L-88-273, Forwards mgt-on-shift Weekly Repts for Wk of 880613
| ML17347A814 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 06/22/1988 |
| From: | Conway W FLORIDA POWER & LIGHT CO. |
| To: | Grace J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| References | |
| L-88-273, NUDOCS 8807120366 | |
| Download: ML17347A814 (65) | |
Text
ACCELHMTZD DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8807120366 DOC.DATE: 88/06/22 NOTARIZED: NO DOCKET g
FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C 05000250 50-251 Turkey Point Plant, Unit 4,'Florida Power and Light C 05000251 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
Florida Power
& Light Co.
RECIP.NAME RECIPIENT AFFILIATION GRACE,J.N.
Region 2, Ofc of the Director
SUBJECT:
Forwards mgt on shift weekly repts for wk of 880613.
DISTRIBUTION CODE:
IE36D COPIES RECEIVED:LTR Q ENCL
/
SIZE: 5 TITLE: Immediate/Confirmatory Action Ltr (50 Dkt-Other Than Emergency Prepar D
NOTES RECIPIENT ID CODE/NAME PD2-2 LA EDISON,G INTERNAL: NRR/DOEA/EAB 11
~E ~+
02 EXTERNAL: LPDR NSIC COPIES LTTR ENCL 1
0 1
1 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD2-2 PD NUDOCS-ABSTRACT RES/DE/EIB RGN2/DRSS/EPRPB NRC PDR COPIES LTTR ENCL 1
1 1
1 1
1 1
1 1
1 A
A TOTAL NUMBER OF COPIES REQUIRED:
LTTR 12 ENCL 11
JUNE 2 2 1988 L-88-273 Dr. J. Nelson Grace Regional Administrator, Region II U.S. Nuclear Regulatory Commission 101 Marietta Street, N. W., Suite 2900 Atlanta, Georgia 30323 Re:
Turkey Point Units 3 and 4
Docket Nos.
50-250 and 50-251'ana ement-on-Shift Weekl Re ort
Dear Dr. Grace:
Pursuant to the Nuclear Regulatory Commission Order dated October 19,
- 1987, the attached summary of Management-on-Shift (MOS) reports is submitted.
The Plant Supervisor-Nuclear Shift Reports are also being submitted.
Should there be any questions on this information, please contact us.
Very truly yours, W. F.
y Senior Vic President - Nuclear WFC/SDF/gp Attachment cc:
J.
Lieberman, Director, Office of Enforcement, USNRC Dr.
G.
E. Edison, Project Manager,
- NRR, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant R. E. Talion, President, FPL mos 001 8807120366 880622 PDR ADOCK 05000250 R
MANAGEMENT ON SHIFT (MOS)
VfEEKL'Y
SUMMARY
REPORT WEEK STARTING:
06 13 88 PAGE QF Five MOS Observers were on shift.
Richard Coulthard, Westinghouse Electric Corporation (06/13-19/88, days);
Peter L.
- Walker, Westinghouse
- Electric Corporation (06/13-19/88, evenings);
Julio C.
Balaguero, Turkey Point Nuclear Plant Operations Support Supervisor (06/14-19/88, evenings);
and Larry L.
- Thomas, Turkey Point Nuclear Plant Outage Manager (06/13-19/88, evenings);
and Terry A
- Finn, Turkey Point Training Department Superintendent (06/19-20/88, evenings).
Both Units 3
and 4
operated at 1004 power throughout the reporting period, except for a Unit 3 reduction to 690 MWe gross for approximately 8
hours on June 15,
- 1988, to replace the generator air side seal oil pump.
Two questionable work practices were reported by the MOS Observers concerning noncompliances with the clearance tag procedure.
One questionable work practice was reported concerning delay in reporting malfunctioning equipment to the Plant Supervisor Nuclear.
During the reporting period, the MOS Observers noted seventeen recommendations and areas for improvement.
These comments and suggestions involved:
The inability of the Moveable Incore Detector System to support flux mapping (repaired 6/19/88).
Two comments on inadequate communications between departments causing unnecessary delay.
The unreliability of two radiation detectors.
Operators lack of familiarity with the Technical Specification Implementation Procedure.
Two comments regarding the perceived need to run flux maps.
ATTACHMENT:
MOS DAILY REPORTS
MANAGEMENT ON SHIFT (MOS)
VfEEKLY
SUMMARY
, REPORT WEEK STARTING:
PAGE OF Two comments on the reliability of the inverter power supply to the Analog Rod Position Indication (ARPI).
A suggested relaxation of the ARPI rod bottom runback bistable setpoint.
The advisability of energized receipt inspections on certain I&C equipment.
A recommended reordering of work under an LCO, for efficiency.
Four comments on inadequate planning or scheduling.
During the reporting period the Plant Supervisor-Nuclear (PSN)
MOS reporting program continued.
In recognition that the PSN is in fact Management on Shift, the form used by the PSNs has been retitled "Shift Report,"
with the Shift Management personnel identified.
The PSNs reported nine questionable work practices.
Two of these were also reported by MOS Observers (clearance tag violation and delayed report of malfunctioning
, equipment).
Two others concerned inadequate support outside normal hours.
The remaining items involved:
Opefation with a Reactor Protection channel out-of-service.
(For an extended period within the LCO).
Insufficient emphasis on LCO related repairs.
Unauthorized manipulation of equipment by Maintenance personnel.
(Fire Protection pressure switch in Turbine Building)
Confusion on requirements for testing of redundant train equipment prior to maintenance.
Attempted use of an out-of-date. maintenance procedure.
ATTACHMENT:
MOS DAILY REPORTS
MANAGEMENT ON SHIFT (MOS)
WEEKLY'UMMARYREFORT WEEK STARTING:
06/13/88 PAGE 3
OF 3
The PSNs noted thirteen recommendations and areas for improvement.
These comments and suggestions involved:
The reliability of the Post Accident Hydrogen Monitors.
Three comments on inadequate scheduling support outside normal working hours.
One comment on poor housekeeping.
A recommendation to improve the couplings on the Main Feed Regulating Valve actuators.
An apparent conflict between Technical Specifications and a
plant procedure.
Difficulty in finding test data sheets to prove a
valve operable.
Metal Impact Monitors on both units out-of-service.
Two comments on poor scheduling.
A need for increased awareness of plant status by maintenance personnel.
An option in the Technical Specification Implementation Procedure that cannot be used with one Nuclear Instrument channel out-of-service.
ATTACHMENT:
MOS DAILY REPORTS
Date 06/13/88 Shift Report Shift Day Wogan Shift Management AI'N Singer Ngi I; Vetromile A.
Questionable Work Practices/Actions Taken/Recommendations Continued operation with Reactor Protection channels out-of-service, with additional periodics being performed (required), that bring us closer to trip or safety injection.
B.
Areas for Improvement/Recommendations/Actions Taken l 6 C should maintain a continued awareness of safety-related system status as they perform maintenance.
A heightened awareness will prevent any further misalignments as occurred 6/13/88 (refer to to APSN log entry).
C.
Good Practices/Professionalism Observed Unit 4 operator awareness
- noticed opposite Auxiliary Feedwater Train flow pressure and notified NWE/APSN in a timely manner.
tteviewed Bp~(J l)ete
~ ~ J~Actions Completed I)ate
Date 06/13/88 Shift Report Peak Reese Shift Management AI'N Dallau fernandez A.
Questionable Work Practices/Actions Taken/Recomme'ndations Again, when Nuclear Job Planning System (NJPS) was needed tonight, it was two hours before we could input a PWO for N-41 into the system.
B.
Areas for Improvement/Recommendations/Actions lf NJPS is required to get needed work performed, it should not have so much down time on the peak and mid shift.
C.
Good Practices/Professionalism Observed
/
Reviewed By Jtt (t.i l)a'.e ( /
J l Actions Completed
!)ate
0-ADM-0i 8 Maragementon Shift(MOS)
MOS l)Alf.Y RKf'OR'l'perations Superintendent,
- Nuclear Date:
06/13/88 From:
A.
Richard Cou Ithard (MO 'seruer)
Plant evolutions observed Shi ft:
Qx Day Q Night 0
Units 3 and 4 at 100',0 power Periodic Rod exercise on Unit 4 per OP-1604.1 Quarterly I 6 C surveillance of Unit Nuclear Instrumentation Channel N-41 per 3-PM 1-059.8 0720 6 1300 Plan-of-The-Day meetings 1535 peaks start of shift meeting Operations monthly surveillance on Channel N-41 (Nuclear Instrumentation) per 3-OSP-59.5 B.
C.
Immediate safety problems None Questionable work practices None Areas for improvement This item was noted in the morning Plan-of-the-Day meeting.
The Unit 4
flux map system does riot have 38 operable
- paths, and a flux map to satisfy ADM-021 (Interim Technical Specifications
) cannot be run.
ADM-02I requires this within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of a Power Range Nuclear Instrumentation Channel is out-of-service.
The concern this morning was that the spike on the N-44 channel observed Sunday Night could have evoked this Technical Specification if taken out-of-service to investigate the problem.
E.
Completed By:
This afternoon when I 6 C returned a Unit 3 Channel N-41 to operations, the operating surveillance test found the currents to be out of specification.
This channel has been out-of-service since 1140 and could evoke the need for a flux map.
Had this N-41 problem occurred on Unit 4, the flux map option to avoid the action statement to reduce Dower to 75'.0 after 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> would not be availa "le.
Professionalism, Summary of Shift, Comments l.
All observed shift activities in the Control Room on day and peak shifts were conducted in a professional manner.
2.
Unit 4 peak shift Reactor Operator took the initiative to provide scenario training for on shift trainees.
Date:
viewed By M
6seruer I
gQ' Operations Superinte Management lP/),
Review By:
Ae'f '>'"J~"
I < <v!J.~
D te t-N clear i 9 c>
/'
ate
< e)f 06/IZrda
0-ADM-019 Management, on Shift (MOS)
MOS l)A1LYRh'.1'ORT
'l'o:
Operations Superintendent
- Nuclear Date:
06/13-14/88 From:
L. L. Thomas (M
bseruer)
Shift:
Q Day gx Night Plant evolutions observed Adjustment to N-41 and test Shift turnover and shift briefing Steady state operations B.
Immediate safety problems None C.
Questionable work practices None Areas for improvement 2.
The communications between Operations and I 6 C
on N-41 being out-of-service and its affect on the plant needs improvement.
At 1740 the peak shift 1 6 C Supervisor was asked by the MOS Observer if he realized Unit 3 was in an action statement, per O-ADM-021, which ends at 2340.
He said he had not been informed.
Once he found out he took the appropriate actions to get the PAVO ready and work accomplished.
The Flux Map should have been started sooner.
Various problems encountered caused it to be completed 27 minutes after the required time of 2340.
Professionalism, Summary of Shift, Comments Good use of training time on peak shift with trainees and reactor operator.
Mid shift performed in a
professional and highly efficient manner when confronted with N-41 problem.
Completed By L, L. Thomas M
bseruer
//
Reviewed By:
( +
c J. '6;r-Op'erations Superi nte e
i3 f)
Management
'eview By: pil'"<><~ I (
t~l/J'N Dte'ate:
06/13-1<
R8 06/l3-4f
0-ADM-019 Management on Shift (MOS)
MOS DAlLYRE)'ORT 0:
Operations Superintendent-Nuclear Date:
06/13-14/88 From:
P. L. Walker (M
bserver)
Shift:
~
Day Qx Night A.
Plant evolutions observed Units 3 and 4, 1000/0 steady state power operation Plant staff reaction to failure of Unit 3
Power Range Channel 8&41 during periodic test B.
Immediate safety problems None Questionable work practices None
0-ADM-019 Management on Shift (MOS)
MOS DAlLYREPORT D.
Areas for improvement 3.
Instrumentation and Control department had six hours, 55 minutes (minus approx.
15 minutes to perform operability check) to repair the offending Power Range Channel.
It was returned to service too late to avoid overrunning the 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> LCO time.
Directions to the technicians performing the repair lacked the emphasis required to ensure that the job would be completed on time.
Reactor Engineering did not include any contingency time when they scheduled the start of the QPTR Flux Map.
Problems arose which prevented them from supporting the required 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> action limit.
The operation staffs did not have a crystal clear idea of what was to happen when. the 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> limit was reached.
There were three paths to success:
Fix the channel; get acceptable QPTR results; or obtain a waiver of the applicable 0-ADM-021 Interim Technical Specification.
A fourth path, reducing power to 75",0 and reducing power range setpoints, was out of the question due to being procedurally impossible, given that one channel was already failed.
When the shift was turned over, many options were already precluded, and the oncoming crew was jammed into a crisis situation.
Proper planning would have already resolved any interpretation of Technical Specification questions, have had a
pre-authorized waiver of 0-ADM-21 Technical Specifications available, had enough information available to adequately supervise supporting group actions, and have a definite plan of what was to occur when the action statement time expired.
Professionalism, Summary of Shift, Comments Question:
Why, when a perfectly valid method of determining QPTR via the 3
operable power range NIS channels
- exists, is the 0-ADM-021 Technical Specification worded to require the use of the much more cumbersome (albeit more accurate) flux mapping method?
Completed By:
Reviewed By:
Peter L. Walker M
seruer
.(c'.< i Operations uperin nde Management
'. /,
Review By: ~
'.~i'~< / E I'te t-Nu e r ate Dat~
O6/13-14/88 06/l 3-7l/5
1)ate 06 14 88 Shift Report Mid Jones Shift Management A [7SN Haley NO'K A.
Questionable Work Practices/Actions Taken/Recommendations At 1140 6/13/88, N-41 was declared out-of-service for calibration and testing.
At 1645 N-41 failed its periodic test and a PWO was issued.
Maintenance was not started until late on peak shift - Reactor Engineering did not perform Flux Map untii 2025 and did not get it complete until 0007 6/14/88, which was greater than 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> requirement per ADM-021. It doesn't seem the correct effort was placed on getting N-41 repaired when a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> action statement was in effect.
Areas for Improvement/Recommendations/Actions Taken If a Power Range Channel is out-of-service greater than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> perform Flux Map to ensure it is complete within the required time frame.
Investigage changing ADM-021 requirement for a Flux Map to verify OPTR values, to perform QPTR calculation per ONOP 12308.2.
If it is expected that maintenance will go beyond 4PM, formulate a game plan with contingencies.
ADM-021 Table 3.3-1 action 2C, reducing power to less than or equal to 75'.b and reduce hi flux trip to less than or equal to 85',o is not a possible option due to minimum degree of redundancy with one channel in trip mode (out-of-service), removing another channel to reset trip setpoints will cause a reactor trip.
Therefore flux map, or returning channel to service is the only option.
C.
Good Practices/Professionalism Observed
/
Revie~'ed Bk'(t~
r r'c l)ates /'/fI Actions Completed Date
E)ate OS l4/Sa Shift Report Days Shift Management AE~SN Singer NS'K Vetromile A.
Questionable Work Practices/Actions Taken/Recommendations A valve on the 3C Bus deluge was manipulated during the resetting of the fire deluge clapper which had a clearance tag hung on it which stated "Do Not Open".
The Turbine Operator and mechanic doing the job were both cautioned about the proper use of the clearance system.
B.
Areas for Improvement/Recommendations/Actions Taken Assure that all plant personnel are retrained in the use of clearances and discuss this also at plant safety meetings.
C.
Good Practices/Professionalism Observed
~ii!
Revie~ ed Hp i) l)ate
~~
~J 1< Actions Completed E)ate
0-ADhf-019 Managementon Shift(MOS)
MOS l)All.YREPORT Operations Superintendent
- Nu'clear-Date:
From:
Richard Coulthard (M
bser oer)
Sh ift:
Qx Day Night A.
Plant evolutions observed Units 3 and 4 operations at 1000'o power Unit 4 Reactor Protection System Logic Test, OSP 49.1 Unit 3 Reactor Coolant Average Temperature/Delta Temperature Test per procedure TP-433 0720 and 1300 Plan of the Day meetings 1540 peaks start of shift meeting B.
C.
Immediate safety problems None Questionable work practices As a result of a misunsderstanding of whether Operations or Maintenance was controlling the PWO on the 3C transformer deluge valve, the fire protection deluge isolation valve was opened in accordance with a procedure, but in violation of a clearance tag.
This problem came to the attention of the day shift APSN during the course of his duties and resulting actions are discussed in the PSN shift report.
It is felt that the APSN responded properly to this event.
The requirement that all clearance tags not be violated is presumably is well known. 'Operations and shift management should re-emphasize to all personnel the importance of not violating clearance tags.
Areas for improvement None Professionalism, Summary of Shift, Comments No unprofessional conduct observed.
Completed By:
viewed By Richard Coulthard M
Ap (
bseruer Operations Superintendent-Nuclear
.'6/ l 4/S 8 Management Review By:
M-N
/dye ate VP Date 06/l 4lgg
0-ADM-019 Managementon Shift,{MOS)
MOS DAlLYREl'ORT To:
Operations Superintendent
- Nuclear Date:
06/14-15/88 From:
J. C. Bala uero (M
bser ocr)
Shift:
Q Day gx Nigh t, A.
Plant evolutions observed Normal 10070 power operations on both units Plant walkdown Conversations with several Operations and Maintenance personnel Shift turnover Shift meeting B.
Immediate safety problems
~-
None C.
Questionable work problems None observed Areas for improvement None observed Professionalism, Summary of Shift, Comments No comments Completed By J. C. Balaguero M
bseroer Reviewed By: 'U
- r. (
Operations Superintendent-Nuclear Da te:
06/14-1)'88 Dat-r iljJ Management Review By:
PM-N Date ate I
0-ADM-019 Management on Shift (MOS)
MOS 1)A1LY RE 1'ORT To:
Operations Superintendent
- Nuclear Date:
06 14-8 From:
P. L. Walker (M
bseruer)
Shift:
Q Day gx Night A.
Plant evolutions observed 100',!0 steady state operation, both units 3 and 4 Evaluation and resolution of possible Unit 3 containment Boundary leakage via sample line from Reactor Coolant System Shift turnover at 11:00 PM B.
Immediate safety problems None C.
Ouestionable work practices None D.
Areas for improvement None E.
Professionalism, Summary of Shift, Comments Quiet night Completed By P. L. Walker M
bseruer Reviewed Ry:
'v
! i.
Operations Superintendent-Nuclear Date:
06/14-1 i 88 Management Review By:
-N 4 rs
ÃVJ D
Date 06 15 88 Shift Report S}lift Mid Shift Management Schimkus A i>SN Murphy NS'K Spence A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken Need to have a little more attention paid to cleaning up loose items in obscure areas of the plant.
A lot of small trash is accumulating in the corners of different operating areas such as the Feedwater platforms or beside pumps, etc.
Recommendation:
Have the foreman in charge of the helpers tour the Secondary with some helpers and point out these minor discrepancies off the beaten path.
The plant generally looks good.
C.
Good Practices/Professionalism Observed A concern was raised about possible by-leakage on the Reactor Coolant System sample valves SV-3-6427 A 6 B inside containment and SV-3-6428 outside containment.
These are boundary isolation valves.
Upon calling the Technical Department Supervisor at midnight, he showed immediate concern and came to the plant with a technician and was able to verify no unacceptable leakage from these boundary valves.
J I
Reviewed H~r! tl) ff.t r.r
.- i!/
l)ate (
~
Jd Actions Completed t>ate
Date 06/15/88 Shift Report Shift Day 0
Shift Management Wogan A )iS Singer Vetromile A.
Questionable Work Practices/Actions Taken/Recommendations IGC GEMS Planners are manipulating equipment without authorization.
PSN stopped further testing and informed personnel they needed to abide by work controls established.
Recommend PWO initiation and work to be done by journeyman.
Also recommend work be authorized through Control Room. i.e., NWE/APSN/PSN rather than Mr. Perrine.
The equipment being manipulated was a fire protection valve in the turbine. building, being manipulated by a contract individual.
B.
Areas for Improvement/Recommendations/Actions Taken None noted C.
Good Practices/Professionalism Observed Great maintenance support in the air side seal pump replacement minimizing the impact
'n unit instability.
, >- /(
Reviewed B)',
< /C
/ ('>(.(',
l)ate ( /t-Actions Completed t)ate
. l)ate 06/15/88 Shift Report Shift Shift Management Reese Dallau N O' Fernandez A.
Questionable Work Practices/Actions=Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken None C.
Good Practices/Professionalism Observed None
/.,I Reviewed HI),. u' l)ate C
1(
Actions Completed l)ate
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0-ADM-019 Management on Shift (MOS)
MOS DAILYREPORT Professionalism, Summary of Shift, Comments 1.
Shift operations were conducted in an entirely professional manner.
2.
My first entry and exit from the RCA were handled in a proficient manner..
Completed By:
bseruer Date:
Reviewed By:
/ />r~ (<<
perafions uperi ntendent-Nuclear I
Management~~
Review By: (:l c'".. ti
. I ~,
~
atA Dat:
/C J.
i
/
0-ADM-0]9 Management on Shift (MOS)
MOS DAlLYREl'ORT Opera tions Su peri ri tend ent -.Nuclear'ate:
06 15-16 88 From:
J. C. Bala uero (M
bseruer)
Plant evolutions observed Shift:
Q Day Qx Night Both units at steady state 1000o power Plant walkdown Shift meeting Shift turnover B.
C.
Immediate safety problems None Questionable work practices Checked the clearance on the 4A Component Cooling Water (CCW) Heat Exchanger and found a clearance tag for vent valve 4-50-585 hung on valve 4-50-375A which is,a redundant vent valve on the same heat exchanger.
Notified the PSN (peakshift) who immediately took corrective action and had the tag hung on the correct valve.
D.
Areas for improvement Strict adherence to procedural requirements shall be reiterated to all operators so that clearance orders are followed verbatim.
Operators have a difficult time isolating CCW Heat Exchangers after scaffolding has been erected because of limited space.
Realizing that the amount of time on LCO's should be limited, it might be a good compromise to isolate the heat exchanger first and erect the scaffolding
- second, while the heat exchanger is being drained.
This should make it easier to operators to isolate the heat exchanger and allow Maintenance plenty of time to erect the scaffolding, especially if we drain the side of the heat exchanger that is not being opened.
0-ADM-019 Management on Shift (MOS)
MOS DAILYREPORT Page'.
Professionalism, Summary of shift, Comments No comments c3 Completed By:
bseruer Date:
I Reviewed By:
(.
/i Opera ions uperi ntendent-lVuclear Management p~. Py'~,
. p
~/p (@
I ta<
ate Date:
t' V~(
/
15ale ne(i e i r ice
0-ADM-019 Managementon Shift(MOS)
MOS l)AlLYRE I'ORT I'sg<<
'lo Operations Superintendent
- Nuclear Date:
From:
(M bseruer)
Shift:
Q Day Qx Night A.
Plant evolutions observed Units 3 and 4, 100',0 steady state operations PSN noticed a
loose coupling on a Unit 4 main feed regulating valve
- action was taken to stabilize the valve in a timely fashion.
B.
Immediate safety problems None C.
Questionable work practices None D.
Areas for improvement None Professionalism, Summary of Shift, Comments The degraded (loose) coupling on the feed regulating valve was handled quickly and efficiently.
Further action to evaluate the operability of the valve will be done during day shift.
Completed By P. L. walker M
bseruer
/
Reviewed By:
Operations Superintendent-Nuclear 06/l 5-l6/88 Da~:
6
/C /V Management Review By:
l, 'z JL</ ti/C Jf M-D te
,~i%
Date PP nr I < I</AA
e l)ate 06/16/88 Shift Report Mid Shift Management Schimkus p, liSN Murphy NM'K Spence A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken Need a better method to couple the Main Feedwater Regulator valves to their actuators.
In the past two years we have had at least 2 load reductions to 60 Megawatts electric, due to the presently installed "split couplings,"
loosening up from vibration and causing valve shaft actuator separation.
Tonight we almost had the same situation, however the coupling had only slightly loosened and the actuator and valve stem threads didn't have a chance to misalign.
Recommendations:
Better method to lock coupling together or re-design the coupling mechanism.
C.
Good Practices/Professionalism Observed Excellent support from IGC and Mechanical Maintenance to immediately focus their efforts on 4A Main Feedwater Regulator loose coupling.
They were on the scene approximately 3 minutes from my notification of the problem.
R d Ily !'!!Mi
(
t)eteC//< ~Actions Completed l)ate
O-.ADM-019 Management on Shift (MOS)
MOS DAII.YREPORT I'use To:
Operations Superintendent
- Nuclear Date:
06/16/88 From:
Richard Coulthard (MO bseroer)
Shift:
Qx Day Q Night A.
Plant evolutions observed C.
D.
Units 3 and 4 operations at l00~o power 07ZO Plan of the Day meeting 1535 peaks start of shift meeting Unit 3
Nuclear Instrumentation Channels N-42 and N-43 quarterly calibration per MP-IZ307.3 Unit 3 Nuclear Instrumentation Channels Operability Test for N-42 and N-43 per OSP-059.4 Immediate safety problems None Questionable work practices None Areas for improvement None E.
Professionalism, Summary of Shift, Comments The NrC conduct of the Power Range Nuclear Instrumentation Quarterly Calibration proceeded quite. smoothly and only required slightly over 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> per channel using procedure MP-12307.3.
This is significantly below the 5 to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> per channel previously reported using the new PMI-059 series of procedures.
Control Room operations were again conducted in a
professional and cooperative manner.
Completed By:
Richard Coulthard M
bseroer Date:
06/16/88 iI nK Da 1 MlLi I III II~ M
/
Reviewed By:
Operations Supenntendent-Nuclear Management g/~//J /i
/
Review By: ~(l( /i'>LC'./
PM-
~
D te
/
I Date:,':/ /./
Date 06/16/88
0-ADM-019 Management on Shift (MOS)
MOS I)AILYREI'ORT To:
Operations Superintendent
- Nuclear Date:
06/16-17/88 From:
A.
J. C. Balaguero (M
bseroer)
Plant evolutions observed Shift:
Q Day Qx
- Night, Steady state full power operations Plant walkdown Shift turnover Shift meeting B.
C.
Immediate safety problems None Questionable work practices None observed D.
Areas for improvement E.
None Professionalism, Summary of Shift, Comments No comments Completed By:
J. C. Bala uero I
bseroer I
Da te:
I Reviewed By:
..-I.~ /" ~ l~
Operations Superintendent-Nuclear Management p
Review By:
! <'i&
'<e Ji <.. I
'/<i
<~ro I<IS M-N te Dote VP 6/ l 6-l 7/88 0
.:~r./ il/
/
~a<e 06/16-17/$ 8
0-ADM-019 Managementon Shift(MOS)
MOS I)A]LY R Ei'0RT
'I'o:
Operations Superintendent-Nuclear Date:
06/16-17/88 From:
P. L. Walker (M
bserver)
Plant evolutions observed Shi ft:
Q Day
~x
- Night, Units 3 and 4, 100",0 steady state power operation Rebolting of Unit 4 feed regulating valve Electrical Bus testing - both units 2330 shift change meeting C.
D.
Immediate safety problems None Ouestionable work practices None Areas for improvement Radiation detectors continue to be a problem.
R-15 6 20 detectors for both units are out.
E.
Professionalism, Summary of Shift, Comments l.
~Ver quiet shift.
2.
I have noticed an increase in the number of unauthori"ed noises over the page system.
Comple ted By:
P. L. Walker M
bseruer Date:
I i6 li tiR Reviewed By operations uperintendent-Nuclear Managementt',
p ~>,./ /
Review By:
. ~ '~
i t."-'./ (a;~/(8 PM-N Date
,4~~ R Date
'~ 'll 06/16-17/88
0-
l)ate 6/16 88 Shift Report Shift Shift Management Schimkus/Harpel A iiSN Singer NS'K Fernandez A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken None C.
Good Practices/Professionalism Observed Routine operations Reviewed Bp(~'
c't't-'
))ete
~~ ~/
d Actions Com'pleted De<<
I
Date 06 17 88 Shift Report iMid Shift Management Schimkus A ]~Sg Murphy g gt y Spence Questionable Work Practices/Actions Taken/Recommendations Compliance and Regulation letter PTN-TECH-88-288 addressing redundant train operability testing prior to maintenance, or testing required upon failure of an Engineered Safety Features (ESF) component has created a
gray area.
Current Technical Specifications definition 1.4 defined operability which states that any ESF equipment plus its support functions must be operable and capable of performing its design functions.
We are currently receiving clearance requests on ESF equipment support equipment.
Examples being:
A.
Residual Heat Removal pump 3A-PC-3-601.
This is a pressure interlock on 3A RHR Loop which when valved out will take 3A RHR Loop out-of-service.
Compliance and Regulation reply was to test this PC-3-600 on 3B RHR pump.
To test this will involve valving out PC-3-600 which will take 3B RHR Looo out-of-service.
Containment Spray Pumps (C.S.P.)
3A and 3B must have their seal cooler floe indicators (FIC-657 and FIC-659) P.M.'d one at a time.
This involves racking out the associated C.S.P.
This means that a surveillance operability test will be required on the companion pump prior to maintenance activities.
If either of the above examples were to occur on any shift other than dayshift (Monday
- Friday) and it was due to a discovered failure of the support component, Operations personnel would not be able to meet the redundant train required test within the specified 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time limit thus non-compliance to a Tech.
Spec.
action statement per licensing letter.
Recommendations:
1.
Re-evaluate PTN-TECH-88-288 letter. Contact USNRC and discuss problem to arrive at a solid answer of how to meet redundant train operability requirements in the cases of Preventive Maintenance, etc. on support equipment.
2.
Evaluate the need for special procedures to utilize (by on-site operators) for operability testing of ESF equipment.
tNote:
Many of our test'rocedures are performed by the Technical Department with Operations support.
3.
Prior to sending clearance requests to the Control Room'on ESF type equipment, ensure that Technical Department is set up to test the redundant train if required.
lf not required, have responsible department supervisor sign and state that "no t"sti:
required" on redundant train.
( V',I a'eviewed Hy >>4'df<y t)ate ( </ J )
Actions Completed l)ate
Date June 17, 1988 Shift Report Page Continuation Page" B.
Areas for Improvement/Recommendations/Actions Taken Due to Intake Cooling Water/Component Cooling Water (ICW/CCW) basket strainers frequent fouling, they must be backwashed approximately I - 3 times per day.
At the same time we have had at least I CCW Heat Exchanger (HX) out-of-service (either unit) every day for cleaning due to higher intake temperatures.
Procedure 3/4-OP-019 steps 7.1.1.1 thru 7.1.1.5 require a113 CCW HX to be operable to backwash.
ADM-021 and current Tech.
Specs don't list this requirement (copies attached).
PUP supplied me with a reason; that it was addressed and reviewed by the Plant Nuclear Safety Committee (PNSC) for the current procedure.
Recommendations:
Re-evaluate and make procedure changes.
C.
Good Practices/Professionalism Observed Routine operations.
Excellent observation by Nuclear Watch Engineer (NWE);
informed PSN that while removing fuse block SV-6428 (Reactor Coolant System sample) his hand slammed into the Reactor Trip Switch casing and 'connectors behind Vertical Panel B.
The PSN observed this and verified the same condition exists on Unit 4 on fuses for CV-956 A. This occurrence is nearly unpreventable due to close proximity of fuse blocks to Reactor Trip Switch.
NWE placed caution tags on both fuse blocks.
This could cause unit trip.
Need attention.
~ jl{bI Ol OshA
e 0
Date 06 17 88 Shift Report Day Jones Shift Management A VSN Haley NWK A.
Questionable Work Practices/Actions Taken/Recommendations It needs to be emphasized to all personnel to use up-to-date procedures per AP 190.86 paragraph 5.7.1.
An IGC technician was attempting to use an out-of-date procedure and he said he was only required to check for new On The Spot Changes.
We pointed out the above procedure requirement.
B.
Areas for Improvement/Recommendations/Actions Taken C.
Good Practices/Professionalism Observed Reviewed By
'4 4
" tatl Date Actions Completed Date
Date 6/17/88 Shift Report Peak Harpel Shift Management AI'N Reese NS'K A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken None C.
Good Practices/Professionalism Observed None Reviewed Hy Date
-- t:fS Actions Completed Date
0-ADM-019 Managementon Shift(MOS)
M OS DAILY R E l'0RT Page 0:
Opera tions Superintendent
- Nuclear From:
Richard Coulthard (M
bseruer)
Shift:
g)
Day o
A.
Plant evolutions observed Units 3 and 4 operations at 100~5 power 07ZO Plan-of-the-Day meeting 1535 Peaks start of shift meeting Preplanned fire 'rill in 480 volt Motor Control Center.
Complete complement of the fire brigade was at the scene in 6 minutes.
PMI-OZ8,Z, Axial Flux, Rod Deviation, and Rod Position Indication (RPI) monthly test on Unit 3 B.
, Immediate safety problems None C.
Questionable work practices None D.
Areas for improvement During the morning, confusion surfaced over controls on moving a large crane from the Unit 4 containment to the Unit 3 containment during which the load must pass oyer Intake Cooling IVater lines and safety-related cable trenches.
There was also conflicting information over the weight of the crane; initially reported at 240,000 lbs., but later reported to be below the 165,000 lbs. limit for this move.
If movements of this size are very infrequent (less than annually), action such as revising ONOP 3408.2.
Intake Cooling Iyater Failure Due To Transport of Heavy Loads, or a notice in the Control Room shift order book, are not appropriate.
If frequency of occurrence is greater, some guidance for the Control Room to evaluate and monitor this type of event might expedite future movements.
Operations was correct to look for guidance on this issue because of regulatory sensitivity to heavy loads.
0-A0 M-019 Management on Shift (MOS)
MOS DAILYREPORT The conduct of 3-PM-028.2 resulted, in a loss of all.power to the Rod Position.lridicators (RPI) for several minutes (i.e., all rods were indicated on bottom).
The conduct of this test raises two concerns:
a) Because of fluctuations in the RPI inverter power supply, the power supply for the RPI's is always switched to the Emergency Power Supply (a lighting panel) for this test in order to get steady-stare data.
Is there a reason the inverter power supply cannot be repaired or restored so these fluxuations do not exist?
b) During the conduct of this test, the Rod Bottom Bistable alarm setpoint is verified and reset if not in tolerance.
These bistables chatter during this process which reduces bistable life.
Since this has been done monthly for some time, there is no reason to suggest this caused the lighting panel to trip.
However, the acceptance criteria for resetting this alarm is 0.209 to 0.310 Volts D.C.
(less than
+
I step).
A +
10 step tolerance on the rod bottom alarm is probably acceptable since it has only an information/condition indication function and is not a calculated setpoint.
It is quite possible this alarm would have to be reset less often (with less tine spent with a chattering relay) if the tolerance were opened to something like 0.15 to 0.45 Volts D.C.
Professionalism, Summary of Shift, Comments 2.
3.
The Operations response to the loss of power of the Unit 3 Rod Position Indicators was carried out in an organized and timely manner.
OP-9700.2, Operation of RPI Power Supply System was used to transfer power from the Lighting Panel back to the RPI Inverters.
The Off-Normal Operating Procedure was pulled out ln case the above action did not solve the problem.
Shift turnover was in progress when this occurred.
I witnessed and concur with the PSN day shift report concerning the desire of an IGC Specialist to use an out-of-date procedure, I consider the overall incident a "good practice" because it demonstrates the Control Room review of On-The-Spot-Changes can prevent out-of-date procedures going to the field for use.
About 1700 on the peak shift, the Licensing Engineer brought a letter concerning testing requirements for Emergency Diesels to the Control Room.
He took the time to review the contents of the letter with the PSN and APSN.
A good practice, especially for a late Friday afternoon.
Completed By:
Richard Coulthard I
bserver Date:
06/17/88 Reviewed By:
Operations S peri ntendent-Nuclear Date Management Review By; 4 M(N I ulna ~
PM B-Vl Date Pl 7l 06/17/88
0-ADM-0]9 Management on Shift (MOS)
MOS l)AILYRE('ORT To:
Operations Superintendent
- Nuclear Date:
From:
P
)V (M
bseruer)
Plant evolutions observed Shift:
Q Day Qx Night Units 3 and 4, 100'/o steady state operation Unit 3, Reactor Coolant Pump seal package acted up again.
Actions were taken to stabilize and recover it.
2330 shift change meeting B.
C.
D.
Immediate safety problems None Questionable work practices None Areas for improvement None Professionalism, summary of Shift, Comments Quiet shift Completed By:
P. L. VValker M
bseruer Date:
Reviewed By:
Opera ions uperi ntendent-Nuclear Date:
-ZQ Management Review By:
M-N ate Date E)are 06/17-18/88
0-ADM-0] 9 Managementon Shift(MOS)
MOS l)AlLYRE1'ORT
'I'o:
Operations Superintendent-Nuclear Date:
06/17-18 88 From:
J. C. Balaguero (M
dseruer)
Shift:
Q Day Qx Night,.
Plant evolutions observed Both units at 100O'o IGC calibration of FM-3-484 steam flow protection channel Unit 3, 3A RCP ¹I seal leakoff decrease Plant walkdown Shift meeting Shift turnover B.
C.
D.
E.
Immediate safety problems None Questionable work practices None observed Areas for improvement None observed Professionalism, Summary of Shift, Comments I
Communications betwen Maintenance and Operations on the status of FM-484 calibration were excellent.
The IGC technician was very informative and gave the Reactor Operator a thorough explanation in a very professional manner.
Shift meeting in the midnight shift continues to be excellent.
The APSN and PSN encourage open communication and insist on getting good feedback on plant problems.
The use of the Plan of the Shift form is a very good idea.
This form gets filled out by the APSN or PSN and distributed to everyone in the shift meeting to serve as an agenda and keep the meeting on track.
Tours of the plant continue to exhibit a high level of cleanliness.
Completed By:
J. C. Bala uero M
dseruer Reviewed By.
KQ Oper ti ns Superintendent-Nuclear Date:
.-3-"
~
Management Review By:
-N icl/
/
ate
~ate 06/17-18/88
Date 06/I 8/88 Shift Report Shift Mid N
Shift Management Schimkus AliS~
Murphy Spence A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken The Post Accident Hydrogen Monitor (PAHM) is required to be in service 30 minutes after a valid Safety Injection 'Signal.
Every time we attempt to test PAFIM's for a monthly surveillance, either one or both channels fail to meet acceptance criteria.
The support to have this problem repaired usually appears close to the end of the required LCO time, i.e., 7 days or 30 days.
The problem appears generally with the span check in which IGC calibrates,
- tests, and then releases the channel for an Operations operability test which usually passes.
Recommend:
A speedier method to calibrate this instrument.
C.
Good Practices/Professionalism Observed None Reviewed By Date g ZC~
Actions Completed Date
Date 6/18/88 Shift Report Shift Day N
Shift Management
- Schimkus, hiurphy'iataszewski A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken 6/17/88 Unit 3 Auxiliary Feedwater Train 2 was removed from service for Preventive Maintenance on flow control valve air filters.
Numerous small air leaks were discovered on Swagelok fittings, etc including some air leaks on the instrument air root valves to the same equipment.
IGC repaired their portion of leaks and PWO's were generated to Mechanical hiaintenance to repair/adjust the packing on their valves (10 valves).
I was questioned by the hiaintenance Supervisor why we were creating a crisis over a non-safety related set of valves which would cause an inconvenience to a GEMS Planner who would have to be called out to plan the work package.
I explained the importance of having a totally reliable core heat sink system on our nuclear units and requested that GEMS initiate,the package.
Recommend:
2.
I Prior to PMS on an Engineered Safety Features (ESF) system by any work group, have the system engineer walk down the system and initiate PWO's on any discrepency not already identified by a PWO.
This should be an=in depth hand-over-hand walk down.
If adequate support personnel is not available on weekends, quit scheduling ESF PCS on weekends, holidays or schedule GEMS to be here for each Department.
C.
Good Practices/Professionalism Observed Routine operations Reviewed By Date HO.
Actions Completed Date
0
Date 6/18/88 Shift Report Peak Harpel Shift Management A l'SN Reese Spence A.
Questionable Work Practices/Actions Taken/Recommendations While performing 3 PMI-028.2 Axial Flux Rod Deviation Periodic on 6/17/88 day shift the breaker for the Rod Position Indication (RPI) backup power supply tripped.
The test was stopped to investigate.
Due to other problems and manpower, IGC didn't restart on the procedure right away.
The 6/18/88 Peak shift IGC Supervisor, who planned to get back into the periodic, went to check the working copy of the procedure to see what progress had been made and noticed that the IGC specialist on Friday had determined Rod Bottom Bistable E-9 to be inoperable.
He promptly notified the PSN.
The RPI was determined to be inoperable and Reactor Engineering was requested to run a flux map.
Any time a piece of equipment is determined inoperable or suspected inoperable the PSN should be promptly notified so approproate actions can be taken to avoid possible violations and initiate corrective action.
B.
Areas for Improvement/Recommendations/Actions Taken None C.
Good Practices/Professionalism Observed None Reviewed By VA. Lu; Date 4
9 Actions Completed Date
0-AD M-019 Management on Shift (MOS)
MOS DAILYREPORT f
>ps>>.'o Oper;.
> ions Superintendent
- Nuclear Date:
06/18/88 From:
(MO bserver)
Plant evolutions observed Shift:
Qx Day 0 Night B.
Units 3 and 4 operations at 100~o power 0735 and 1535 beginning of shift briefing 3-OP-14004.1, Steam Generator Protection Channels - periodic test Immediate safety problems None C.
Questionable work practices None Areas for improvement None Professionalism, Summary of Shift, Comments None Completed By:
M bseruer Date:
Reviewed By:
C4; Opera ons Superintendent-Nuclear Date:
6-I Management Review By:
IMIai >>>L>>I m
-N Date Vl D
06/18/88
0-ADM-019 Managementon Shift(MOS)
MOS i)A]LYRE('ORT To:
Opera tions Superintendent
- Nuclear Date:
06/18-19/88 From:
P. L. )Valker l'M 6seruer)
Shift:
Q Day
~x Night A.
Plant evolutions observed Units 3 and 4, 100'/o power, steady state operations Analog Rod Position Indication (ARPI) Rod Bottom Bistable repairs-ARPI calibration - another trip of ARPI alternate power supply 2330 shift turnover B.
C.
Immediate safety problems None Questionable work practices The Instrumentation and Control technicians performing the ARPI periodic failed to report the Rod Bottom Bistable malfunction to the PSN (which occurred around 1515 on June
- 17) until approximately 2000 on June 18, 1988.
The failure should have been reported almost immediately.
D.
Areas for improvement Licensing referred to "System Operation Review Program" document to resolve the ARPI operability question.
The channel was declared inoperable and flux mapping every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> was initiated.
The basis for doing the flux map is to determine the position of the rod(s).
In this case, the ARPI channel was clearly able to determine the position of the rod, and the map was unnecessary.
A differentiation between the ARPI function of determining position of the rod and the runback bistable function needs to be made.
Professionalism, Summary of Shift, Comments None Completed By:
P. L. )Valker M
bseruer Date:
06/18-19/88 Reviewed By:
Operations Superintendent-Nuclear Date:
Management Review By:
PM-N at ate Date 06/18-19/88
0
> I
0-ADM-019 Managementon Shift(MOS)
MOS 1)AILYRE I'ORT
'I'o:
Operations Superintendent-Nuclear "-
Date:
. 06/18-19/88.
From:
J. C. Balaguero (M
bseruer)
Shift:
Q Day Qx Nigh t, A.
Plant evolutions observed Full power steady state operation Plant walkdown Shift turnover Shift meeting RPI Bistable replacement B.
Immediate safety problems None C.
Questionable work practices None D.
Areas for improvement None Professionalism, Summary of Shift, Comments There has been a noticeable improvement in professionalism in the Control Room as well as communications beteween Maintenance and Operations since the last time I was here as a MOS Observer.
Completed By:
J. C. Bala uero bseruer Date:
06 18-19 88 Reviewed By:
Management Review By:
Operations Superintendent-Nuclear Date Date:
( "'0""+
Date 06/18-19/88
Date 6/19/88 Shift Report Shift Mid Shift Management Schimkus Murphy Spence A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken It was noticed by the midshift APSN that the Unit 4 Containment purge valve data sheet in our Redbook Surveillances indicated that valve POV-4-2603 had not been tested prior to exceeding 200', during past outage.
There was no data in our Control Room to prove or disprove the operability concern.
The dayshift PSN/APSN followed up on this concern and solicited Technical Department support to find the test data sheets proving operability.
Actions taken were to update the data sheet with proper information and transmit old data sheets to Document Control.
Recommendations:
Note:
The PSN is responsible for review of O-OSP-200.1 (Redbook Surveillances).
The PSN is responsible for review of the RCO logs.
Make the Containment Purge Valve Cycle Data Sheet Checkoff, a PSN surveillance check per O-OSP-200.1 on a monthly basis in Modes 1,2 and a daily check in Modes 3,4,5,6.
Make the Startup Surveillance O-OSP-200.2 reflect a Technical Departmemt Signoff (TDS) to ensure prior to Mode 4 during heat up; they review 3/4-OSP-201.1 attachment 5 and update cycle data sheets in accordance with current number of cycles, remove old sheets in book and transmit them to Document Control.
Note:
Tracking of actual Local Leakrate Test (LLRT) status and tracking of valve cycles
~be ond 10 cycles is beyond the'scope of Control Room staff capabilities.
This informatfon is under Technical Department jurisdiction outside our Control Room.
C.
Good Practices/Professionalism Observed While performing Unit 3 RPI periodic, the alternate RPI power supply breaker tripped causing all rods to indicate on bottom.
APSN took appropriate actions to meet Technical Specification requirements.
The APSN/IGC Supervisor/Electrical Department
- Chief, immediately conferred about problem and decided on the following course of action:
a) Complete RPI periodic, after breaker
- reset, b) Document what conditions existed at time of trip, c) Document any further occurrences and their conditions, d) Change defective breaker and bench test for trip set point (weak breaker).
This will determine if root cause is breaker or RPI system.
Excellent logic!
Reviewed Hy Date (Ip-E Actions Completed Date
Date 6/19/88 Shift Report Day N
Shift Management Schimkus Murphy
~~ y Mateszewski A.
Questionable Work Practices/Actions Taken/Recommendations IGC Supervisor said that IGC Specialist forgot to bring tools out of containment and re-install flux mapper E-drive cover plate.
Due to low manpower staffing the Health Physics Department did not have adequate personnel to support containment entry.
Actions taken:
PSN requested HP perform call out for support.
PSN requested IGC to make preparations to perform entry for above discrepencies.
PSN notified Maintenance Superintendent of situation.
B.
Areas for Improvement/Recommendations/Actions Taken Due to Unit 3 RPI alternate power breaker tripping twice during IGC scheduled surveillance a PWO was initiated at 0154 on 6/19/88 to replace defective breaker (LP-317 Bkr-18),
At this time the midshift Electrical Chief was instructed by PSN to call out a GEMS Planner to incorporate a work package.
This was questioned by Electrical Chief but he reassured PSN that he would do this immediately,- At 0735 pre-shift briefing the day shift Electrical Chief informed us that work package was not prepared yet, as the GEMS Planner came in at approximately 0630.
Actions Taken:
Notified Maintenance Superintendent.
C.
Good Practices/Professionalism Observed Acting Maintenance Supervisor (W.R. Williams) thanked PSN for notification of shift report and reassured that he willfollow-up on the cause of why these situations occurred.
Reviewed By
(. i-Date b Z Actions Completed J
Date 06/19/88 Shift Report Shift Peak V
N Harpel Shift Management AI'N Reese gt y Spence A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken None C.
Good Practices/Professionalism Observed None Reviewed By Date 4"E4 Actions Completed Date
0-ADM-019 Management on Shift (MOS)
MOS DAILYREPORT f'use To:
Operations Superintendent
- Nuclear Date:
06/19/88 From:
Richard Coulthard (M
bserver)
Shift:
Qx Day p Night Plant evolutIons observed Units 3 and 4 operations at 100oo power 0735 and 1535 beginning of shift meetings Unit 4 Incore Flux Map using two detectors B.
C.
D.
Immediate safety problems None Questionable work practices None Areas for improvement This is a'followup to my bIOS report of June 17, item D-2 on Rod Position Indication (RPI) testing.
VVhen power is transferred from the RPI inverter to the LP-317 source, the Rod Position Indication on the affected rods drops 5 or 6 steps.
This would seem to induce a significant uncertainty into the calibration data when the power supply is transferred back to the RPI inverter.
This was reported by the operators and verified on the June 18 evening test on the RPI's.
Professionalism, Summary of Shift, Comments The'rocess from the time a relatively simple problem is identified and the PAVO written, until work is initiated, should be reviewed.
I have observed two instances this week (Nuclear Instrumentation Channel N-41 currents and lighting panel
- 317, Breaker
- 18) where the specialists and electricians were available on site to work the job, but had to wait for the work package process to start very simple jobs.
It was 1530 today before a replacement breaker was located and work started on LP-317, Breaker 18.
Completed By:
M bseroer Date:
Reviewed By:
Operati s Superintendent-Nuclear Date:
Management Review By:
HAMI L> I >II illM M-D
~l Date ~
D 06/19/88
0-ADM-019 Management on Shift (MOS)
MOS l)AlLYREPORT To:
Opera t ions Superintendent
- Nuclear Date:
06/19-20/88 From:
A.
P. L. IValker(I bseruer)
Plant evolutions observed Shift:
Q Day Qx Night Units 3 and 4, 100oo steady state power operation until a Xenon ocscillation was induced in Unit 4 for a test.
2330 shift change meeting B.
C.
D.
E.
Immediate safety problems None Questionable work practices None Areas for improvement None Professionalism, Summary of Shift, Comments Extended runs at 100",i are good for morale.
Everyone appears to be doing a good job.
Completed By:
P. L. Pal'r',er I
bseroer Date.
06/19-20/88 Reviewed By:
. Operatio s
uperintendent-Nuclear Date:
('."@ '80 Managemen t Review By:
I-N
"/
/
IITl a ate VP G6/1<'%fhb
0-ADM-019 Managementon Shift(MOS)
MOS l)AILYRE I'ORT
'I'o:
Operations Su peri ntendent
- Nuclear Date:
06/19-20/88 From:
A.
T. A. Finn (M
bseroer)
Plant evolutions observed Shift:
Q Day Qx Night Units 3 and 4, 100 0'o steady state operation Plant tour PSN/APSN shift turnover intermediate Range periodic 4-OSP 59.2 B.
C.
D.
Immediate safety problems None Questionable work practices None Areas for improvement None Professionalism, Summary of Shift, Comments Quiet professional shifts.
Completed By:
T. A. Finn M
bseroer Date; 06/19-20/88 Reviewed By:
'R9. u I'peratio uperintendent-Nuclear Date:
Management Review By:
ae Date ~1l 06/19-20/88
Date 06/20/88 Shift Report Shift Mid N
Shift Management Schirzkus murphy Spence A.
Questionable Work Practices/Actions Taken/Recommendations None B.
Areas for Improvement/Recommendations/Actions Taken Steam Generator (SG) Tube Rupture is probably the most likely accident to occur in the nuclear industry.
Based on numerous plants having found debris inside the secondary tube sides of their S/G (including Turkey Point) a method to detect loose debris while on line was formulated:
Metal Impact hionitoring system (MIMS). At this time Unit 3 MIMS has been out-of-service since 3/04/88, and Unit 4 MIMS'since 6/11/88. It is presently impossible to perform the mid-shift check for noise.
Recommendations:
Repair this system, it could be a valuable tool. (See attached comments).
C.
Good Practices/Professionalism Observed 2.
SRO candidate requested a PSN tour of plant as to enhance his knowledge of plant systems.
He asked many questions and showed to me that he has indeed studied the systems in depth.
Good work, BillLindsey.
Unit 3 NTO, (Fred Bennykofer) while making his rounds observed cloudy oil in the "A" Auxiliary Feedwater pump oil reservoir.
His only requirement is to record level in sight glass.
When I checked the situation it was obvious he stuck his head in the pipes to make this observation.
Actions:
Declared 3A Auxiliary Feedwater pump out-of-service and issued PWO to change oil.
Reviewed By Date Actions Completed Date
MIMS SRO, Joe Scott initiated this list at PSN re uest.
Operator hardspots - the system is outside the unit operator surveillance area.
Due to its location it's often forgotten about.
When an alarm is received by the unit operator, he has to find someone to investigate it for him.
This may include running the tape for 10 minutes.
The system often gives false alarms, has tape
- problems, etc.
Currently the machine has nowhere to hang the microphone so it hangs on the recorder power leads.
Suggestions for improving MIMS:
1) 2)
3) 4)
Write operators a surveillance procedure.
Move the unit operators surveillance boundries to include the MIMS rack.
Present a MIMS lecture in requal including use ot the tape machine.
Increase IGC surveillance for PM's.
PWO'S UNIT 3 PWO SYSTEM 8'ATE PROBLEM C3 17705 C317706 C318495 C401006 99 99 99 99 01/13/88 01/13/88 12/14/87 05/13/88 Bin A-1 Ch.l Not sounding Bin A-1 Ch.Z Not sounding Bin A-2 Ch.5 Excessive noise Bin A-3 Excessive false alarms PWO'S UNIT 4 C401455 C401463 C401110 C404701 99 99 99 99 06/06/88 06/11/88 06/06/88 04/12/88 Recorder doesn't work Allchannels - rushing noise Bin A-2 Ch.6 Constant false alarms Bin A-2 Ch.3 Inoperable Copies of PWO's attached, C401110 not found.