET NUMBER (2) PAGE (3i Washin ton Nuclear Plant - Unit 2
""'("Engineered Safety Feature System Actuation Caused By Inadvertent Fuse Removal and 050003971OF06 Loss of Power Due to Inade uate Fuse Labelin /Inade uate Trainin /Personnel'Error EVENT DATE (5) LER NUMBER 18) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEGVENTrAL RLvrsrON OAY eACILITY NAMES DOCKET NUMBERISI NUMBER NUMBER MONTH YEAR 0 5 0 0 0 0 514 8 9 8 9 01 6 0 0 0 6 1 3 8 9 0 5 0 0 0 OPERATING THIS AEPOATIll IS SUBMITTED PURSUANT T 0 THE REGUIREMENTs oF 10 cFR 4)I (cere>> one or morr ol mr lorlowinpt (11 MODE (0) 20.402(bl 20.405(c) X 50,73(ol(2)(ivl 73,7)(rr)
POWE R 20.405( ~ illl ii) 50.35(c)(ll 50,73(o)(2)(v) 73.7)(cl LEYEL 0 0 0 20AOS(el I 1 lbil 50.38(cl(21 50.73(o l(2) (viil OTHER ISprcily rn AOHrrct 20.405(ol(1) liiil 50,73(ol(2)(i)
OrlOW md in Trvt, IVBC perm S0.73(el(2)(niil(A) 366AI 20A05(o ) (Iv) 50.73( ~ l(2)(ii) 50,73( ~ I(2I(viii)IB) 20.405(o)(l)lvl 50 73( ~ l(2)(iiil 50.7 3 (4 I (2 I ( x I LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE J .D. Arbuckle Com liance En ineer COMPLETE ONE LINE FOA EACH COMPONENT FAILURE OESCAIBEO IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC TVRER AEPOATABLE TO NPRDS CAUSE SYSTEM COMPONENT MANVFAC TURER EPOA :~ ',-~'IYj,';.
TABLE:yR,jg<~(~g<~
SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION IIIyrr, complrtr EXPECTED SVBMISSIOrY OA TEI DATE I15)
YES NO ABSTAAcT ILimir to 1400 rpecel. I e., rpprooimrrrly RINrn rinplr rpece typrwnrtrn Ii nHI (18)
On May 14, 1989 at 0912 hours0.0106 days <br />0.253 hours <br />0.00151 weeks <br />3.47016e-4 months <br />, a Plant Reactor Operator inadvertently tripped the Division 1 and 2 offsite power supply feeders which caused a loss of power to safety related power Buses SM-7 (Division 1) and SM-4 (Division 3). The loss of power to bus SM-7 caused the Division 1 Diesel Generator to start and load bus SM-7. In addition, the loss of Division power caused the loss of power to Reactor Protection System (RPS) Bus 1
A which caused multiple Engineered Safety Feature (ESF) isolations and actuations. At the time of the event the plant was shutdown for the annual refueling and maintenance outage. Preventive maintenance was scheduled for Division 2 of the AC Distribution System. (including safety related Bus SM-8) and event. The Backup Power Supply TR-B (which powers safety related buses SM-7 and SM-8) it was inoperable prior to and during the was de-energized and unavailable.
The cause of the event was the inadervertent removal of potential transformer fuses that sense TR-S (offsite startup) line voltage and provide trip and lockout signals to breakers S-1 and S-2 (through which buses SM-1 and SM-2 are powered). As a result, off-site power was lost or unavailable to all safety related buses, and Diesel Generator 1 (DG-1) started and was relied upon to restore safety related bus SM-7 to power. The following systems were lost due to the loss of power: Residual Heat Removal (RHR)
Shutdown Cooling, Plant Service Water (TSW), Fuel Pool Cooling (FPC), Tower Makeup Water (TMU), Control and Service Air (CAS) and Control Rod Drive (CRD). The loss of power to Bus SM-7 de-engerized RPS Bus A causing an RPS half scram. The loss of RPS Bus A also causes an Outboard Nuclear Steam Supply Shutoff System (NSSSS) isolation of Groups 1 (Main Steam Line Drains only), 2, 5, 6, and 7. NSSSS Group 5 isolates RHR Shutdown Cooling. In addition, the loss of RPS A power causes some NSSSS Group 3 (Primary and Secondary Containment Ventilation and Purge Systems) and Group 4 (Miscellaneous Balance of Plant) isolations and actuations.
NRC Form 358 (9.83)
I NRC Form 3SSA (94)3) U.S, NUCLEAR REOULATORY COMMISSION LICENSEE NT REPORT (LER) TEXT CONTINUA ON APPROVEO OMB NO. 3180-O(04 EXPIRES: 8/31/88 FACILITY NAME (I) OOCKET NUMBER (2)
LER NUMBER (8) PAOE I3)
YEAR @(< SEQUF NTIAL g~R'I REVISION NUMBER NUMSSR Washington Nuclear Plant - Unit 2 0 s 0 0 03 97 8 9 0 1 0 0 0 2 0 6 TEXT ///mors spssois rsr/Irirrd, Irss sddio'ons/HRC Fonrr 3884'4/(IT)
Abstract (continued)
Plant operators restarted RPS-MG-lA and reset the RPS half scram. The operators restored power to Division 1 SM-7 through SM-1 by 0941 hours0.0109 days <br />0.261 hours <br />0.00156 weeks <br />3.580505e-4 months <br />. The Division 3 (High Pressure Core Spray) bus SM-4 power was restored by 1002 hours0.0116 days <br />0.278 hours <br />0.00166 weeks <br />3.81261e-4 months <br />. By 1017 hours0.0118 days <br />0.283 hours <br />0.00168 weeks <br />3.869685e-4 months <br /> RHR Shutdown Cooling, Plant Service Water and Control and Service Air were recovered and, at 1426 hours0.0165 days <br />0.396 hours <br />0.00236 weeks <br />5.42593e-4 months <br />, Fuel Pool Cooling was restored. The TMU System was not restarted due to the planned SM-8 outage which de-energized the discharge valve for pump TMU-P-lA.
The root causes of this event are 1) inadequate labeling of Potential Transformer Cabinet doors, 2) infrequent training of Operations personnel on pulling PT fuses, and 3) personnel error in not following procedures. Corrective actions include 1) improving the labeling of the Potential Transformer cabinet doors, 2) providing training on pulling PT fuses, and 3) counselling the individual involved.
There is no safety significance associated with this event. The Division 1 Diesel, Generator started and restored power to safety related bus SM-7 as designed, and RHR Shutdown Cooling was restored within the allowable Technical Specification time limit.
Plant Conditions a) Power Level - 0%
b) Plant Mode - 5 (Refueling)
Event Descri tion On May 14, 1989 at 0912 hour0.0106 days <br />0.253 hours <br />0.00151 weeks <br />3.47016e-4 months <br /> s, a Plant Reactor Operator inadvertently tripped the Division and 1 2 offsite power supply feeders which caused a loss of power to safety related power Buses SM-7 (Division 1) and SM-4 [Division 3: High Pressure Core Spray (HPCS)j. The loss of power to bus SM-7 caused the Division 1 Diesel Generator to start and load bus SM-7. In addition, the loss of Division 1 power caused the loss of power to Reactor Protection System (RPS) Bus A which caused multiple Engineered Safety Feature (ESF) isolations and actuations.
At the time of the event the Plant was in operational condition 5 (Refueling) with the reactor head removed, the reactor cavity flooded up and the fuel pool gates removed. In addition, buses SM-7 and SM-4 were powered from the Startup Power Supply TR-S through buses SM-1 and SM-2 and breakers Sl and S2. The Division'2 .bus SM-3 and associated safety related bus SM-8 were de-energized in maintenance. The Backup Power Supply TR-B (offsite power supply to safety related buses SM-7 and SM-8) was de-energized to prevent backfeed into the breakers scheduled for maintenance, and the Division 2 and 3 diesel generators were out of service for planned maintenance activities.
NRC FORM SddA ~ I/.S. CPOr (SSS-Ssn-SSS OOO)n (9 83)
NRC Form 38dA (94)3) U.S, NUCLEAR REGULATORY COMMISSION LICENSEE E NT REPORT (LER) TEXT CONTINUATION APPROVED OMS NO. 3150&104 EXPIRES: 8/31/88 FACILITY NAME (1) DOCKET NUMBER (1)
LER NUMBER (8) PAGE (3)
SEOVENTIAL REVISION NVMSSR NUMss/I Washin ton Nuclear Plant - Unit 2 o3 97 89 0 1 6 000 3 OF TEXT /llmors 4/rssois rsrlrrlrsd, oss sddr(r'oos/HAC Form JSSA'4/ (IT)
The event occurred when the reactor operator implemented the last action on a Danger Tag Clearance Order which was described as UE-PT-SM3/1 Fuses (3) Auxiliary Cubicle". On examining the SM-3 Auxiliary Cubicle the reactor operator was confronted with two internal cabinets, one over the other, reading "Bus Potential Transformers" on the upper cabinet and "Line Potential Transformers" on the lower.
The PT fuses are located inside the cabinet doors and opening the doors removes the associated PT fuses from the circuit. The designations UBusR and "Line" Potential Transformers were the only labels in the cubicle. In an attempt to relate the Clearance Order EPN to the auxiliary cubicle labels, the operator consulted with other reactor operators and the Work Control Center Group for determining the appropriate equipment on the clearance order. The operator also reviewed the appropriate Electrical Wiring Diagram (EWD) to determine the correct fuses to be pulled. The operator felt that he had determined from the drawing that the two sets of fuses in the cubicle were in series and were the appropriate fuses to be pulled.
He then removed the UBus Potential Fuses" from the circuit. Although these were the correct fuses, he was expecting to see two fuses but found three and questioned which fuses should be pulled. During this process the operator failed to involve Operations supervision as required by procedure.
As a result of further review of the EWD and subsequent discussions with other individuals, the operator felt he had now identified the correct fuses. The operator then proceeded to the auxiliary cubicle and also pulled the "Line Potential Fuses," causing the loss of power to SM-1 and SM-2. This action was beyond the scope of that provided in the Clearance Order.
The loss of power to Class lE Bus SM-7 caused the Division 1 Diesel Generator to start and load Bus SM-7. The loss of power caused the following systems to be temporarily lost: RHR (Shutdown Cooling), Plant Service Water (TSW), Fuel Pool Cooling (FPC), Control Rod Drive (CRD), Tower Makeup Water (TMU) and Control and Service Air (CAS).
In addition, the loss of RPS A caused an Outboard Nuclear Steam Supply Shutoff System (NSSSS) isolation. The outboard isolations occurred for NSSSS Group 1 (Main Steam Line Drains only), Group 2 (Reactor Water Sample valves), Group 5 [Residual Heat Removal (RHR) and Traversing In-Core Probe (TIP) Systems], Group 6 (RHR Shutdown Cooling), and Group 7 (Reactor Water Cleanup System). In addition, loss of RPS A power causes some NSSSS Group 3 (Primary and Secondary Containment Ventilation and Purge System) and NSSSS Group 4 (Miscellaneous Balance of Plant) isolations and actuations. The Standby Gas Treatment (SGT) System also started on loss of power to RPS Bus A.
At the time of the event, RPS-Bus-B had previously been transferred to alternate power and was not affected by the event. In addition, the HPCS System had previously been isolated for maintenance.
NRC FORM 388A ~ V.S. CPOr )r/88-81O-SS&/OOO)O (84)3)
NRC Form 368A (94)3) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE E (=NT REPORT ILER) TEXT CONTINUATION APPROVED OMB NO, 3150W104 EXPIRES: 8/3)/88 FACILITY NAME (I) OOCKET NUMBER (2)
LER NUMBER (6) PACE (3)
~+'O SEQUENT/Al YEAR NUMBBA 'O NUMBBA Mashin ton Nuclear Plant - Unit TEXT llfmoss space ls seooked. use addio'ooa/l/RC Form 355A'sl (IT) 2 05000397 89 01 0 0 4 OF Immediate Corrective Action Plant operators restarted RPS-MG-lA and reset the RPS half scram. By 0941 hours0.0109 days <br />0.261 hours <br />0.00156 weeks <br />3.580505e-4 months <br /> the "Line Potential Transformer" fuses had been reinserted and TR-S power returned to SM-7 with DG-1 in idle. SM-4 power was restored by 1002 hours0.0116 days <br />0.278 hours <br />0.00166 weeks <br />3.81261e-4 months <br />. By 1017 hours0.0118 days <br />0.283 hours <br />0.00168 weeks <br />3.869685e-4 months <br /> RHR Shutdown Cooling had been returned to service as had the rest of the systems listed above, with the exception of Fuel Pool Cooling which was returned to service at 1426 hours0.0165 days <br />0.396 hours <br />0.00236 weeks <br />5.42593e-4 months <br />. The TMU System was not restarted due to the planned SM-8 outage which de-energized the discharge valve for pump TMU-P-1A.
Further Evaluation and Corrective Action A. Further Evaluation
- 1. The starting of the Division 1 Diesel Generator and the Nuclear Steam Supply Shutoff System isolations and actuations are Engineered Safety Features and; therefore, this event is reportable per 10CFR50.73(a)(2)(iv).
- 2. Had the backup power supply bus TR-B been available, relay logic would have allowed Breaker B-7 to energize SM-7 and return power to the RPS-MG-1A before the NSSSS isolation actuations occurred. Flywheel energy in the RPS-MG-lA would have carried transient. In addition, Backup Power Supply TR-B would have re-powered it through the loss of power SM-8 if it had been operable. The Division 2 and Division 3 Diesel Generators would have also started if they had been operable.
no other structures, components, or systems inoperable prior to the event There were that contributed to the event.
- 3. The root causes of this event are as follows:
~ Inadequate labeling of the RBusR and "Line" Potential Transformer cabinet doors. Had the appropriate Equipment Part Number (EPN) label been affixed to the cabinet doors, the operator would have been able to determine and pull the correct PT fuses.
~ Infrequent PT fuse training of Operations personnel. Pulling PT fuses is not frequently performed by operators and, as a result, training as to designation, significance, and orientation is normally not covered in refresher training.
~ Personnel error. The reactor operator failed to involve Operations supervision as required by procedure when potential problem existed.
it was determined that a In addition, the operator expanded the scope of the Clearance Order without authorization to do so. The operator had pulled five fuses instead of three as designated by the Clearance Order. Plant procedures were not a cause of this event.
NAC FOAM 38BA ~ I/.S. CFOG (988-820-889 000)0 (9 831
NRC Form 36&A (9413) U.S. NUCLEAR AEGULATOAYCOMMISSION LICENSEE E NT REPORT (LER) TEXT CONTINUATION APPAOVEO OMS NO, 3150WI0&
EXPIRES: 8/31/88 FACILITY NAME (11 OOCKET NUMBER (31 LER NUMBER (6I PAGE (3)
YEAR h SEOVENTIAL REVISION NVMS&R gpss N VMS&A Washin ton Nuclear Plant - Unit TEXT lifmore epeee ie rerfofred, Fee eddf(lone/ NRC Form 36EA'ef (171 2 0 5 0 0 0 3 9 7 0 1 O 5'"O B. Further Corrective Actions
- 1. SM-3 Auxiliary Cabinet and similar cabinet labeling will be improved to eliminate the possibility for inaccurate identification of Potential Transformer fuses.
- 2. The Operations department will provide training to operators as to designation, significance, and orientation of the "Line" and "BusU Potential Transformers in the SM-3 Auxiliary Cabinet and similar cabinets.
- 3. The reactor operator involved was counselled on 1) the importance of informing Operations supervision when a problem is discovered during the clearance order process, and 2) the importance of following procedures.
- 4. This LER will be required reading for all Plant Operators (Licensed and Non-Licensed).
- 5. A double verification program for clearance order implementation is currently required prior to removal and reinstallation of fuses in the control room. The Operations department will evaluate expanding this program beyond the control room.
Safety Si nificance There is no safety significance associated with this event. The Division 1 Diesel Generator started and repowered Bus SM-7 as designed. At the time of the event the reactor water level was greater than 22 feet above the reactor vessel flange which provides a large heat sink for core cooling and adequate time to restore RHR Shutdown Cooling. Residual Heat Removal Shutdown Cooling was restored within the allowable Technical Specification time limit. Additionally, no Plant condition requiring the ESF isolations and actuations existed and all ESF isolations and actuations occurred as designed. Accordingly, this event posed not threat to the health and safety of the public or Plant personnel.
Similar Events88-021 EIIS Information Text Reference EIIS Reference System Component Bus SM-7 (Div. 1) and SM-4 (Div. 3) EB SWGR Diesel Generator DG-1 EK DG Reactor Protection System (RPS) JC RPS-Bus-A JC BU Bus SM-8 (Div. 2) EB SWGR NRC FORM 3&&A AVAST CPOs 1888-530 58$ r00010 (8831
NRC Form 388A U.S. NUCLEAR REGULATORY COMMISSION (9 83)
LICENSEE -NT REPORT (LER) TEXT CONTINUA N APPROVEO OMB NO, 3(50&)04 EXPIRES: Bl3(l88 FACILITY NAME (I ) OOCKET NUMBER (31 LER NUMBER (6) PAGE (3)
YEAR SEGVENTIAL os% REVISION NUMB'EA V R NVMBEA Washin ton Nuclear Plant - Unit TEXT fllmoro opoooi4 roqolrod, 044 oddidonoi HRC Form 388A 3) (17) 2 o s << o 3 9 7 8 9 0 1 6 00 06 OF 0 6 EIIS Information Text Reference EIIS Reference System Component TR-B and TR-S EA XFMR Breakers S-1 and S-2 EA BKR Bus SM-1 and SM-2 EB BU Residual Heat Removal (RHR) System (Shutdown Cooling) BD Plant Service Water (TSW) System KG Fuel Pool Cooling (FPC) System DA Tower Makeup Water (TMU) System KI Control and Service Air (CAS) System LD Control Rod Drive (CRD) System AA Nuclear Steam Supply Shutoff System (NSSSS) BD Primary and Secondary Containment and Purge Systems VH RPS-MG-lA JC MG TMU-P-lA KI P Diesel Generator DG-2 and DG-3 EK DG Fuses E-PT-SM3/1 EA FU Main Steam Line Drain Valves SN LOV Reactor Water Sample Valves AD ISV Traversing In-Core Probe (TIP) System IG Reactor Water Cleanup (RWCU) System CE Standby Gas Treatment (SGT) System. BH RPS-Bus-B JC BU High Pressure Core Spray (HPCS) System BG NRC FORM 3@BA
~ V.ST QPOa (986-530-589(00070 (94)3)