ML17219A611

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Insp Repts 50-335/87-10 & 50-389/87-09 on 870405-0502. Violations Noted:Tech Spec Radiation Monitors Inoperable & Administrative Procedure 0010124 Not Implemented & as Result Alteration/Jumper Not Properly Documented & Controlled
ML17219A611
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 05/29/1987
From: Bibb H, Crlenjak R, Wilson B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17219A610 List:
References
50-335-87-10, 50-389-87-09, 50-389-87-9, NUDOCS 8706100141
Download: ML17219A611 (13)


See also: IR 05000335/1987010

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/87-10

and 50-389/87-09

Licensee:

Florida Power and Light Company

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-335

and 50-389

License Nos.:

DPR-67

and NPF-16

Facility Name:

St. Lucie

1 and

2

Inspection

Conducted:

April 5 - May 2,

1987

Inspectors:R.'

Cr enga

,

S nior Resident

Inspec or

j

H. B. Bibb, Resident

Inspector

~/<2 Cr

ate

igne

ate

igne

Approved by:

ct

- ~

c

B.

i son, Section

C ie

Division of Reactor

Projects

ate

igne

SUMMARY

Scope:

This inspection

involved on site activities in the areas

of Technical

Specification

compliance,

operator

performance,

overall

operations,

quality

assurance

practices,

station

and corporate

management

practices,

corrective

and

preventive

maintenance

activities, site security procedures,

radiation control

activities,

and surveillance activities.

Results:

Of the areas

inspected,

two violations were identified (paragraph

9).

One unresolved

item was identified (paragraph

9).

8706100141

870601

PDR

ADOCK 05000335

8

PDR

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

  • K. Harris, St. Lucie Vice President
  • G. J. Boissy, Plant Manager
  • R. Sipos,

Services

Manager

  • J. H. Barrow, Operations

Superintendent

T. A. Dillard, Maintenance

Superintendent

  • J. B. Harper,

gA Superintendent

L. W. Pearce,

Operations

Supervisor

  • R. J. Frechette,

Chemistry Supervisor

  • C. F. Leppla, I 5

C Supervisor

  • C. A. Pell, Technical Staff Supervisor

E. J. Wunderlich, Reactor Engineering Supervisor

H. F. Buchanan,

Health Physics

Supervisor

G. Longhouser,

Security Supervisor

  • C. l,. Burton, Reliability and Support Supervisor

J. Barrow, Fire Prevention Coordinator

R. E. Dawson, Assistant Plant Superintendent

- Electrical

C. Wilson, Assistant Plant Superintendent

- Mechanical

N.

G. Roos, guality Control Supervisor

Other

licensee

employees

contacted

included

technicians,

operators,

mechanics,

security force members,

and office personnel.

  • Attended exit interview

Exit Interview

The inspection

scope

and findings were

summarized

on May 11,

1987, with

those

persons

indicated in paragraph

1 above.

The licensee

did not identify as proprietary

any of the materials

provided

to or reviewed

by the inspectors

during this inspection.

Licensee Action on Previous

Enforcement Matters

(Closed

- Units

1

and

2)

UNR 335,

389/85-28-02,

Uncertainties

In Time

Performance

of 24 Hour Surveillance:

Ambiguities in recording the time of

performance

on

several

copies

of OP-2-3200020

(Primary

System

Manual

Calorimetric),

performed

in October,

1985

were previously reported

( IE

Report

335,

389/85-28).

The inspector

reviewed

80 'copies

of similarly

completed

procedures

for Units

1

and

2.

No discrepancies

were noted.

This item is considered

closed.

Unresolved

Items

(UNR)

An UNR is

a matter which more information is required to determine

whether

it is acceptable

or may involve

a violation or deviation.

One

UNR is

addressed

in paragraph

9

(UNR 389/87-09-01).

Plant Tours (Units

1 and 2)

The inspectors

conducted

plant tours periodically during the inspection

interval to verify that monitoring equipment

was recording

as required,

equipment

was properly tagged,

operations

personnel

were

aware of plant

conditions,

and plant housekeeping

efforts were adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

were

properly

established,

critical clean

areas

were being controlled in accordance

with

procedures,

excess

equipment

or material

was

stored

properly

and

combustible materials

and debris

were disposed

of expeditiously.

During

tours,

the inspectors

looked for the

existence

of unusual fluid leaks,

piping

vibrations,

pipe

hanger

and

seismic restraint settings,

various

valve

and breaker positions,

equipment

caution

and danger tags,

component

positions,

adequacy of fire fighting equipment,

and instrument calibration

dates.

Some tours were conducted

on backshifts.

The inspectors

routinely conducted

partial

walkdowns of emergency

core

cooling

systems

(ECCS).

Valve,

breaker/switch

lineups

and

equipment

conditions

were

randomly verified both locally and in the control

room.

During the inspection

period the inspectors

conducted

a complete walkdown

of the accessible

areas

of the Units

1

and

2 emergency

diesel

generators

to verify that the lineups

were in accordance

with licensee

requirements

for operability and that equipment material conditions were satisfactory.

Additionally, flowpath verifications

were

performed

on the following

systems:

Units

1

and

2 high and low pressure

safety injection, chemistry

and volume control,

and auxiliary feedwater.

Plant Operations

Review (Units

1 and 2)

The inspectors,

periodically during

the, inspection

interval,

reviewed

shift logs

and

operations

records,

including

data

sheets,

instrument

,traces,

and

records 'of equipment

malfunctions.

This review included

control

room logs

and auxiliary logs, operating

orders,

standing

orders,

jumper

logs

and

equipment

tagout

records.

The

inspectors

routinely

observed

operator

alertness

and

demeanor

during plant tours.

During

routine

operations,

operator

performance

and

response

actions

were

observed

and

evaluated.

The

inspectors

conducted

random

off-hours

inspections

during the reporting interval to assure

that operations

and

security

remained

at

an acceptable

level.

Shift turnovers

were observed

to verify that they were

conducted

in accordance

with approved

licensee

procedures.

The inspectors

performed

an in-depth review of the following

safety-related

tagouts

(clearances):

1-4-217

1A Boric Acid Makeup

(BAM) Pump - reset impeller

1-4-215

1B Charging

Pump - planned maintenance

(PM)

1-4-212

1A BAM Pump - inservice test

1-3-181

1A

BAM Pump - install

pump

Technical Specification

(TS) Compliance

(Units

1 and 2)

During this reporting interval, the inspectors verified compliance

with

limiting conditions

for operations

(LCO's)

and

results

of selected

surveillance

tests.

These verifications

were

accomplished

by direct

observation

of monitoring

instrumentation,

valve

positions,

switch

positions,

and

review of completed

logs

and

records.

The licensee's

compliance

with

LCO

action

statements

were

reviewed

on

selected

occurrences

as they happened.

Maintenance

Observation

Station

maintenance

activities of selected

safety-related

systems

and

components

were observed/reviewed

to ascertain

that they were conducted

in

accordance

with requirements.

The following items were considered

during

this review;

LCO's were met, activites

were accomplished

using

approved

procedures,

functional tests

and/or calibrations

were performed prior to

returning

components

or systems

to service; quality control records

were

maintained; activities were accomplished

by qualified personnel;

parts

and

materials

used

were properly certified;

and radiological controls

were

implemented

as required.

Work requests

were reviewed to determine

status

of outstanding

jobs

and

to

assure

the priority was

assigned

to

safety-related

equipment.

The inspectors

observed/reviewed

portions of

the following maintenance activities:

PW0

4624

5053

62-299

62-2008

62-2036

Semi-Annual Calibration of Fluke Digital Voltmeter

Unit

1 "A" CVCS [Chemical

and Volume Control System]

Heat

Tracing Cabinet - Loss of Cabinet

Power

Repair

Leak on Unit 2 Instrument Air Dryer Heater

2C Changing

Pump

-PM

2C Auxiliary Feedwater

Pump -

PM

Review of Nonroutine Events

Reported

by the Licensee

(Units

1 and 2)

The following Licensee

Event Reports

(LER's) were reviewed for potential

generic

impact,

to detect

trends,

and to determine

whether corrective

actions

appeared

appropriate.

Events which were reported

immediately were

also reviewed

as they occurred to determine that technical

specifications

were

being

met

and that the public health

and safety

were of upmost

consideration.

The following LER's are considered

closed:

335/87-09 - Technical Specification

(TS) Radiation Monitors Inoperable

On April 12,

1987,

the

1A emergency

core cooling system

(ECCS)

emergency

exhaust

fan radiation monitor was discovered

to have failed.

Efforts to

effect repairs

were

unsuccessful

during the following 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The

licensee

decided

that the

ECCS area

was

a more critical area to monitor

than

was the fuel handling building

(FHB) area.

On April 15, to satisfy

the requirements

of Unit

1

TS 3.3.3.1.b,

the licensee installed temporary

ducting to allow the

FHB exhaust

radiation monitor to sample

the

ECCS

area,

leaving

the

FHB

area

exhaust

unmonitored.

The

FHB

exhaust

'entilation fan

was

on at this time

and

remained

on for the next five

days.

The

FHB exhaust

should

have

been

secured

or periodically sampled

in

accordance

with Unit 1

TS 3.3.3.10.b.

On April 20,

1987,

a chemistry

technician

noted

that

the

FHB ventilation

fans

were still running.

Additionally, he

knew that

TS required

samples

were not being taken

on the

FHB exhaust

and

immediately

informed operations.

Operations

personnel

secured

all

FHB fans at 8:00 a.m.,

on April 20,

1987.

Repairs

were

completed

and

the

lA ECCS

emergency

exhaust

fan radiation monitor was

returned to service at 4:00 p.m.,

on April 20,

1987.

With regards

to the

above

events

the following plant

procedures

were

reviewed

by the inspector:

a

~

Administrative Procedure

(AP) 0010432,

Nuclear Plant

Work Orders,

which

states:

"All modifications,

preventive

and

corrective

maintenance

performed

by

Florida

Power

and

Light maintenance

personnel

and maintenance

directed work by contractors

and vendors at

St.

Lucie Plant shall

be authorized

through the Nuclear Plant

Work

Order."

A work order

was not issued

to perform the shifting of the

FHB

radiation

monitor suction

to the

ECCS

emergency

radiation

monitor suction.

b.

Administrative Procedure

(AP) 0010124,

Control

and

Use of Jumpers

and

Disconnected

Leads

which states:

"To ensure

control of all jumpers,

disconnected

leads

and temporary piping in safety related circuits

and systems,

one of the following methods

shall

be used:.

( 1)

Control

by procedure - The documentation

in a procedure shall

be

used

when the procedure specifies

the alteration

and restoration

of a circuit or system.

(2)

Control

by the

Jumper/Lifted

Lead

Request

Log -

When

an

alteration

is not .controlled

by

an

approved

procedure (i.e.,

troubleshooting

electronic

equipment

or temporary modifications

to permit interim operation)

and is unattended

(not hand held),

it shall

be

recorded

in the Jumper/Lifted

Lead

Log

and

a

Temporary

Circuit Alteration

Tag

attached.

This shall

be

accomplished

as outlined in Section 8.0 of this procedure.

(3)

Hand Held - As long as continuous

h sical contact is maintained

with the disconnected

lead or gumper

and Reed

the controls in

steps

1 and

2 above

are not required."

These

procedures

were not implemented

and

as

a result, the temporary

alteration/jumper

was not properly documented

and controlled.

N

l

c ~

Operating

Procedure

(OP)

0010129

-

Equipment

Out of Service-

Class

1, Which states:

"Figure

1 shall

be filled out at any time

a

Class

1

piece of equipment

is

removed

from service."

Inspector's

note:

Figure

1 referred to above, is the log sheet

portion of the

Equipment

Out of Service

Log.

And, "the Assistant

Nuclear Plant

Supervisor

is

responsible

for maintaining

the

Equipment

Out of

Service Log."

This

procedure

was

not properly

implemented

in that the out of

service

equipment

was not logged.

The

above

described

items a., b.,

and

c.

are

examples

of failure to

follow/implement procedures

and together

are considered

to be

a violation

(335/87-10-01).

Additionally, the inspector

reviewed the following Unit 1 TS:

TS 3.3.3.10,

Table

3.3-13

Action

3 states

that effluent releases

can

continue for up to 30 days with the

FHB exhaust radiation monitor out of

service if grab samples

are taken

once

per eight hours

and analyzed within

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The

TS was not followed in that grab samples

were not taken

on

a shiftly bases

during the five days that the

FHB exhaust ventilation fan

was operating

unmonitored.

This is

a violation (335/87-10-2).

The following events

were

reported

immediately

by the

licensee

and

reviewed

by the inspector;

On April 22,

1987,

at 1:35 p.m. Unit 2 tripped from 100K power due to

a

turbine trip caused

by personnel

error while performing routine electrical

maintenance.

Electrical

maintenance

personnel

were

performing routine

circulation

water

pump

(CWP)

ammeter

calibrations.

The

ammeter

calibrations

consisted

of shorting

out the

leads

to the appropriate

ammeter

by utilizing a jumper across

the associated

terminals in reactor

turbine gauge

board

(RTGB), section

202.

The meters

are

them removed from

the

RTGB for calibration.

The electricians

had jumpered the

2A2

CWP meter

at terminal block (TB) No. 5, points

57 and

58 in RTGB, section

202.

They

then

jumpered

the

282

CWP meter at

TB No. 5, points

82

and

83 in RTGB,

section

202.

For the

281

CWP meter,

the drawing indicated that they

should

jumper

TB No.

29 points

92

and 93,

RTGB, section

202.

At this

point

the electricians

jumpered

across

TB No.29,

however,

they

had

unknowingly crossed

into

RTGB, section

201.

This action resulted

in

shorting

the control

switch for the feeder

breaker to the

480 volt 2A1

load center

(LC) and at 1:35 p.m. the station service transformer

2Al 4160

KV breaker

tripped.

This resulted

in the

loss of

a large

number of

non-safety

related

equipment in the plant,

however, this should not have

resulted

in

a turbine trip/reactor trip.

A turbine/reactor trip was

experienced.

Subsequent

investigation

revealed

that the loss of LC 2A1 resulted in the

deenergization

of

two control

element

drive

mechanism

(CEDN)

bus

undervoltage

(UV) relays.

This made up, contrary to design,

the turbine

trip on reactor trip logic, causing

a turbine trip,

The cause of the

CEDM

bus

UV relay deenergization

was

a set of rolled/reversed

leads in

CEDM

cabinet

2.

The original

plant. design

had

the

lead

in the rolled

configuration,

howe'ver

this

had

caused

two earlier

reactor trips.

Consequently

a plant change/modification

(PC/M) was implemented in 1983 to

change

the leads.

They were functionally tested to the

new confirguration

in 1984.

A review, by the licensee,

of associated

work documents

revealed

that

no

changes

were authorized

subsequent

to the

PC/M referred

above.

The licensee

is currently investigating this event to determine

how the

leads

were rolled.

Until the investigation is completed

and reviewed

by

the inspector this item is unresolved

(UNR, 389/87-09-01).

On April 9, 1987, with Unit 2 at .100 percent

power, Instrument

and Control

( I&C) personnel

were

performing

the monthly surveillance

test of the

engineered

safety features

actuation

system.

During the testing, it was

noted that

one annunciator

did not illuminate.

After completion of the

test,

IKC personnel

commenced

trouble shooting to determine

the cause of

the annunciator failure.

A jumper was placed

on the wrong terminal, main

steam isolation signal

actuation

pushbutton,

causing

the closure of the

main steam

and feedwater isolation valves.

This resulted in an automatic reactor trip due to low steam generator level.

With regards

to plant

response

two pieces

of plant equipment

did not

respond

as

expected

during

the

event.

The

steam

driven auxiliary

feedwater

pump

(AFW) tripped

on overspeed

and

one main steam safety valve

(MSSV) remained partially open for approximately eight minutes.

The two

electric driven

AFW pumps

functioned properly

and the

steam

driven

AFW

pump

was restarted

without problem.

The licensee

investigated

the

cause

of the

pump trip and could not determine

the cause.

The

pump trip was

determined

to

be

an isolated

event.

In reference

to the partially open

MSSV, operations

personnel

reduced

steam generator

pressure

to allow the

valve to reclose.

This was also

an isolated event,

however, the licensee

is continuing to determine

the cause for the valve sticking.

The trip described

above is

one of several

which have occurred

over the

past

few months

which involve personnel

error

and is possibly indicative

of

a trend in this area.

The licensee

is pursing

these

problems

and is

taking corrective actions

in an attempt to reverse

the negative

trend.

The inspectors

are monitoring these actions.

Physical

Protection (Units

1 and 2)

The inspectors verified by observation

and interviews during the reporting

interval that measures

taken

the assure

the physical

protection of the

facility met

current

requirements.

Areas

inspected

included

the

organization

of the security force, the establishment

and maintenance

of

gates,

doors

and isolation

zones

in the proper conditions,

that

access

control

and badging

was proper,

and procedures

were followed.

W

ll.

Survei 1 l ance Observati ons

During the

inspection

period,

the

inspectors

verified operations

in

compliance

with selected

technical

specifications

(TS)

requirements.

Typical of these

were confirmation of compliance with the

TS for reactor

coolant

chemistry,

refueling

water

tank

(level,

temperature

and

chemistry),

containment

pressure,

control

room ventilation

and

AC and

DC

electrical

sources.

The inspectors verified that testing

was performed in

accordance

with adequate

procedures,

test instrumentation

was calibrated,

limiting conditions for operations

were met,

removal

and restoration of

the affected

components

were accomplished,

test results

met requirements

and

were

reviewed

by personnel

other

than the individual directing the

test,

and

that

any deficiencies

identified during

the testing

were

properly reviewed

and resolved

by appropriate

management

personnel.

The

inspectors

observed

portions of the following surveillance(s):

INC 1-1220050

R.13

- Linear Power

Range Safety

Channel quarterly

Calibration

AP 1-00110125

- Schedule of Periodic Tests,

Checks

and Calibrations

- Check Sheets

1,2,3,4,5,

and 6,Data

Sheets

3,4,5,21,22,

and

26

lI