ML17223A857
| ML17223A857 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 07/10/1990 |
| From: | Crlenjak R, Elrod S, Madden P, Michael Scott NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17223A854 | List: |
| References | |
| 50-335-90-14, 50-389-90-14, GL-88-17, NUDOCS 9007260095 | |
| Download: ML17223A857 (35) | |
See also: IR 05000335/1990014
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
ATLANTA,GEORGIA 30323
Report Nos:
50-335/90-14
AND 50-389/90-14
Licensee:
Florida Power
5 Light'ompany
9250 West Flagler Street
Miami, FL
33102
Docket Nos.:
50-335
and 50-389
Facility Name:
St. Lucie
1 and
2
License Nos.:
and
Inspection
Conducte
Inspectors
ay
- June
11,
1990
S.
.r
,
e ior
esi.
e t Inspector
Mdpr~
M.
.
catt,
R
i en
ns
ec or
at
ig e
at
Ss
ne
Approved By:
P.
.
ad
Reactor
Ins ector
Dat
Signe
P yO
R.
V. Cr enJa
ction
Ch'ivision
of Reactor Projects
Da
Si
ed
SUMMARY
Scope:
This routine resident
inspection
was
conducted
onsite
in the
areas
of plant
operations
review, maintenance
observations,
surveillance
observations,
review
of nonroutine events,
and followup of Generic 'Letter 88-17.
Results:
The licensee's
focus this inspection
period
was
power operation of both units
and
completion of the wrap-up from the recently
completed
Unit
1 refueling
outage.
Response
to minor equipment failures
was rapid.
Planning for the
upcoming Unit 2 refueling outage
was increasing in tempo.
Within the scope of
this
inspection,
the
inspectors
determined
that
the licensee
continued
to
demonstrate
satisfactory
performance
to ensure
safe plant operations.
Within the areas
inspected,
the following violation was identified:
Failure to follow a test procedure,
paragraph
3.
1
REPORT
DETAILS
Persons
Contacted
Licensee
Employees,
- D. Sager,
St. Lucie Site Vice President
- G. Boissy, Plant Manager
J.
Barrow, Operations
Superintendent
J; Barrow, Fire Prevention Coordinator
- R. Church,
Independent
Safety Engineering
Group
H. Buchanan,
Health Physics
Supervisor
C. Burton, Operations
Supervisor
C. Crider,
Outage Supervisor
- D. Culpepper,
Site Engineering
Supervisor
- R. Dawson,
Maintenance
Superintendent
- R. Decker,
Plant Licensing Engineer
- R. Englmeier, guality Assurance
Superintendent
R. Frechette,
Chemistry Supervisor
C. Lep'pla,
IKC Supervisor
L. McLaughlin, Plant licensing Superintendent
L. Rogers,
Electrical Maintenance
Supervisor
J.
Dyer, guality Control Supervisor
N. Roos,
Services
Manager
- D. West, Technical Staff Supervisor
J.
West,
Mechanical
Maintenance
Supervisor
W. White, Security Supervisor
G.
Wood, Reliability and Support Supervisor
- E. Wunderlich, Reactor Engineering
Supervisor
Chairman
Other
licensee
employees
contacted
included
engineers,
technicians,
operators,
mechanics,
security force members
and office personnel.
- Attended exit interview
and initialisms
used
throughout this report are listed in the
last paragraph.
Review of Plant Operations
(71707)
Unit
1 began
the inspection
period at power, but was manually tripped
on
May 24,
when
an o-ring failed in the turbine hydraulic control
system.
It was restarted
later that day following turbine hydraulic control
system
repair.
The unit was
placed on-line
on
May 25,
and
ended
the inspection
period
on day
17 of power operation.
Unit 2 began
and
ended
the inspection period at power,
day
145 on line.
A
Unit
2 maintenance
and refueling
outage
was
announced
to begin
about
September
15,
1990.
Plant Tours
The
inspectors
periodically conducted
plant= tours to verify that
monitoring
equipment
was
recording
as
required,
equipment
was
properly tagged,
operations
personnel
were aware of plant conditions,
and plant housekeeping
efforts were
adequate.
The inspectors
also
determined
that
appropriate
radiation
controls
were
properly
established,
critical clean
areas
were being controlled in accordance
with procedures,
excess
equipment or material
was stored properly and
combustible
materials
and
debris
were
disposed
of expeditiously.
During tours,
the
inspectors
looked for the existence
of unusual
fluid leaks,
piping vibrations,
pipe
hanger
and seismic restraint
settings,
various
valve
and breaker positions,
equipment caution
and
danger
tags,
component
positions,
adequacy
of fire fighting
equipment,
and
instrument
calibration
dates.
Some
tours
were
conducted
on backshifts.
The frequency of plant tours
and control
room visits by site management
was noted to be adequate.
The inspectors
routinely conducted partial walkdowns of ESF,
and
support
systems.
Valve, breaker,
and switch lineups
and equipment
conditions
were
randomly verified both locally and in the control
room.
The following accessible-area
ESF system
walkdowns were
made
to verify that
system
lineups
were
in accordance
with licensee
requirements
for operab'ility
and equipment material
conditions
were
satisfactory:
Unit
1 pipe penetration
room; Unit
1 pipe tunnel; Unit
1
CST; Unit 2 pipe penetration
room;
and Unit 2 fuel unloading area
and
SFP.
During
a tour, Unit
1
CST level transmitter
LT-12-12 bracket
was
observed
to
be
mounted
to
a vertical pipe using only
a U-bolt
rather
than the usual U-bolt and
two through bolts.
The bracket
was
a cut away version of the bracket normally used at St. Lucie
for Rosemount
brand transmitters.
The seismic qualities
were
questioned
based
on this observation.
A seismic
report
was
produced
addressing
Rosemount
model
1152 transmitters
mounted
on
the cut away bracket
which was attached
to
a substantial
plate,
but it did not address
brackets
mounted to pipes.
The licensee
is reviewing this
area
in more depth.
The drawing for this
foundation,
JPN-174-190.002,
Instrument
Installation Details,
primarily addressed
a different brand transmitter or a different
location/style
transmitter.
NCR 1-513,
submitted
by the
IKC
group,
resulted
in
174-190D
which
changed
the
drawing
reference
and mounting details for LT-12-12 to those applicable
to LT-12-11 in identical service.
The
new reference
specified
a
solid side
mount attached
to the pipe with
a U-bolt and
two
through bolts.
During tours,
both units'ipe penetration
rooms exhibited poor
housekeeping.
Debris,
unwanted drip catches,
excessive
tube for leaking valves,
ladders,
staging/scaffolding,
and
unstowed
outage-related
material
were prevalent.
Some of the
more relevant
problems
were'.
The Unit
2
room
had
a
blow down valve that
was leaking
steaming
moisture at
a rate that
caused
condensation
to drip
from components
in at least
one half of the room's overhead.
The water vapor in the Unit
2
room
had
caused
rusting of two
containment
ends;
the
rust
appeared
to
be
superficial.
The Unit
2
room
had
three
high pressure
3/8 inch instrument
tubes
damaged/bent
(pressurizer
steam
space
sample,
steam
blow
down
sample,
and pressurizer
surge
sample lines).
The tubing
and
associated.
appeared
to
have
been
damaged
while
working abov'e
the tubing.
The
damaged
lines, were not part of
the unisolable
RCS boundary.
Scaffolding in the Unit 2 room could hinder handwheel
operation
of several
manual
valves.
Once
the problems
were identified, the licensee
took prompt correc-
tive actions.
Upon re-inspection
of the Unit
1 pipe penetration
room
on June
2,
after
some
refurbishment,
the
space
was
found to
be
improved
and
reduced
Health Physics controls could be applied.
Two blowdown valve
steam
leaks
had
appeared
since
the cleanup effort.
One of them was
wetting about
one third of the
space.
This was identified to plant
management
and the leaks
were repaired.
The licensee
recognized
that they
had not been conducting sufficient
walkdown
inspections
of the
pipe penetration
rooms
and
took
two
additional
steps
to enhance
control of them:
)
The
pipe penetration
rooms
were
added
to the weekly walkdown
tour schedule.
The training programs for operators
and other selected
personnel
were
being
reviewed
for
enhancements
concerning
material
condition observation
and reporting.
During
a tour of Unit
1
ICW areas
on Nay 30,
a number of areas
of improved material
conditions
were noted.
Some
exceptions
identified to the plant staff were
promptly addressed.
Two
notable
exceptions
were safety-related
valves
FCV 21-3B and
21-3A, which isolate the lubrication water to the main ci rculat-
ing pumps
upon
ESF actuation.
Though the valves would function,
the
air-pressure-to-open,
spring-pressure-to-close
tubular
operators
were significantly deteriorated
such
that future
operation
could
be affected.
Both valves
were
placed
out of
service
and closed
pending repair.
4
b.
Plant Operations
Review
The
inspectors
periodically
reviewed shift
logs
and
operations
records,
including data
sheets,
instrument traces,
and
records
of
equipment malfunctions..
This review included control
room logs
and
auxiliary logs,
operating
orders,
standing
orders,
jumper logs
and
equipment tagout records.
The inspectors
routinely observed
operator
alertness
and
demeanor
during
plant
tours.
During routine
operations,
control
room staffing,'ontrol
room access
and operator
performance
and
response
actions
were
observed
and evaluated.
The
inspectors
conducted
random
off-hours
inspections
to assure
that
operations
and security
remained
at
an acceptable
level.
Shift
turnovers
were
observed
to verify that
they
were
conducted
in
accordance
with
approved
licensee
procedures.
Control
room
status
was Verified.
The inspectors
reviewed
the following safety-related
tagouts
(clearances):
1-4-2,
tags
84 to 88,
Train
"B" MSIV Control Air Solenoid
Valves;
1-4-34,
tags
1
and
2 for V6461 and V6363,
sample line isolation
'alves for the equipment drain tank
and the chemical drain tank,
respectively;
1-6-42,
Replace
FCV-21-3B Actuator;
1-6-56, Repair
FCV-21-3B Flanges;
and
2-5-112,
Repair
2B
ICW Pump.
On May 24, Unit
1 operators
manually tripped the reactor
due to
a
DEH fluid (hydraulic oil) leak from the number three governor
valve's
servo valve.
The servo valve, which had
begun leaking
in the early morning,
was isolated for repair after
a
10 percent
power reduction.
The valve cover, which also served
as
a spray
shield,
was
removed
to facilitate replacing
the five o-rings
between
the servo valve body and mounting plate
and
was left off
following repair
to
enable
the
observation
of
any
minor
post-repair
leakage.
Valving-in the
servo
valve initiated
a substantial
new leak
'hat,
with the valve cover/spray
shield
removed,
could not
be
isolated.
At that point, with turbine
DEH control
pressure
decreasing,
the operations
staff manually tripped
the plant
before the turbine low oil pressure trip setpoint
was reached.
Close examination'f
the o-ring set initially removed
from the
servo
valve
and
the
second
set installed
during
the repair
revealed
that
both sets
of o-rings
were oversized.
Improper
o-ring retention in the retaining grooves
caused
both leaks.
The
o-rings,. which
were
non-safety-related,
were
improperly
identified in the
FPL stock system.
The licensee
replaced all Unit
1
turbine
valve o-rings
and
issued
a
SNOW
NPWO to replace
those
located
on
the
Unit
2 turbine
valves.
There
were
no
known
safety-related
applications for these
specialized
o-rings.
During the plant trip, all equipment
responded
appropriately except
a
6.9
KY breaker
that did not
make
a 'rapid transfer
from the unit's
main to auxiliary transformer;
this tripped
two
and
one
MFP.
During the recovery after the trip, the tripped
and
MFP were
restarted.
Subsequent
testing
by the licensee
could not duplicate
the problem.
On
May 17, Unit
2 experienced
indications of
a
2A main feed water
regulating
valve
control
problem.
Recording
chart
indication
displayed
about
a
ten
percent
variation in
2A
SG level without
corresponding
fluctuations of power or other parameters.
Operations
personnel
took manual
control of the
2A main feed regulating valve
and established
that the controller was working properly.
The technical
support staff instrumented
the feed regulating
system
control features
and,
SG level indication to determine
the cause for
the erratic indications.
Initially, it was found that the recorder
had
worn parts.
Its mechanical
wear
was causing
a
4 to
6 percent
indication swing.
Further investigation
was continuing at the
end of
the inspection
period.
A containment
entry was
planned
to evaluate
the process
signals
from SG level transmitters.
On May 29, the Unit 2 "A" train containment
vacuum relief valve,
25-7,
low pressure
alarm
was actuated
by pressure
switch
PIS25-12A.
The accumulator air pressure
provides
stored
energy to
open
the
valve
on
a
low differential
pressure
between
the
containment
and
the
(less
than
-0.07 psig).
The
low
pressure
alarm could
have
meant that stored
energy
was
not available to open the valve if called upon.
Based
on the annunciator indication, the site properly entered
the
TS 3.6.5 four-hour action
statement
for an
inoperable relief valve.
Inspection
and test
by
18C
personnel
indicated
that
pressure
was about
70 psig
and the action statement
was exited.
Further review revealed:
That
PIS25-12A
was
non-safety-related,
had
no calibration
schedule,
and
had not been calibrated
since
1982.
As
a previous
coranitment
to the
NRC,
the
licensee
was
in the
process
of
finding
such
instruments
and
placing
them
on
a calibration
schedule.
That the
PIS25-12A alarm setting
had drifted several
psig high
and caused
the annunciator
alarm.
11
The
PIS25-12A
70 psig
set point agreed
with the set point
document supplied
by engineering.
This set point disagreed
with
the
50 psig
CWD set point; engineering
was looking into why the
CWD had not been
updated.
That the actual
operation of
FCV 25-7 was controlled
by another
detector that would have performed the actual
safety function if
required
and
had
been calibrated
on its required schedule.
The inspectors
reviewed quality control activities
and findings
to determine if the objectives
were being met.
The documented
final results
of the following types
of activities
were
sampled:
Field welds in safety-related
pipe (corrective actions only);
gC hold points in electrical
procedures;
Inspection of stuffing boxes for charging
pumps;
and
Post maintenance
cleanliness
inspections.
The activities were in order
and appropriate corrective actions
were
completed.
c.
, Technical Specification
Compliance
Licensee
compliance with selected
TS
LCOs was verified. This included
the
review
of
selected
surveillance
test
results.
These
verifications
were accomplished
by direct observation
of monitoring
instrumentation,
valve positions,
and switch positions,
and by review
of completed
logs
and records.
The licensee's
compliance with
LCO
action
statements
was
reviewed
on
selected
occurrences
as
they
happened.
The inspectors
verified that plant procedures
involved
were
adequate,
complete,
and the correct revision.
Instrumentation
and recorder traces
were observed for abnormalities.
d.
Physical
Protection
The inspectors verified by observation
during routine activities that
security program plans
were being implemented
as evidenced
by: proper
display of picture badges;
searching
of packages
and personnel
at the
'lant entrance;
and vital area portals
being locked
and alarmed.
The inspectors,
as
a result of routine plant tours
and various operational
observations,
determined
that
the
general
plant
and
system
material
conditions
were
being satisfactorily
maintained,
the
plant security
program
was
being effective,
and that the overall
performance
of plant
operations
was
good.
Areas of weak
housekeeping
controls
were quickly
corrected.
No violations or deviations. were identified.
3.
Survei 1 lance Observations
(61726)
Various
plant
operations
were verified to
comply with selected
TS
requirements.
Typical of these
were confirmation of TS compliance for
reactor
coolant chemistry,
RMT conditions,
containment
pressure,
control
room ventilation
and
and
DC electrical
sources.
The
inspectors
verified
that
.testing
was
performed
in
accordance
with
adequate
procedures,
test instrumentation
was calibrated,
LCOs were met,
removal
and restoration
of the affected
components
were accomplished
properly,
test results
met requirements
and
were reviewed
by personnel
other than
the individual directing the test,
and that
any deficiencies
identified
during the testing
were properly
reviewed
and
resolved
by appropriate
management
personnel.
The following surveillance tests
were observed:
OP 2-0110050,
Rev 9, Control
Element Assembly Periodic Exercise;
OP
3200051,
Rev 6, At Power Determination of Moderator Temperature
Coefficient and
Power Coefficient (performed
on Unit 2);
18C
2-1400052,
Rev
16,
Engineered
Safeguards
Actuation System-
Channel
Functional Test;
Procedure
1&C 2-0700051,
Rev
System Monthly
Functional Test;
Procedure
AP 1-0010125A,
Rev 15, Surveillance
Data Sheets,
Data Sheet
number 26, Accident Monitoring Instruments;
and
OP
1-0120051,
Rev
10,
Flow Determination
by Calorimetric
Procedure.
During the Unit 2 performance of OP 3200051,
CEA 56 froze in position
while the active control
group
was being returned to its full power
position.
The rest of the control
group
moved
several
more steps
before
the
operator's
action
stopped
group
movement
prior to
receiving
a group deviation alarm.
Operations
took the proper steps
to remedy the situation
by contacting
I8C personnel.
Control logic
was reset
by driving the
CEA back into the core in manual
individual
mode.
The clearing of the logic did not identify the cause for the
freeze.
The test itself was not invalidated
by the delay to realign
CEA 56 and its results
were satisfactory.
The history of this unit's
CEA control circuits indicated that the
associated
ACTH cards
occasionally
froze
CEAs for unexplained
reasons.
ACTH cards function to monitor
CEA position
and to prevent:
rod
drops
and slips;
CEDM coil
burnouts;
and
CEA group
deviations.
In its attempt to perform the above functions,
the
ACTM card complex
logic sometimes
froze the
CEA at inappropriate
times but would not
prevent
the
CEA from dropping into the core
on
a reactor trip.
One
of the
problems with the cards
was that the card did not store
the
information regarding
the
cause for'ts decisions;
storage of such
information would enhance
CEDM troubleshooting. '&C plans to have
card
memory additions
available for card modification during the
September,
1990, refueling outage.
Procedure
I&C 2-1400052
was performed during prototype testing of new
circuit boards for the upcoming Unit 2
ESF system
ATWS modification.
Design
engineers
from Consolidated
Control,
Inc,
the
equipment
vendor,
provided the prototype circuit boards
and participated
in the
test.
The licensee
generated
safety evaluation
FLO 128-35.5007,
Rev
.
0, for the test
and
issued
detailed
instructions
in
NPWO 1244/70.
Although several
minor problems
were identified during testing,
the
overall result of the real
time prototype
assessment
was
an enhanced
modification
process.
The
I&C surveillance
procedure
was later
utilized
as
a functional
check of the existing
system
when it was
returned
to service.
Procedure
I&C 2-0700051,
Rev 13, Auxiliary Feedwater
System Monthly
Functional
Test,
tested
the bistables,
the automatic initiation, and
the control
system that integrated
the actions of the
combined
output.
The testing
was well controlled
and observed
results
were
satisfactory.
Procedure
AP 1-0010125A,
Rev 15, Surveillance
Data Sheets,
Data Sheet
26,
Accident
Monitoring
Instruments,
checked
the
status
and
operability of the various
instruments
used during an accident.
The
surveillance
was performed to satisfy
requirements.
The "A" train liquid plasma display, normally used for indication and
for. data gathering
during performance
of the
CET and
HJTC procedure
segments,
had
been
shut
down since
March
11
due to partial readout
failure.
The data fields would become
garbled
soon after the screen
was either energized
or reset.
The cause
was thought to be
a strong
field adjacent
to the display.
With the
"A" display shut
down, operations
could not complete
the
surveillance
using the
RVLMS back panel for data collection because:
No
I&C personnel
were
on shift on Saturday,
June
2, to supply
expertise
or calibrated
equipment;
The existing test did not address
use of the
RVLMS back panel
for data collection;
and
No operations
personnel
knew
how to
make
the
necessary
math
conversions
from an auxiliary read out on
a back panel.
The test
was deferred until the June
4,
when
I&C energized
the
"A"
train display
and operations satisfactorily collected
the data prior
to the display becoming garbled.
The "A" train display
was then left
in operation
and available for operator
use
on
a reset-to-read
basis.
This deferral
was acceptable
from a regulatory standpoint.
I&C persons
indicated that the display would require modification to
operate
properly
and
that
a modification
would
require
Juno
engineering
support.
ISC had not submitted
a request for engineering
support at the time of the test.
Operations
was discussing
potential
modifications with IKC to support display modification/repair during
the September,
1990, refueling outage.
The
"A" and "8" train plasma display information was. utilized in the
site's off normal
procedures.
Similar information utilizing the
same
inputs,
but processed
by
a different computer
program with slightly
different results,
was available
from the
fRDADS which, though not TS
controlled,
was also displayed
in the control
room on another
CRT.
At the time of the test,
the operations
personnel
were not fami liar
with the
computer
program
involved with the
ERDADS computation.
Althou'gh operator efficiency may
be
reduced
by having to reset
the
display prior to each
use,
regulatory requirements
are being met.
-The performance
of
OP
1-0120051,
Rev 10,
Flow Determination
by
Calorimet'ric Procedure,
was observed
on
May 14.
This
was
a precise
test
based
on highly accurate
measurements
of loop temperatures.
It
is normally performed
once per operating
cycle following refueling to
confirm adequate
loop flow.
The measurements
were
made
by disconnect-
ing (by switches)
certain
panel
meters
to reduce
measurement
channel
'loading
and
then
measuring
appropriate
channel
voltages
with
a
high-impedance
digital volt meter.
The procedure
required taking at
least ten data sets while plant parameters
remained
near constant.
During the test,
the licensee's
staff did not follow instruction
steps
8.3 through 8.6.
These
steps
directed certai.n action sequences
involving coordination with the
RCO at
the control
board,
control
board
loop temperature
meter switch position selection,
and confirm-
ation that measurements
were being
made only on channels
that had the
meter disconnected
by switches.
The test
persons
instead utilized an
unapproved
method to isolate the loop temperature
meters
and complete
the
data
without coordination.
During the test,
the inspector
questioned
the approval of the technique
in use.
No temporary
change
was
sought.
The licensee,
subsequent
to test completion,
confirmed
the resulting
data validity.
Subsequent
to the test,
a procedure
change
was initiated to upgrade
the procedure
and corrective actions
were taken to sensitize
the test staff to strict, procedure
adherence.
Procedure
gl 5-PR/PSL-1,
Rev 37, Preparation,
Revision,
Review/Approval
of Procedures,
section
5.5,
implemented
10 CFR 50 Appendix
8,
Criterion 5,
through
the
approved
FPL topical
gA report,
and also
implemented
TS 6.8. 1,
which required
that certain
procedures
be
established,
implemented
(followed),
and maintained.
Procedure
gI
5-PR/PSL-1
required that procedures
be strictly adhered
to. It also
provi.ded
the
method to obtain
approved
temporary
procedure
changes
10
and, if appropriate,
subsequent
permanent
changes.
Failure to adhere
to the
OP was identified as violation 335/90-14-01.
The
inspectors
determined
that
the
above
testing activities
were
performed in a satisfactory
manner
and met
TS requirements
except for
the
one violation discussed
above.
4.
Maintenance
Observation
Station
maintenance
activities involving selected
safety-related
systems
and
components
were
observed/reviewed
to
ascertain
that
they
were
conducted
in accordance
with requirements.
The following items
were
considered
during this review:
LCOs were met; activities were accomplished
using
approved
procedures
functional
tests
and/or calibrations
were
performed prior to returning
components
or systems
to service; quality
control records
were maintained; activities were accomplished
by qualified
personnel;
parts
and
materials
used
were
properly certified;
and
radiological
controls
were
implemented
as
required.
Work requests
were
reviewed to determine
the status
of outstanding
jobs
and to assure
that
priority was
assigned
to safety-related
equipment.
Portions
of the
following .maintenance activities were observed:
NPWO 2077/62
performed
PHs
on the "A" train Zurn strainer,
SS-21-3A1,
for the safety-related
ICW
pump lubricating water
system.
The
strainers
had
been rebuilt in September
1989,
as part of an upgrade
program based
on
NRC inspection findings at that time.
PN activities
were
being appropriately
conducted
and
the
disassembled
strainers
appeared
to be in good physical
shape.
NPWO 5138/62
was written to replace
the burned out lights in the Unit
2 SFP.
The job grew from minimal health physics preparation with the
lights
being
replaced
in their standards
at pool
side to maximum
ALARA considerations
including
use of air-fed hoods,
hot particle
controls,'nd
the
submerged
light standards
being entirely
replaced.
The old standards
were to
be
reworked in
a controlled
space
separate
from the
SFP.
The electricians
involved were taking
more
than
adequate
interest
in revising
,the
scope
and
making
preparations
for the work.
NPWOs 0904/62
and 0905/62
replaced
the monel shaft sleeves
on the
2A
and
28
ICW pumps
because
of accelerated
corrosion.
The shaft sleeves
were pitted
such
that maintaining
proper
packing
leak off was
difficult.
NCR 2-331
was written to obtain resolution for apparent
galvanic cell
corrosion
between
the
per-plan
impregnated
packing
material
and
the
adjacent
monel
shaft
The
engineering
resolution,
which will occur after this
inspection
period,
may require
a change of packing material.
For those
maintenance
activities observed,
the inspectors
determined that
they
were
conducted
in
a satisfactory
manner
and that
the
work was
properly performed
in accordance
with approved
maintenance
work orders.
No violations or deviations
were identified in the
performance
of the
above
NPWOs.
Pe
5.
Onsite
Followup of Written Nonroutine
Event
Reports
(Units
1
and
2)
(92700)
LERs were reviewed for potential
generic
impact, to detect trends,
and to
determine
whether corrective
actions
appeared
appropriate.
Events that
were reported
immediately were reviewed
as they occurred
to determine if
the
TS were satisfied.
LERs were reviewed in accordance
with the current
(Closed)
LER 50-335/89-03,
on
Low Steam
Generator
Water Level
During Startup
Due to Procedural
Deficiency
(Refer to
NRC IR 50-335/89-20).
On July 17,
1989, during.a turbine startup,
the reactor tripped
as
a
result of inadequate
flow to the
steam
generators.
Main
flow to the
steam
generators
was
prevented
because
main
block valves
MV-09-5 and
MV-09-6 were not opened.
This
event
can
be attributed to
a deficiency in procedure
OP 1-0030124,
Turbine
Startup
Zero
to Full
Load,
which did not require
the
operators
to verify the position of the feedwater
block valves.
The
inspector
reviewed
procedure
OP 1-003124,
Rev 48,
and
OP 2-0030124,
Rev 34,
and verified that these
procedures
now require valves
MV-09-5
and
MV-09-6 to
be
open
when transferring
feedwater control from the
15'4 feed regulating valves to the main feed regulating valves.
The
inspector
found the licensee's
corrective actions
to be acceptable.
This item is closed.
(Closed)
LER 50-335/90-04,
Inadvertent Partial Actuation of "A" Train
Containment Isolation
and Containment
Spray
Systems
Due to Equipment
Malfunction (Refer to
NRC IR 50-335/90-08).
On
February
28,
1990,
Unit
1
was
in
Mode
6
when
an inadvertent
partial
actuation
of the
occurred.
Train
"A" of the
containment
spray
and the containment isolation system
were partially
actuated.
The root cause
of the event
was
equipment malfunction.
The licensee
found several.
loose
screws
on
a terminal
board that was
being worked.
Attaching
a jumper wire to that terminal
board
(TB519)
during the work activity caused
the connections
to be jarred loose,
breaking
the circuit,
and partially initiating the
The
licensee's
investigation determined that the majority of the terminal
screws
were tight and that the most likely cause of the loose
screws
was
not being fully tightened
during initial installation.
The
inspector
verified that
the
licensee
initiated
and
completed
PWO
61-6254
and
61-6219 to verify and check tightness
of the
ESFAS panel
terminal connections.
This Item is closed.
(Closed)
LER 50-389/89-03,
Inadvertent
Actuation of Containment
Isolation Actuation Signal
Due
To Personnel
Error (Refer to
NRC IR
50-389/89-10).
12
On March 21,
1989 with Unit 2 in Mode 6,
a CIAS was received.
This
inadvertent
actuation
was
a result of a personnel
error.
Licensee
personnel
(licensed
operator)
depressed
the check
source
on the
"D"
channel
CIAS monitor while the
"A" channel
was
in the tripped
condition.
This completed
the
2 out of 4 logic resulting in the
inadvertent
actuation.
As
a result of the actuation
the
2B Diesel
Generator
started
and
was
running when,
upon resetting
the CIAS, the
Diesel tripped
on high crankcase
pressure.
This trip was bypassed
by
design while the
ESFAS was active.
The diesel trip resulted
from the
lubricating oil relief valve,
which is in close proximity'o the
crankcase
pressure
detector,
relieving oil
under
fast start
conditions.
This
caused
the detector
to
sense
a high pressure
condition
and trip the diesel.
To prevent high crankcase
pressure
trips,
the
licensee
installed lubricating oil relief valve splash
guards
on both diesels.
The inspector
reviewed
PWO 62-2798
and
62-3276 which installed the oil deflectors
'and verified that the work
had
been
completed.
-
The inspector
found the licensee's
corrective
actions to be satisfactory.
This item is closed.
(Closed)
LER 50-389/89-04,
Containment
Local
Leak
Rate
Exceeds
Technical Specifications
Due to Valve Closure Stop Out of Adjustment
Due to Personnel
Error.
On June
5, 1989, with Unit 2 at
100% power,
a routine local leak rate
surveillance
test.
was
performed
on
the
containment
containing
the
containment
purge
system
exhaust
line.
The
leakage rate
was found'o exceed
the
TS limits.
The root
cause of the leakage
was determined
to be personnel
error in that the
valve adjustment
stop
was not properly locked
down by the personnel
who previously
tested
the
valve.
To prevent
this
event
from
recurring,
the
licensee
revised
the
technical
manual
to provide
guidance
on how to tighten the valve travel adjustment
screw locknut.
The
inspector
reviewed
the
change
to Technical
Manual
8770-5625,
Butterfly Valves Safety Class,
and found it acceptable.
This item is
closed.
Preparation for refueling (60705)
Refueling Activities
( 60710)
These activities were reviewed for Unit 1 during the period from November,
1989,
through March,
1990,
and were reported,
in part, in IRs 335/89-26,
335/90-08,
and 335/90-11.
The inspection attributes
included
management
supervision,
fuel receipt
and storage,
fuel
movement,
CEA installation,
core
reassembly,
operational
and
health
physics
controls,
and quality
verification.
The activities
were generally
well controlled
and well
monitored.
No violations or deviations
were identified in this area.
Followup of, Headquarters
and Regional
Requests
(Units
1 and
2) (92701)
Generic Letter
NO. 88-17,
Loss of Decay Heat Removal,
13
History:
Possible
Loss
of
Inventory
During
Low Coolant
Level
Operation,
dated
June
8,
1988,
was issued just prior to the Unit
1 outage
commencing
August,
1988.
Since
the training cycle
was over,
the site
issued
the
IN as
required, reading,and
the
operations
group
conducted
meetings
on
the
subject
each shift.
Previous
work instructions
had
installed the
dams in an incorrect order;
the work instructions
were
changed
to correct this.
PCMs (listed
below)
were
issued
to install
remote
RCS level indication in the control
room.
Loss of Decay
Heat Removal,
was issued
on October
17,
1988.
The site
has
taken steps
in
responding
to
the
GL
as
addressed
in several
letters
'to the
NRC.
Additionally,
INPO issued Case'tudy
88-018,
Loss of Decay
Heat Removal,
September
1988,
which
has
a
few more
suggestions
for the licensee
to
consider.
The
CE owners
group
had also supplied information to the site.
Unit 2 shut
down in early February,
1989, for a refueling outage.
Mid-loop
operation
went smoothly during that Unit 2 refueling.
On April 7, 1989,
the. resident
inspectors .observed
implementation of the
GL response.
The
current
(February,
March,
and April, 1990)
Unit
1 refueling
involved
mid-loop operations
which were also observed
by the inspectors.
Material Reviewed:
During the course of the review by the inspectors,
the following material
was considered:
Temporary Instruction
2515/101,
Loss of Decay Heat
Removal
(Generic
Letter
NO. 88-17)
10 CFR 50.54(f), of February
16,
1989
FPL letter L-89-38, Loss of, Decay Heat Removal, of February
1,
1989
FPL letter
Loss of Decay
Heat
Removal
(Generic Letter 88-17), of January
1,
1989
NRC Generic letter 88-17,
Loss of Decay Heat Removal, of October
17,
1988
INPO case
Study 99-018,
Loss of Decay Heat Removal, of September
1988
NRC
Possible
Sudden
Loss of
Inventory During Low Coolant Level Operation, of June 8,
1988
OP-0010129,
Rev
14,
Equipment
Out of Service
(the actual
out of
service
logs for periods
when mid nozzle operation
was occurring,
February
6 to 19 and April 15 to 19,
1989)
, OP-1-0120021,
Rev 23, Draining of Reactor Coolant System
14
OP-2-0120021,
Rev 13, Draining the Reactor Coolant System
ONOP 1-0440030,
Rev 10,
Shutdown Cooling Off-Normal
ONOP 2-0440030,
Rev 11,
Shutdown Cooling Off-Normal
I&C Procedure
1400097,
Rev 0, Core Exit Temperature
Monitoring During
Reduced
RCS Inventory
I&C Procedure
1400023,
Rev 0, Incore instrumentation
Outage
Tasks
Work Process
Sheet
8435-848,
Rev 0,
Install/Remove
Nozzle
Dams, of
November 7,- 1988 [Unit 2j
Work Process
Sheet
6659-1297,
Rev 1, Install/Remove
Nozzle
Dams,
Hot
and Cold Legs, of September
12,
1988 [Unit 1j
Memorandum of Instruction, Instruction for Closing Penetration
P-50,
approved
by Facility Review Group
on February 8,
1989
QA Audit JQQ-89-131,
February Monthly Performance
Monitoring, of
March 31,
1989
OP 1-1600023,
Rev 33, Refueling Sequence
Guidelines
OP 2-1600023,
Rev 18, Refueling Sequence
Guidelines
Plant
Change/Modification
(PCH)
N0.89-287,
Remote
Reactor
Vessel
Level Indicator, of June
30,
1988 [Unit 2]
NO.88-187,
Remote
Reactor
Vessel
Level Indicator, of July 30,
1988 [Unit 1]
FPL Letter FRN-89-088, of January
29,
1989
Memorandum
JQQ-89-048,
Independent
Verification of PSL Response
Loss of Decay Heat Removal, of January
31,
1989
Memorandum
SGOM-90-1-001,
Proper
Sequence
of S/G Primary Side
Manways
and Nozzle
Dams Installation (PSL-l), of January
26,
1990
Mechanical
Maintenance
Procedure
M-0029A, Rev 5,
(SG)
Primary Side Maintenance
QA Audits:
QSL-88-316,
September
15,
1988
QSL-OPS-89-687,
August 24,
1989
QSL-OPS-89-656,
March 31,
1989
QSL-OPS-90-707,
February 6,
1990
15
Areas
Inspected
a
~
b.
T~rainin
The inspectors
examined training records,
training material,
and the
class
training
plan for the
special
GL training.
The licensed
operators,
unlicensed
SNPOs,
STAs,
and
selected
technical
staff
received this training.
No maintenance
or trades
persons
received
the training.
Maintenance
and trades
persons
were often observed
to
be directed
by the operations
staff to not perform certain
work
during mid-loop operation
or to ensure
that precautions
were taken
during work performance while th'e plant was in a mid-loop condition.
The training
covered
the industry experience
in the events,
the
.pertinent
aspects
of the
GL, and the operational
impact of mid-loop
operation.
The bulk of the training was given
as special
training
immediately after
issuance
of the
GL.
Hot leg
and cold leg
dam
installation
sequence
training
was given during operator requalifi-
cation training in January,
1989.
Training materials
and
time
allotted to training appeared
to have
been
adequate.
Additional training did occur in the plant.
Operations
personnel
were
given instructions
as to actions
to take
and stations
to
be
manned;
a special
operator
was placed at the shut
down cooling board
in the control
room,
a nuclear operator
manned
a position in contain-
ment at
a tygon tube
RCS standpipe,
and the indicated
RCS level
was
logged every
15 minutes.
Containment
Closure
Containment
closure
would have
been
carried
out by two letters
of
instruction
during
the
Spring,
1989,
Unit
2 outage.
Mechanical
maintenance/backfit jointly issued
a letter providing instructions to
cl,ose
the
main containment
hatch
during
a loss
of
OHR while in
,mid-loop
operation.
One
other
containment
was
administratively allowed during mid-loop operation.
P-50
was
used
for
steam
generator
eddy current
testing;
the backfit
organization
issued
the
closure
instruction for that penetration.
Backfit personnel
were continuously stationed
in the containment
to
close
the containment at the order from the operations shift super-
visor.
The inspectors
did observe
the personnel
on shift and sighted
containment
closure
tools
and material.
Pre-shift briefings
were
held to discuss
containment
closure details.
Back-shift dry runs of
contacting
personnel
for containment
closure
were implemented.
The method for determining
the required
containment
closure time was
a graphical
method
found in the
RCS drain procedure.
Based
on the
RCS conditions
at the time of a postulated
DHR loss,
the time till
RCS boil off occurred
could
be determined.
The licensee
indicated
that the curves
in this procedure
were derived
from
EBASCO calcula-
tions indica'ted in FPL letter FRN-89-088
(see
above).
16
c.
RCS Temperature
Indication
The licensee
developed
a procedure for temporary
hookup of the
for control
room display while in an
outage
with the vessel
head
removed.
The procedure
connects
two CETs from one train of a safety
power supply
and
one
CET from another.
The procedure
was adequate
to
establish
the
hookup.
The installed cabling
was
observed
in the
containment
and control
room.
Additionally, normally available
system temperature
indication was available in the control
room.
d.
RCS Level Indication
Level indications
were in accordance
with FPL commitments in response
to the
GL.
The noted exception
to this
was the audible alarm to be
installed in Unit 2 by August,
1990.
Level indication
was provided
by two means
as follows:
The referenced
PCMs installed level indication in the form of
instrument loops;
two separate
transmitters
attached
to one
loop tap provided wide and narrow range signals.
Level read out
was provided by double indicating Sigma meters.
The meters
were
powered
from two separate
nonsafety
power
panels
which also
supply the transmitters
in containment.
Unit
1
had additional
monitoring capacity in that level could be viewed
on the
This capacity
was
scheduled
for installation in Unit 2 during
the
September,
1990,
outage.
A licensed
operator
was assigned
to monitor level indication during mid-loop operation.
A tygon tube
was installed
on
a separate
RCS tap for additional
indication.
A non-licensed
operator
was
assigned
in the
containment
to monitor
RCS level indication
on this tube during
critical evolutions.
This operator
was in radio communication
with the control
room.
There
was
good correlation
between
the
tygon tube
and the level transmitter
loop indications.
e.
Controls while in Mid Loop Operation
Overall operations
control of RCS perturbations
was good.
Heightened
awareness
was evident during mid-loop evolutions.
All unnecessary
work was prevented
on the
RCS boundary during these
periods.
When the loop level sensing
lines were filled and vented for use in
February,
1989,
the site
gA group
documented
procedure
adherence
problems
as minor audit findings.
Use of the
CETs for temperature
indication
was satisfactory.
Available additional
support instru-
ments,
such
as those
reading
SDC flow parameters,
were functional.
f.
Water Addition with the Loss of DHR
Prior to entering
mid-loop,
the
RCS draining
procedure
required
operability of the charging
system
and the off normal
procedure for
'Qe
17
e
SDC required that at least
one
pump
be available.
Observation
and selected
operational
log reviews
indicated
that the
pumps
were
available for mid-loop operation.
g.
Nozzle
Dam Installation
Prior to draining to mid loop, the pressurizer
was vented to atmos-
pheric
pressure
and
then
nozzle
dams
were installed
by the
above
referenced
work process
sheets.
These
sheets
contained
specific
sequence
steps
to ensure
that simultaneous
nozzle
blockage did not
occur.
Operations
maintained overall control via their work permits.
As with
any
set
of
new
procedures
and
their
attendant
new
inter-relationships, it has
taken
time to make
adjustments
to the
procedures
and work flow paths.
Importantly, the licensee
has
been
attentive
to the details of the inter-relationships
and accomplish-
ment of this complex evolution.
Overall, the licensee's
effort has
been
comprehensive.
Exit Interview (30703)
The inspection
scope
and findings were
summarized
on June
8,
1990, with
those
persons
indicated in paragraph
1 above.
The inspector described
the
areas
inspected
and discussed
in detail
the inspection
findings listed
below.
Proprietary
material
is not contained in this report. Dissenting
comments
were not received
from the licensee.
Item Number
Status
Description
and Reference
335/90-14-01
open
VIO - Failure to follow a test procedure,
paragraph
3.
9.
Abbreviations,
and Initialisms
A
ADV
A/E
AFM
ANPO
ANPS
ANSI
ASME Code
Ampere(s)
Auxiliary Building
ASEA Brown Boveri
(company)
Alternating Current
Automatic
CEA Timing Module
Atmospheric
Dump Valve
Architect/Engineer
Auxiliary Feedwater Actuation System
(system)
As Low as Reasonably
Achievable (radiation exposure)
Auxiliary Nuclear Plant [unlicensed] Operator
Assistant Nuclear Plant Supervisor
American National
Standards
Institute
Administrative Procedure
American Society of Mechanical
Engineers
Boiler and Pressure
Vessel
Code
0
18
'BCS
BQAP
CFR
CIAS
CIS
CRAC
CWD
CWO
DCN
DDPS
DEV
F
FI
FIS
FRG
FT
GDC
GL
GMP
Automatic Test Instrument (in the
ESF cabinets)
Anticipated Transient Without Scram
Backfit Construction
Sketch
Backfit Quality Assurance
Procedure
(EBASCO Services
Inc.)
'orrective
Action Request
Component Cooling Water
Combustion Engineering
(company)
Control
Element Assembly
Control
Element Drive Mechanism
Control
Element Drive Mechanism Control System
Code of Federal
Regulations
Containment Isolation Actuation Signal
Containment Isolation System
Control
Room Auxiliary Control (panel)
Cathode
Ray Tube
Containment
Spray (system)
Condensate
Storage
Tank
Current Transformer
Chemical
5 Yolume Control
System
Control Wiring Diagram
Construction
Work Order
Direct Curren't
Design
Change Notice
Digital Data Processing
System'igital
Electro-Hydraulic (turbine control
system)
Deviation (from Codes,
Standards,
Coamitments,
etc.)
Demonstration
Power Reactor
(A type of operating license)
Estimated Critical Position
Emergency
Core Cooling System
Emergency Diesel
Generator
Emergency Operating
Procedure
Environmental
Protection
Agency
Electric Power Research
Institute
Emergency
Response
Data Acquisition Display System
Engineered
Safety Feature
Engineered
Safety Feature Actuation System
Fahrenheit
Flow Control Yalve
Flow Indicator
Flow Indicator/Switch
The Florida Power
8 Light Company
.
Facility Review Group
Final Safety Analysis Report
Flow Transmitter
General
Design Criteria (from lOCFR 50, Appendix A)
General
Electric Company
[NRC] Generic Letter
General
Maintenance
Procedure
Ig
gpm
HFA
HJTC
HVE
HVS
I8C
ICW
IFI
IN
IR
IX
JPE
JPN
KV
KW
LCO
LER
LIV
LT
MFI V
min
MOVATS
mrem
MTI
MV
NPF
Gallon(s)
Per Minute (flow rate)
Hydraulic Control Valve
A GE relay designation
Heated Junction
Thermocouple
Health Physics
High Pressure
Safety Injection (system)
Heating
and Ventilating Exhaust (fan, system, etc.)
Heating
and Ventilating Supply (fan, system, etc.)
Heat Exchanger
Instrumentation
and Control
Intake Cooling Water
[NRC] Inspector
Followup Item
Integrated
Leak Rate Test(ing)
fNRC] Information Notice
Institute for Nuclear
Power Operations
[NRC] Inspection
Report
InService Inspection
(program)
Ion Exchanger
(Juno
Beach)
Power Plant Engineering
Juno
Beach)
Nuclear Engineering
KiloVolt(s)
KiloWatt(s)
Load Center (electrical distribution)
TS Limiting Condition for Operation
Licensee
Event Report
Licensee Identified Violation
Letter of Instruction
Low Pressure
Safety Injection (system)
Level Transmitter
Low Temperature
Overpressure
Protection
(system)
Measuring
5 Test Equipment
Motor Control Center (electrical distribution)
Main Feed Isolation Valve
Main Feed
Pump
Main Feed Water
Motor Generator
minute
Motor Operated
Valve
Motor Operated
Valve Test System
millirem
Maintenance
Procedure
Moisture Separator/Reheater
Maintenance
Team Inspection
Motorized Valve
Megawatt(s)
Non Conformance
Report
NonCited Violation (of NRC requirements)
Non Destructi.ve
Examination
Nuclear Production Facility (a type of license)
20
NPWO
NRC
ONOP
OP
PBT
PAID
P IS
psig
ppm
PWO
'WR
QI
RCB
RCO
RDT
Rev
RVLMS
SDCHX
SDCS
Nuclear Plant Operator
Nuclear Plant Supervisor
Nuclear Plant Work Order
Nuclear Regulatory
Commission
Nuclear
Steam Supply System
Operating Instruction
Off Normal Operating
Procedure
Operating
Procedure
Post'ccident
Panel
Performance
Based Training
.
Plant Change/Modification
Pressure
Control Valve
Piping
& Instrumentation
Diagram
Pressure
Indicator
Pressure
Indicator/Controller
Pressure
Indicator/Switch
Preventive
Maintenance
Power Operated Relief Valve
Pounds
per square
inch (gage)
Part(s)
per Million
Pressure
Transmitter
Plant Work Order
Pressurized
Water Reactor
Quality Assurance
Quality Control
Quality Instruction
Qualified Safety Parameter
Display System
Reactor Auxiliary Building
Reactor Containment Building
Reactor
Compartment
Fan Cooler
Reactor Control Operator
Pump
Reactor
Coolant Pressure
Boundary
Reactor Drain Tank
Revision
[NRC] Regulatory Guide
Reactor [licensed] Operator
Reactor Protection
System
Reactor Turbine Generator
Board
Reactor
Vessel
Level Monitoring System
Refueling Water Tank
Service Advice Letter
Systematic
Assessment
of Licensee
Performance
Safety Assessment
System
Shut
Down Cool,ing
Shut
Down Cool.ing Heat Exchanger
Shut
Down Cooling System
Spent
Fuel
Pool
21
SNOW
SNPO
Tavg
TCB
TCW
TDI
TEDB
TI
TS
V
Safety Injection (system)
Safety Injection Tank
Short Notice Outage
Work
Senior Nuclear Plant [unlicensed] Operator
Senior Reactor [licensed] Operator
Shift Technical
Advisor
Reactor
average
temperature
Temporary
Change
Trip Circuit Breaker
Turbine Cooling Water
Training Department
Instruction
Temperature
Element
Total Equipment
Data
Base
[NRC] Temporary Instruction
Three Mile Island
Temperature
Recorder
Technical Specification(s)
[NRC
Unresolved
Item
Volt s)
Volume Control
Tank
Violation (of NRC requirements)