LER-1983-011, Forwards LER 83-011/01T-0.Detailed Event Analysis Encl |
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s' DUKE POWER Coxiwsy P.O. DOK 33180 CHAMLOTTE. N.O. 28242 HAL H. TUCKER TELEPHONE
- - wwa enstasnewt (704) 373-4531 mer.Lram ruusseve-room c:
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Mr. James P. O'Reilly, Regional Administrator 3
, 7;j
- fo U. S. Nuclear Regulatory Commission m
Region II iy 101 Marietta Street NW, Suite 2900 3
.m Atlanta, Georgia 30303 E
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Re: McGuire Nuclear Station Unit 1
- . 7,
,c, Docket No. 50-369
Dear Mr. O'Reilly:
s Please find attached steportable Occurrence Report R0-369/83-11. This report concerns T.S.6.9.1.12(i), " Performance of structures, systems, or components that requires remedial action or corrective measures to prevent operation in a manner less conservative than assumed in the accident analysis report or Technical Specifications bases...".
This incident was considered to be of no significance with respect to the health and safety of the public.
Note that inspection of the non-fuel bearing components is still in progress and therefore an 3; curate assesonent of broken spring parts cannot presently be made. 'A follow-up report will be submitted to address this issue.
Very truly yours, 4
Hal B. Tucker PBN:jfw Attachment cc: Document Control Desk Records Center p
U. S. Nuclear Regulatory Commission Institute of Nuclear Power Operations i-Washington, D. C.
~20555 1100 circle 75 Parkway, Suite 1500 Atlanta, Georgia 30339 Mr. W. T. Orders Senior Resident Inspector McGuire Nuclear Station OFFICIAL COPY 0 000 b PDR
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. DUKE POWER COMPANY McGUIRE NUCLEAR STATION REPORTABLE OCCURRENCE REPORT NO. 369/83-11 I
j REPORT DATE: March 24, 1983 FACILITY: McGuire Unit 1, Cornelius, NC j
l IDENTIFICATION: Breaks Discovered in Non-Fuel Bearing Component Holddown
[
Springs
DESCRIPTION
On March 10, 1983, during inspection of the fuel assemblies, the holddown spring for a Non-Fuel Bearing Component (NFBC) was observed to be broken.
This discovery led to the inspection of all NFBC holddown assemblies for the Unit I core. Of the 94 NFBC's equipped with the same spring design, 21 were determined 1
to be broken. Of these 21 broken springs, three were identified as having double fractures such that a semicircular spring section might move free of the yoke guide and into the flow of the coolant system.
No immediate corrective action was required, as the fuel assemblies had been removed from the core.
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This incident is due to Design Deficiency, as the broken holddown springs are j
theorized to have resulted from fatigue failure.
EVALUATION: Prior to McGuire Unit 1 initial fuel loading, Westinghouse identified j
deficiencies in the design of-.holddown assembly springs of NFBC's (OHI Unit I had discovered breaks in NFBC holddown springs in April of 1980). The purpose of these springs is to hold the NFBC's (which include thimble plugs, burnable poison rods and sources) in the fuel assemblies, resisting the lifting force of reactor coolant flow. Experience at other plants had shown that springs identical to those at l
McGuire were prone to breakage in the first 3000 hours0.0347 days <br />0.833 hours <br />0.00496 weeks <br />0.00114 months <br /> of operation. The close i
match of spring and reactor coolant pump resonances was theorized to be a contri-t buting factor to the failures, as was poor spring heat-treating during manufacture.
L Another consideration was the barrel-shape of the spring, which placed the center l
coils further into the coolant flow path.
The~ analyses of that time-indicated that single location fractures were the most likely failure mode within the first fuel cycle. This was not considered a safety concern.
It was decided that old design springs in the NFBC holddown assemblies which were intended to remain in the core past the first cycle (thimble plugs and secondary sources) would be replaced with a new design.
i These matters were previously addressed in Mr. W. 0. Parker's November 18, 1980 letter to Mr. H. R. Denton (NRC/NRR) in which he responded to the NRC's earlier questions concerning the springs (letter from Mr, R. L. Tedesco (NRC/NRR) to Mr.
W. O. Parker, dated October 8, 1980).
The new design holddown spring has a cylindrical outline and is tuned to a higher frequency. It was installed in the holddown assemblies of the 44 thimble plugs i
and 2 secondary sources. This modification (exchanging spring designs) was completed by October 1980.
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Report No. 369/83-11 Page 2 Unit I has not been operated continuously at 100% full power _due to problems with steam generator design. Operating at 50% of full power has allowed the holddown-springs to undergo an equivalent full fucl cycle of stress (in hours) without having actually completed the cycle.
Af ter discovering the broken springs in the holddown assembly of 21 NFBC's, an inspection was. performed on the 46 new design springs used in the holddown assemblies of the thimble plugs and secondary sources.- All of these springs were confirmed to be intact and undamaged.
CORRECTIVE ACTION
Upon notification.of the broken springs, both Duke and Westinghouse began evaluation of alternate core designs which minimized or elimin-ated use of the defective holddown springs. A core design has been developed which reloads all fuel assemblies in their previous locations, replaces all burnable poison assemblies with thimble plugs, inserts two new secondary source assemblies, and reinserts the two secondary sources (each of which contain 16 partially depleted burnable poison rodlets). Therefore, all springs of the defective design have been removed from'the core.
A reload type safety evaluation is being performed by Westinghouse to justify. the modified core design. The purpose of.this evaluation is to verify that the existing nuclear design / safety parameters input to the FSAR Chapter 15 safety analyses are still bounding. This evaluation is being performed utilizing the methodology contained _in WCAP-9272 (Reload Safety Evaluation Methodology Topical).
It is currently anticipated that this modification to the core design will be accomplished under the provisions of 10 CFR 50.59.
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The primary consequences of the removal of old burnable poison rod assemblies are the potential extension of the-first cycle, and the necessity of additional core physics testing during the upcoming start-up. After core reload the following physics tests _are planned:
I.
Core Loading Core verification will be videotaped and checked in usual manner.
4 This assures fuel, control rod, secondary source, and thimble plugs j.
are properly located.
II.
Hot Zero Power Tests 1.
Isothermal Temperature Coefficient (ARO) 2.
Flux Map (ARO) 3.
Measurement of Control Rod Banks D aad C in sequence using boration/ dilution 4.
ARO Cirtical boron concentration l
III.
75% Power Tests 1.
Incore/Excore calibration
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e Report No. 369/83-11 Page-3 2.
Target Axial Flux Difference 3.
Flux map IV.
100% Power Tests 1.
Target Axial Flux Difference 2.
Power-Coefficient (to satisfy original test program) 3.
Flux map SAFETY (FALYSIS: By replacing the NFBC's containing old-design holddown springs with thimble plug assemblies incorporating new design springs, the likelihood of spring-failure will be significantly reduced.
Potential problems associated with springs in the holddcwn assemblies of NFBC's were thoroughly addressed in a Westinghouse analysis postulating effects of broken springs. Rodlet failure or thimble wear due to vibration of unrestrained assemblies, power distribution effects or bypass flow due to assembly lift, and reduction in Upper Head Injection inlet flow area were all determined to be negligible.
The potential for loose parts in the reactor coolant system was evaluated by Westing-house based upon single fractures of springs. Past experience had.shown this to be the only failure mode encountered. As Unit I was observed to have double fractures in the failed springs, these assumptions are not valid for this incident.
Three of the damaged springs were confirmed to have double breaks but all pieces; were retained about the hub af the handling portion of the core component. No other damage or indications of adverse wear was observed. Westinghouse represen-tatives have observed these assemblies and copies of TV tapes have been provided to them for their further investigation.
The inspection of NFBC's'is still in progress (involving lifting the assemblies to allow better camera access to the bottom of the barrel-shaped springs) and an accurate assessment of broken spring parts cannot presently be made. A follow-up i
report will be submitted to address this issue.
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| 05000369/LER-1983-001-03, /03L-0:on 830105,during Review of 791220 Safety Injection (SI) Pumps & Flow Adjustment Functional Test II, Discrepancy Discovered Between Test Data & Omitted Acceptance Criteria.Caused by Procedure Error | /03L-0:on 830105,during Review of 791220 Safety Injection (SI) Pumps & Flow Adjustment Functional Test II, Discrepancy Discovered Between Test Data & Omitted Acceptance Criteria.Caused by Procedure Error | | | 05000369/LER-1983-002-03, /03L-0:on 830110,while in Mode 1,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Cause Under Investigation.Design Defect Indicated in Vacuum Breaker Contractor Coil Circuit | /03L-0:on 830110,while in Mode 1,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Cause Under Investigation.Design Defect Indicated in Vacuum Breaker Contractor Coil Circuit | | | 05000369/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000369/LER-1983-003-03, /03L-0:on 830117,during Mode 1 Weekly Sampling Collection,Conventional Waste Water Treatment Composite Sampler Found Inoperable.Caused by Frozen Sample Line Due to Improper Installation of Insulation.Insulation Reinstalled | /03L-0:on 830117,during Mode 1 Weekly Sampling Collection,Conventional Waste Water Treatment Composite Sampler Found Inoperable.Caused by Frozen Sample Line Due to Improper Installation of Insulation.Insulation Reinstalled | | | 05000369/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000369/LER-1983-004-03, /03L-0:on 830121,during Monthly Battery Insp,Cell 9 of Battery Evca Had Specific Gravity Below Tech Spec Limit.Caused by Normal Degradation.Bus Evda Tied to Operable Battery Bank.Cell 9 Jumpered Out & Battery Returned to Svc | /03L-0:on 830121,during Monthly Battery Insp,Cell 9 of Battery Evca Had Specific Gravity Below Tech Spec Limit.Caused by Normal Degradation.Bus Evda Tied to Operable Battery Bank.Cell 9 Jumpered Out & Battery Returned to Svc | | | 05000369/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000369/LER-1983-005-03, /03L-0:on 830127,while in Mode 5,evaluation of Initial Ice Condenser Basket Weights Found Numerous Accessible Row 8 & 9 Baskets Had Net Ice Weights Below Tech Specs.Caused by Heat Loading & Air Current | /03L-0:on 830127,while in Mode 5,evaluation of Initial Ice Condenser Basket Weights Found Numerous Accessible Row 8 & 9 Baskets Had Net Ice Weights Below Tech Specs.Caused by Heat Loading & Air Current | | | 05000369/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-006-03, /03L-0:on 830131,unit Changed from Mode 5 to 6 W/ Control Room Area Outside Air Pressure Filter Train 2 (VC-B) Inoperable.Subj Train & VC Train a Inoperable on 830125,26 & 29.Caused by Misinterpretation of Tech Specs | /03L-0:on 830131,unit Changed from Mode 5 to 6 W/ Control Room Area Outside Air Pressure Filter Train 2 (VC-B) Inoperable.Subj Train & VC Train a Inoperable on 830125,26 & 29.Caused by Misinterpretation of Tech Specs | | | 05000369/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-007-03, /03L-0:on 830131,vent Radiation Monitors 1EMF-35, 36 & 37 Declared Inoperable Following Loss of Sample Flow Alarm.Caused by Clogged Charcoal Filter.Filter Replaced | /03L-0:on 830131,vent Radiation Monitors 1EMF-35, 36 & 37 Declared Inoperable Following Loss of Sample Flow Alarm.Caused by Clogged Charcoal Filter.Filter Replaced | | | 05000369/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000369/LER-1983-008-03, /03L-0:on 830124,weekly Composite Sample Analysis Not Performed for Conventional Waste Water Treatment Sys Continuous Discharge.Caused by Personnel Error & Procedural Deficiency.Procedures Will Be Changed by 830331 | /03L-0:on 830124,weekly Composite Sample Analysis Not Performed for Conventional Waste Water Treatment Sys Continuous Discharge.Caused by Personnel Error & Procedural Deficiency.Procedures Will Be Changed by 830331 | | | 05000369/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000369/LER-1983-009, Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-009-03, /03L-0:on 821112,during Troubleshooting & Checkout Activities Following Diesel Generator Mod Work,Diesel Generator 1B Experienced Failures.Caused by Wires on Wrong Terminal,Burned Diodes & Spurious Low Crankcase Signals | /03L-0:on 821112,during Troubleshooting & Checkout Activities Following Diesel Generator Mod Work,Diesel Generator 1B Experienced Failures.Caused by Wires on Wrong Terminal,Burned Diodes & Spurious Low Crankcase Signals | | | 05000369/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000369/LER-1983-010-03, /03L-0:on 830216,while in Mode 6,control Room Outside Air Intake Radiation Monitors 1EMF-43A &43B Declared Inoperable.Caused by Personnel Error.Monitors Returned to Svc & Inlet Valves Opened After Testing | /03L-0:on 830216,while in Mode 6,control Room Outside Air Intake Radiation Monitors 1EMF-43A &43B Declared Inoperable.Caused by Personnel Error.Monitors Returned to Svc & Inlet Valves Opened After Testing | | | 05000369/LER-1983-011-01, While Core Unloaded During Fuel Assembly insp,21 of 94 Nonfuel Bearing Components Equipped W/Same Spring Design Discovered W/Broken Holddown Springs.Caused by Design Deficiency | While Core Unloaded During Fuel Assembly insp,21 of 94 Nonfuel Bearing Components Equipped W/Same Spring Design Discovered W/Broken Holddown Springs.Caused by Design Deficiency | | | 05000369/LER-1983-011, Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-012-03, /03L-0:on 830302,four Existing Auxiliary Feedwater Flow Transmitters Determined Not Environmentally Qualified for 330 F Main Steam Break Environ.Transmitter Overlooked in Review Response to NUREG-0588 | /03L-0:on 830302,four Existing Auxiliary Feedwater Flow Transmitters Determined Not Environmentally Qualified for 330 F Main Steam Break Environ.Transmitter Overlooked in Review Response to NUREG-0588 | | | 05000369/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000369/LER-1983-013-03, /03L-0:on 830315,during Upperhead Injection Level Switch Calibr,Switches Found Out of Tolerance.Caused by Design Deficiency.Rev to Tech Specs Changing Switch Setpoint Submitted | /03L-0:on 830315,during Upperhead Injection Level Switch Calibr,Switches Found Out of Tolerance.Caused by Design Deficiency.Rev to Tech Specs Changing Switch Setpoint Submitted | | | 05000369/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-014-03, /03L-0:on 830303,routine Surveillance on Conventional Waste Water Sys Radiation Monitor 1EMF-31 Found Channel Out of Tolerance.Caused by Cracked Detector Crystal. Crystal Replaced W/High Temp Crystal | /03L-0:on 830303,routine Surveillance on Conventional Waste Water Sys Radiation Monitor 1EMF-31 Found Channel Out of Tolerance.Caused by Cracked Detector Crystal. Crystal Replaced W/High Temp Crystal | | | 05000369/LER-1983-014, Forwards LER 83-014/03L-0 | Forwards LER 83-014/03L-0 | | | 05000369/LER-1983-015, Forwards LER 83-015/03L-0 & 83-003/03L-0 | Forwards LER 83-015/03L-0 & 83-003/03L-0 | | | 05000369/LER-1983-015-03, /03L-0:on 830319 & 31,reactor Trip Breaker a Failed to Open on Undervoltage (UV) Trip Signal & Bypass Breaker B Failed to Trip on UV Signal,Respectively.Caused by Mechanical Problems W/Uv Mechanisms.Logic Modified | /03L-0:on 830319 & 31,reactor Trip Breaker a Failed to Open on Undervoltage (UV) Trip Signal & Bypass Breaker B Failed to Trip on UV Signal,Respectively.Caused by Mechanical Problems W/Uv Mechanisms.Logic Modified | | | 05000369/LER-1983-016-03, /03L-0:on 830327,hanger 1MCA-ND-H260 Discovered Pulled Loose from Wall Anchors & Snubbers 1MCA-ND-H177 & H317 Found Locked Up During Subsequent full-stroking.Caused by Water Hammer Event Resulting in Void Formation | /03L-0:on 830327,hanger 1MCA-ND-H260 Discovered Pulled Loose from Wall Anchors & Snubbers 1MCA-ND-H177 & H317 Found Locked Up During Subsequent full-stroking.Caused by Water Hammer Event Resulting in Void Formation | | | 05000369/LER-1983-016, Forwards LER 83-016/03L-0 | Forwards LER 83-016/03L-0 | | | 05000369/LER-1983-017-03, /03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised | /03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised | | | 05000369/LER-1983-017, Forwards LER 83-017/03L-0 | Forwards LER 83-017/03L-0 | | | 05000369/LER-1983-018-03, /03L-0:on 830407,following Identification of Inoperable RHR Sys (Nd) Hanger & Snubbers,Sys Walkdown Revealed Addl Hanger Failure.Caused by Nd Sys Water Hammer. Hangers Repaired & Procedures Revised | /03L-0:on 830407,following Identification of Inoperable RHR Sys (Nd) Hanger & Snubbers,Sys Walkdown Revealed Addl Hanger Failure.Caused by Nd Sys Water Hammer. Hangers Repaired & Procedures Revised | | | 05000369/LER-1983-019-03, /03L-0:on 830413,representative Fuel Pool Ventilation Sys Carbon Filter Sample Analysis Indicated Sample Failed to Meet Methyl Iodide Penetration Criteria. Sample Analyses Made to Determine Cause | /03L-0:on 830413,representative Fuel Pool Ventilation Sys Carbon Filter Sample Analysis Indicated Sample Failed to Meet Methyl Iodide Penetration Criteria. Sample Analyses Made to Determine Cause | | | 05000369/LER-1983-020-01, /01T-0:on 830503,soap Bubble Test of 47 Secondary Containment Bypass Leakage Paths Not Performed During Initial Integrated Leak Rate Test.Caused by Procedural Deficiency.Procedures Revised | /01T-0:on 830503,soap Bubble Test of 47 Secondary Containment Bypass Leakage Paths Not Performed During Initial Integrated Leak Rate Test.Caused by Procedural Deficiency.Procedures Revised | | | 05000369/LER-1983-021-03, /03L-0:on 830419,while in Mode 5,nuclear Svc Water Sys Valve 1RN-69 Actuator W/Mechanical Latch Replaced by Actuator Requiring Electrical Antihammer Circuit.Caused by Deficient Procedure | /03L-0:on 830419,while in Mode 5,nuclear Svc Water Sys Valve 1RN-69 Actuator W/Mechanical Latch Replaced by Actuator Requiring Electrical Antihammer Circuit.Caused by Deficient Procedure | | | 05000369/LER-1983-022-03, /03L-0:on 830421,bellows Leak Test Not Performed on Penetration M354 After Initial Integrated Leak Rate Test.Caused by Procedural Deficiency Since Penetration Not Listed in Initial Procedures | /03L-0:on 830421,bellows Leak Test Not Performed on Penetration M354 After Initial Integrated Leak Rate Test.Caused by Procedural Deficiency Since Penetration Not Listed in Initial Procedures | | | 05000369/LER-1983-023-01, /01T-0:on 830506,discovered That RHR Sys (Nd) Train a Improperly Declared Operable on 830423 & Subsequent Change from Mode 5 to Mode 4 Occurred on 830428.Caused by Water Hammer Failures | /01T-0:on 830506,discovered That RHR Sys (Nd) Train a Improperly Declared Operable on 830423 & Subsequent Change from Mode 5 to Mode 4 Occurred on 830428.Caused by Water Hammer Failures | | | 05000369/LER-1983-024-03, /03L-0:on 830426,Fire Door 1000B Declared Inoperable When Damage,Consisting of Bent Door,Broken Hinge, Bent Hinge,Broken Door Lock & Broken Door Closer Discovered. Cause Unknown.Fire Watch Established | /03L-0:on 830426,Fire Door 1000B Declared Inoperable When Damage,Consisting of Bent Door,Broken Hinge, Bent Hinge,Broken Door Lock & Broken Door Closer Discovered. Cause Unknown.Fire Watch Established | | | 05000369/LER-1983-025-03, /03L-0:on 830508,while in Mode 2,fire Detection Sys Zones 72 & 149 Declared Inoperable Due to Alarms Remaining in Alarm Condition.Fire Watch Patrols Established. Caused by Control Interface Module failure.W830527 Ltr | /03L-0:on 830508,while in Mode 2,fire Detection Sys Zones 72 & 149 Declared Inoperable Due to Alarms Remaining in Alarm Condition.Fire Watch Patrols Established. Caused by Control Interface Module failure.W830527 Ltr | | | 05000369/LER-1983-026-03, /03L-0:on 830430,performance of RCS Leakage Calculation Determined Unidentified Leakage Greater than 1 Gpm.Caused by Leakage Past Bonnet Seal Ring on Valves 1NC-18 & 1NV-239.Valves Sealed | /03L-0:on 830430,performance of RCS Leakage Calculation Determined Unidentified Leakage Greater than 1 Gpm.Caused by Leakage Past Bonnet Seal Ring on Valves 1NC-18 & 1NV-239.Valves Sealed | | | 05000369/LER-1983-027-03, /03L-0:on 830505,discovery of Water in Outside Air Pressure Filter Train 2 Led to Control Area Ventilation Sys Train B Inoperability.Caused by Water Backflow Through Drain Lines Into Filter Package.Filter Cleaned | /03L-0:on 830505,discovery of Water in Outside Air Pressure Filter Train 2 Led to Control Area Ventilation Sys Train B Inoperability.Caused by Water Backflow Through Drain Lines Into Filter Package.Filter Cleaned | | | 05000369/LER-1983-028-01, /01T-0:on 830525,impulse Lines for Two Redundant Steam Generator 1D Level Instruments Came within 2 Inches of Each Other at One Point.Caused by Const/Installation Deficiency.One Line Rerouted | /01T-0:on 830525,impulse Lines for Two Redundant Steam Generator 1D Level Instruments Came within 2 Inches of Each Other at One Point.Caused by Const/Installation Deficiency.One Line Rerouted | | | 05000369/LER-1983-029-03, /03L-0:on 830510 & 15,boron Concentration Dropped Below 1,900 Ppm in Cold Leg Injection Accumulator.Caused by Leakage Into Accumulator from RCS Through Check Valves 1NI70 & 1NI71.Valves Repaired | /03L-0:on 830510 & 15,boron Concentration Dropped Below 1,900 Ppm in Cold Leg Injection Accumulator.Caused by Leakage Into Accumulator from RCS Through Check Valves 1NI70 & 1NI71.Valves Repaired | | | 05000369/LER-1983-029-01, /01T-0:on 830601,Westinghouse Notified Util That Extended Operation at Low Power & Subsequent Escalation to Power in Same Fuel Cycle Would Result in Heat Flux Hot Channel Factor Limit Violations for LOCA Analysis | /01T-0:on 830601,Westinghouse Notified Util That Extended Operation at Low Power & Subsequent Escalation to Power in Same Fuel Cycle Would Result in Heat Flux Hot Channel Factor Limit Violations for LOCA Analysis | | | 05000369/LER-1983-030-01, /01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules Recalibr | /01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules Recalibr | | | 05000369/LER-1983-031-03, /03L-0:on 830512,reactor Coolant Pump Taken Out of Svc Following Sporadic Low Oil Level Alarms from Pump Motor 1D Upper Reservoir.Level Found Slightly Low.Cause Not Determined.Oil Added.Pump Restarted | /03L-0:on 830512,reactor Coolant Pump Taken Out of Svc Following Sporadic Low Oil Level Alarms from Pump Motor 1D Upper Reservoir.Level Found Slightly Low.Cause Not Determined.Oil Added.Pump Restarted | | | 05000369/LER-1983-032-03, /03L-0:on 830513,control Area Ventilation Sys Train a Failed to Meet Pressurization Criteria.Caused by Degradation of Door Seals & Lack of Trip Interlocks.Door Seals Taped & Later Replaced.Test Rerun | /03L-0:on 830513,control Area Ventilation Sys Train a Failed to Meet Pressurization Criteria.Caused by Degradation of Door Seals & Lack of Trip Interlocks.Door Seals Taped & Later Replaced.Test Rerun | | | 05000369/LER-1983-033-03, /03L-0:on 830701,two Programmed Setpoint Circuit Cards of Each Steam Generator Water Level low-low Channel Not Tested During Required Monthly Surveillance.Cause Not Known.Monthly Surveillance Procedure Revised | /03L-0:on 830701,two Programmed Setpoint Circuit Cards of Each Steam Generator Water Level low-low Channel Not Tested During Required Monthly Surveillance.Cause Not Known.Monthly Surveillance Procedure Revised | |
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