The following information was provided by the licensee via phone and email:
At 0924 EDT on April 1, 2026, it was determined that Unit 3 was in an unanalyzed condition because two emergency diesel generators (EDGs) were inoperable. One EDG was inoperable due to scheduled maintenance, and the second EDG was inoperable due to blocking for an emergent plant issue. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. The second EDG was returned to service, and the condition was exited.
This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D).
The NRC Resident Inspector has been notified.
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
Unit 2 was unaffected by this condition. No other limiting conditions exist. The second
EDG was blocked due to a failed transformer, but the transformer has been repaired.