LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl |
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March 2, 1983 Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 2900 Atlanta, Georgia 30303 he: McGuirs Nuclear Station Unit 1 Docket No. 50-369
Dear Mr.-O'Reilly:
Please find attached Reportable Occurrence Repcrt EO-369/33-06. This report concerns T.S. 3.7.6, "Two independent control area ventilation systems shall be operable", and T.S. 3.0.4, " Entry into an OFERATIONAL MODE or other speci-fied condition shall not be made unless the conditions of the limiting condi-tion for operation are met without reliance on provisions contained in the liCT10N requirements". Titis incident was considered to be of no significance with respect to the health and asfety of the public.
Very truly yours,
- B. "Ad/
Hal B. Tucker PBN:j fw Attachment cc: Document Control Desk Records Center U. S. Nuclear Regulatory Commission Institute of Nuclear Power Operations Washington, D. C.
20555 1100 circle 75 Parkway, Suite 1500 Atlanta, Georgia 30339 Senior Resident Inspector McGuire Nuclear Station
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DUKE POWER COMPANY McGUIRE NUCLEAR STATION REPORTABLE OCCURRENCE REPORT NO._8_3-06 REPORT DATE: March 2, 1983 FACILITY: McGuire Unit 1, Cornelius, NC IDENTIFICATION: Changed from Mode 5 to 6 with Control Area Ventilation System Train B Inoperable
INTRODUCTION
On January 25, 1983, during Mcdc 5, the Control Rcon Area Outside Air Pressure Filter Train 2 (VC-B) was declared looperc61e. This resulted from the discovery of water-damaged componen:s in the filter packcge.
A faulty loop-seal level control, which isolates filter component drain linee to prevent bypass air flow and drain line backflow, was identified as the
cause
This level control allowed water to back up into the filter package, During Mode 5, no immediate corrective action is required, nor was taket.. upon J
declaring one VC train inoperable. A work request was written to retern VC-B Train to aa operable status. VC-B Train's inoparability io classified ss an Installation Deficiency, since the float operated level control was inproperly installed and adjusted.
VC-A Train was also declared inoperable for several hours on 1/26-27/83, ard again on 1/29/33. This was due to maintenance work on 1FD145 and IPDI44, Fuel Oil Transfer Filter lA2 1 solation valves, which required Diesel Generator IA, and therefore the emergency bus feeding VC-A Train, be declared inoperable.
On 1/31/83, with the VC-B Train still inoperable, the Unit I reactor vessel head was detensioned,'thus entering Mode 6.
Although Technical Specification 3.7.6 Action requirements for Modes 5 and 6 do not address possible mode changes while a VC train is inoperable, Operations personnel evaluated the change to Mode 6 as being no different than continued operation in Mode 5.
Upon review of this action, Duke Power has interpreted this mode change as being a violation of Technical Specification 3.0.4.
This specification states that an operational mode shall not be entered by relying on the action requirements for the opera-bility of an applicable system, unless entering or passing through such a mode as prescribed in the action requirements. This difference in interpretation of the allowability of mode changes is classified as an Administrative Deficiency.
EVALUATION: When preparing to load carbon into the Unit 2 Annulus Ventilation System filter package, water was discovered in the housings of both filter trains.
The source of the water was determined to be the Make-up Demineralizer Water System (YM), which provides water to filter package loop-seals. The YM source was then isolated.
Further investigation revealed water had entered the Outside Air Pressure Filter Train 2 (VC-B).
Water entered this filter package, a shared unit system, along with other Unit 2 filter packages, by overfilling the level control tanks and backing up the condensate drain lines. The loop-seal level control (McDonnell and Miller, Inc., Model No. 847 Make-up Water Feeder) had been installed in dry lines and allowed to rust, and had not been properly adjusted.
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Report No. 83-06 Page 2 YM system overflow from the VC-B Train level control tank shares a common drain line with other filter package loop-seals. The loop-seals of these Unit 2 filter packages (not yet loaded or in service) were also improperly adjusted, allowing YM system flow to continue even though the loop-seal level control tanks were full. This unchecked flow exceeded the capacity of the 2 1/2" common drain lines, creating the potential for backflow. This was the case in the VC-E Train filter package, where the carbon bed and HEPA filters were damaged.
On 1/26/83, Diesel Generator (D/G) 1A was declared inoperable due to a leaking diaphragm on Fuel Oil Transfer Filter 1A2 isolation valvo 1FD145. The diaphragm 1
was replaced. During the time that maintenance was performed on 1FD145, VC-A 1 rain was declared inoperable due to loss of the emergency bus (supplied by D/G 1A). D/G IA and VC-A Train were returned to operable status on 2/27/83.
Further maintenance work was required on 1/29/83, resulting in D/G 1A and VC-A Train being declared inoperable.
(The leaking diaphragm of 1FD144, the second Fuel 011 Transfer Filter isolation valve, was replaced).
In both cases, the diaphragm had become oil-saturated and began to leak, requiring replacement.
Replacement diaphragms for these 2" Grinnell Diaphragm Values are rated for a five year life.
The Action Statements for Techaical Specification 3.7.6, under which VC-B was declared inoperable, cre segregated into two classes. Action prescribed for Modes 1,2,3 and 4 and that of Modes 5 and 6 are listed separately. Changing modes with VC-B Train declared inoperable was the result of an Operations interpretation of Technical Specification 3.7.6, which does not differentiate between action statements applicable during Modes 5 or 6.
As no differences existed in regards to VC System inoperability for the two modes, the mode change was evaluated as having no effect. However, Duke Power's subsequent reevaluation of the mode change (after Mode 6 had been entered) was based upon the failure of the VC system to meet the Limiting Condition for Operation. This was interpreted as a violation of the Technical Specification for Applicability, 3.0.4.
SAFETY ANALYSIS
As the exact time that water entered the Outside Air Pressure Filter Train 2 cannot be determined, a conservative assumption that the incident occurred with Unit 1 in Mode I should be made. The VC system includes two 100%
filter trains for the purpose of cleaning control room air (1000 cfm recirculating) and introducing clean fresh air (1000 cfm outside) in the case of an accident.
Impairment of this function by wetting the filter components would be minimal.
The removed HEPA filter showed no holes or displacement of media, and would have still performed efficient particulate removal, if required. The wet carbon in the bottom of the bed combined with the wet portion of the HEPA filter would raise the differential pressure across the filter package and thereby reduce design flow rate. By this means, the condition of the filter train could have been discovered had the system operation been required.
In such a case, the redundant train was available for use.
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Report No. 83-06 Page 3 Prior to working on D/G 1A, and disabling emergency power to VC-A Train, Unit 1 entered Mode 5.
Action specified when both VC trains are inoperable in Modes 5 or 6 is the disallowance of positive changes in reactivity or core alterations.
These conditions were met.
Changing modec with one train of VC inoperable had no impact, as the action statament does not change froc Mode 5 to 6.
Operations parsonnel are ucli J
cuare that an increase in operational mode (i.e., proceeding through start-up) requires prior VC system operability.
Ihis incident had no effect upon the health and safety of the public.
CORRECTIVE ACTION
After discovering water-damaged filtcr components in the Outside Air Pressure Filter Train 2, the carbon bed and installed HEPA filters 4
were removed, the filter housing cleaned, and filters reloaded. As water had entered the system by backing up the drain lines, the possibility of line bicekage downstream of the filter packages was investigated. Downstreau drain lines were cut and inspected for obstructions in several places. No obstruc-tions were encountered, and piping was rejoined.
The loop-seal level controls were then checked and found to be improperly adjusted and rusted. This was attribated to their having been installed in dry lines. The aake-up water 4
feeders were cleaned and properly adjusted.
Reloaded carbon and HEPA filters in the Outside Air Pressure Filter Train 2 were tested per "In-Place Test of HEPA and Carbon Adsorber Filters" The system was returned to service on 2/3/83. Proper loop-seal level control was functionally tested by aligning YM supply to the loop and monitoring flow with the instrumenta-tion provided. The loop-seal filled and then allowed no further flow.
In order to eliminate any future confusion arising from a change from Mode 5 to 6, a change in Technical Specification 3.7.6 is being pursued. This change will list an exception to Technical Specification 3.0.4 in the Action Statements for Modes 5 and 6.
This will then explicitly permit such a mode change (in either direction) with a VC train inoperable. The next issue date for Technical Specif1-cations will be prior to Unit 2 fuel' loading.
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| 05000369/LER-1983-001-03, /03L-0:on 830105,during Review of 791220 Safety Injection (SI) Pumps & Flow Adjustment Functional Test II, Discrepancy Discovered Between Test Data & Omitted Acceptance Criteria.Caused by Procedure Error | /03L-0:on 830105,during Review of 791220 Safety Injection (SI) Pumps & Flow Adjustment Functional Test II, Discrepancy Discovered Between Test Data & Omitted Acceptance Criteria.Caused by Procedure Error | | | 05000369/LER-1983-002-03, /03L-0:on 830110,while in Mode 1,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Cause Under Investigation.Design Defect Indicated in Vacuum Breaker Contractor Coil Circuit | /03L-0:on 830110,while in Mode 1,pressurizer Heater Group 1B Failed to Energize in Manual & Declared Inoperable.Cause Under Investigation.Design Defect Indicated in Vacuum Breaker Contractor Coil Circuit | | | 05000369/LER-1983-002, Forwards LER 83-002/03L-0 | Forwards LER 83-002/03L-0 | | | 05000369/LER-1983-003-03, /03L-0:on 830117,during Mode 1 Weekly Sampling Collection,Conventional Waste Water Treatment Composite Sampler Found Inoperable.Caused by Frozen Sample Line Due to Improper Installation of Insulation.Insulation Reinstalled | /03L-0:on 830117,during Mode 1 Weekly Sampling Collection,Conventional Waste Water Treatment Composite Sampler Found Inoperable.Caused by Frozen Sample Line Due to Improper Installation of Insulation.Insulation Reinstalled | | | 05000369/LER-1983-003, Forwards LER 83-003/03L-0 | Forwards LER 83-003/03L-0 | | | 05000369/LER-1983-004-03, /03L-0:on 830121,during Monthly Battery Insp,Cell 9 of Battery Evca Had Specific Gravity Below Tech Spec Limit.Caused by Normal Degradation.Bus Evda Tied to Operable Battery Bank.Cell 9 Jumpered Out & Battery Returned to Svc | /03L-0:on 830121,during Monthly Battery Insp,Cell 9 of Battery Evca Had Specific Gravity Below Tech Spec Limit.Caused by Normal Degradation.Bus Evda Tied to Operable Battery Bank.Cell 9 Jumpered Out & Battery Returned to Svc | | | 05000369/LER-1983-004, Forwards LER 83-004/03L-0 | Forwards LER 83-004/03L-0 | | | 05000369/LER-1983-005-03, /03L-0:on 830127,while in Mode 5,evaluation of Initial Ice Condenser Basket Weights Found Numerous Accessible Row 8 & 9 Baskets Had Net Ice Weights Below Tech Specs.Caused by Heat Loading & Air Current | /03L-0:on 830127,while in Mode 5,evaluation of Initial Ice Condenser Basket Weights Found Numerous Accessible Row 8 & 9 Baskets Had Net Ice Weights Below Tech Specs.Caused by Heat Loading & Air Current | | | 05000369/LER-1983-005, Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | Forwards LER 83-005/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-006-03, /03L-0:on 830131,unit Changed from Mode 5 to 6 W/ Control Room Area Outside Air Pressure Filter Train 2 (VC-B) Inoperable.Subj Train & VC Train a Inoperable on 830125,26 & 29.Caused by Misinterpretation of Tech Specs | /03L-0:on 830131,unit Changed from Mode 5 to 6 W/ Control Room Area Outside Air Pressure Filter Train 2 (VC-B) Inoperable.Subj Train & VC Train a Inoperable on 830125,26 & 29.Caused by Misinterpretation of Tech Specs | | | 05000369/LER-1983-006, Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | Forwards LER 83-006/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-007-03, /03L-0:on 830131,vent Radiation Monitors 1EMF-35, 36 & 37 Declared Inoperable Following Loss of Sample Flow Alarm.Caused by Clogged Charcoal Filter.Filter Replaced | /03L-0:on 830131,vent Radiation Monitors 1EMF-35, 36 & 37 Declared Inoperable Following Loss of Sample Flow Alarm.Caused by Clogged Charcoal Filter.Filter Replaced | | | 05000369/LER-1983-007, Forwards LER 83-007/03L-0 | Forwards LER 83-007/03L-0 | | | 05000369/LER-1983-008-03, /03L-0:on 830124,weekly Composite Sample Analysis Not Performed for Conventional Waste Water Treatment Sys Continuous Discharge.Caused by Personnel Error & Procedural Deficiency.Procedures Will Be Changed by 830331 | /03L-0:on 830124,weekly Composite Sample Analysis Not Performed for Conventional Waste Water Treatment Sys Continuous Discharge.Caused by Personnel Error & Procedural Deficiency.Procedures Will Be Changed by 830331 | | | 05000369/LER-1983-008, Forwards LER 83-008/03L-0 | Forwards LER 83-008/03L-0 | | | 05000369/LER-1983-009, Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | Forwards LER 83-009/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-009-03, /03L-0:on 821112,during Troubleshooting & Checkout Activities Following Diesel Generator Mod Work,Diesel Generator 1B Experienced Failures.Caused by Wires on Wrong Terminal,Burned Diodes & Spurious Low Crankcase Signals | /03L-0:on 821112,during Troubleshooting & Checkout Activities Following Diesel Generator Mod Work,Diesel Generator 1B Experienced Failures.Caused by Wires on Wrong Terminal,Burned Diodes & Spurious Low Crankcase Signals | | | 05000369/LER-1983-010, Forwards LER 83-010/03L-0 | Forwards LER 83-010/03L-0 | | | 05000369/LER-1983-010-03, /03L-0:on 830216,while in Mode 6,control Room Outside Air Intake Radiation Monitors 1EMF-43A &43B Declared Inoperable.Caused by Personnel Error.Monitors Returned to Svc & Inlet Valves Opened After Testing | /03L-0:on 830216,while in Mode 6,control Room Outside Air Intake Radiation Monitors 1EMF-43A &43B Declared Inoperable.Caused by Personnel Error.Monitors Returned to Svc & Inlet Valves Opened After Testing | | | 05000369/LER-1983-011-01, While Core Unloaded During Fuel Assembly insp,21 of 94 Nonfuel Bearing Components Equipped W/Same Spring Design Discovered W/Broken Holddown Springs.Caused by Design Deficiency | While Core Unloaded During Fuel Assembly insp,21 of 94 Nonfuel Bearing Components Equipped W/Same Spring Design Discovered W/Broken Holddown Springs.Caused by Design Deficiency | | | 05000369/LER-1983-011, Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | Forwards LER 83-011/01T-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-012-03, /03L-0:on 830302,four Existing Auxiliary Feedwater Flow Transmitters Determined Not Environmentally Qualified for 330 F Main Steam Break Environ.Transmitter Overlooked in Review Response to NUREG-0588 | /03L-0:on 830302,four Existing Auxiliary Feedwater Flow Transmitters Determined Not Environmentally Qualified for 330 F Main Steam Break Environ.Transmitter Overlooked in Review Response to NUREG-0588 | | | 05000369/LER-1983-012, Forwards LER 83-012/03L-0 | Forwards LER 83-012/03L-0 | | | 05000369/LER-1983-013-03, /03L-0:on 830315,during Upperhead Injection Level Switch Calibr,Switches Found Out of Tolerance.Caused by Design Deficiency.Rev to Tech Specs Changing Switch Setpoint Submitted | /03L-0:on 830315,during Upperhead Injection Level Switch Calibr,Switches Found Out of Tolerance.Caused by Design Deficiency.Rev to Tech Specs Changing Switch Setpoint Submitted | | | 05000369/LER-1983-013, Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | Forwards LER 83-013/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1983-014-03, /03L-0:on 830303,routine Surveillance on Conventional Waste Water Sys Radiation Monitor 1EMF-31 Found Channel Out of Tolerance.Caused by Cracked Detector Crystal. Crystal Replaced W/High Temp Crystal | /03L-0:on 830303,routine Surveillance on Conventional Waste Water Sys Radiation Monitor 1EMF-31 Found Channel Out of Tolerance.Caused by Cracked Detector Crystal. Crystal Replaced W/High Temp Crystal | | | 05000369/LER-1983-014, Forwards LER 83-014/03L-0 | Forwards LER 83-014/03L-0 | | | 05000369/LER-1983-015, Forwards LER 83-015/03L-0 & 83-003/03L-0 | Forwards LER 83-015/03L-0 & 83-003/03L-0 | | | 05000369/LER-1983-015-03, /03L-0:on 830319 & 31,reactor Trip Breaker a Failed to Open on Undervoltage (UV) Trip Signal & Bypass Breaker B Failed to Trip on UV Signal,Respectively.Caused by Mechanical Problems W/Uv Mechanisms.Logic Modified | /03L-0:on 830319 & 31,reactor Trip Breaker a Failed to Open on Undervoltage (UV) Trip Signal & Bypass Breaker B Failed to Trip on UV Signal,Respectively.Caused by Mechanical Problems W/Uv Mechanisms.Logic Modified | | | 05000369/LER-1983-016-03, /03L-0:on 830327,hanger 1MCA-ND-H260 Discovered Pulled Loose from Wall Anchors & Snubbers 1MCA-ND-H177 & H317 Found Locked Up During Subsequent full-stroking.Caused by Water Hammer Event Resulting in Void Formation | /03L-0:on 830327,hanger 1MCA-ND-H260 Discovered Pulled Loose from Wall Anchors & Snubbers 1MCA-ND-H177 & H317 Found Locked Up During Subsequent full-stroking.Caused by Water Hammer Event Resulting in Void Formation | | | 05000369/LER-1983-016, Forwards LER 83-016/03L-0 | Forwards LER 83-016/03L-0 | | | 05000369/LER-1983-017-03, /03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised | /03L-0:on 830405,during Draining of Refueling Cavity RHR (Nd) Pumps Began to Cavitate & Eventually Both Nd Pumps Stopped.Caused by Level Gauge Isolation.Cavity Refilled.Nd Sys Vented.Procedures Revised | | | 05000369/LER-1983-017, Forwards LER 83-017/03L-0 | Forwards LER 83-017/03L-0 | | | 05000369/LER-1983-018-03, /03L-0:on 830407,following Identification of Inoperable RHR Sys (Nd) Hanger & Snubbers,Sys Walkdown Revealed Addl Hanger Failure.Caused by Nd Sys Water Hammer. Hangers Repaired & Procedures Revised | /03L-0:on 830407,following Identification of Inoperable RHR Sys (Nd) Hanger & Snubbers,Sys Walkdown Revealed Addl Hanger Failure.Caused by Nd Sys Water Hammer. Hangers Repaired & Procedures Revised | | | 05000369/LER-1983-019-03, /03L-0:on 830413,representative Fuel Pool Ventilation Sys Carbon Filter Sample Analysis Indicated Sample Failed to Meet Methyl Iodide Penetration Criteria. Sample Analyses Made to Determine Cause | /03L-0:on 830413,representative Fuel Pool Ventilation Sys Carbon Filter Sample Analysis Indicated Sample Failed to Meet Methyl Iodide Penetration Criteria. Sample Analyses Made to Determine Cause | | | 05000369/LER-1983-020-01, /01T-0:on 830503,soap Bubble Test of 47 Secondary Containment Bypass Leakage Paths Not Performed During Initial Integrated Leak Rate Test.Caused by Procedural Deficiency.Procedures Revised | /01T-0:on 830503,soap Bubble Test of 47 Secondary Containment Bypass Leakage Paths Not Performed During Initial Integrated Leak Rate Test.Caused by Procedural Deficiency.Procedures Revised | | | 05000369/LER-1983-021-03, /03L-0:on 830419,while in Mode 5,nuclear Svc Water Sys Valve 1RN-69 Actuator W/Mechanical Latch Replaced by Actuator Requiring Electrical Antihammer Circuit.Caused by Deficient Procedure | /03L-0:on 830419,while in Mode 5,nuclear Svc Water Sys Valve 1RN-69 Actuator W/Mechanical Latch Replaced by Actuator Requiring Electrical Antihammer Circuit.Caused by Deficient Procedure | | | 05000369/LER-1983-022-03, /03L-0:on 830421,bellows Leak Test Not Performed on Penetration M354 After Initial Integrated Leak Rate Test.Caused by Procedural Deficiency Since Penetration Not Listed in Initial Procedures | /03L-0:on 830421,bellows Leak Test Not Performed on Penetration M354 After Initial Integrated Leak Rate Test.Caused by Procedural Deficiency Since Penetration Not Listed in Initial Procedures | | | 05000369/LER-1983-023-01, /01T-0:on 830506,discovered That RHR Sys (Nd) Train a Improperly Declared Operable on 830423 & Subsequent Change from Mode 5 to Mode 4 Occurred on 830428.Caused by Water Hammer Failures | /01T-0:on 830506,discovered That RHR Sys (Nd) Train a Improperly Declared Operable on 830423 & Subsequent Change from Mode 5 to Mode 4 Occurred on 830428.Caused by Water Hammer Failures | | | 05000369/LER-1983-024-03, /03L-0:on 830426,Fire Door 1000B Declared Inoperable When Damage,Consisting of Bent Door,Broken Hinge, Bent Hinge,Broken Door Lock & Broken Door Closer Discovered. Cause Unknown.Fire Watch Established | /03L-0:on 830426,Fire Door 1000B Declared Inoperable When Damage,Consisting of Bent Door,Broken Hinge, Bent Hinge,Broken Door Lock & Broken Door Closer Discovered. Cause Unknown.Fire Watch Established | | | 05000369/LER-1983-025-03, /03L-0:on 830508,while in Mode 2,fire Detection Sys Zones 72 & 149 Declared Inoperable Due to Alarms Remaining in Alarm Condition.Fire Watch Patrols Established. Caused by Control Interface Module failure.W830527 Ltr | /03L-0:on 830508,while in Mode 2,fire Detection Sys Zones 72 & 149 Declared Inoperable Due to Alarms Remaining in Alarm Condition.Fire Watch Patrols Established. Caused by Control Interface Module failure.W830527 Ltr | | | 05000369/LER-1983-026-03, /03L-0:on 830430,performance of RCS Leakage Calculation Determined Unidentified Leakage Greater than 1 Gpm.Caused by Leakage Past Bonnet Seal Ring on Valves 1NC-18 & 1NV-239.Valves Sealed | /03L-0:on 830430,performance of RCS Leakage Calculation Determined Unidentified Leakage Greater than 1 Gpm.Caused by Leakage Past Bonnet Seal Ring on Valves 1NC-18 & 1NV-239.Valves Sealed | | | 05000369/LER-1983-027-03, /03L-0:on 830505,discovery of Water in Outside Air Pressure Filter Train 2 Led to Control Area Ventilation Sys Train B Inoperability.Caused by Water Backflow Through Drain Lines Into Filter Package.Filter Cleaned | /03L-0:on 830505,discovery of Water in Outside Air Pressure Filter Train 2 Led to Control Area Ventilation Sys Train B Inoperability.Caused by Water Backflow Through Drain Lines Into Filter Package.Filter Cleaned | | | 05000369/LER-1983-028-01, /01T-0:on 830525,impulse Lines for Two Redundant Steam Generator 1D Level Instruments Came within 2 Inches of Each Other at One Point.Caused by Const/Installation Deficiency.One Line Rerouted | /01T-0:on 830525,impulse Lines for Two Redundant Steam Generator 1D Level Instruments Came within 2 Inches of Each Other at One Point.Caused by Const/Installation Deficiency.One Line Rerouted | | | 05000369/LER-1983-029-03, /03L-0:on 830510 & 15,boron Concentration Dropped Below 1,900 Ppm in Cold Leg Injection Accumulator.Caused by Leakage Into Accumulator from RCS Through Check Valves 1NI70 & 1NI71.Valves Repaired | /03L-0:on 830510 & 15,boron Concentration Dropped Below 1,900 Ppm in Cold Leg Injection Accumulator.Caused by Leakage Into Accumulator from RCS Through Check Valves 1NI70 & 1NI71.Valves Repaired | | | 05000369/LER-1983-029-01, /01T-0:on 830601,Westinghouse Notified Util That Extended Operation at Low Power & Subsequent Escalation to Power in Same Fuel Cycle Would Result in Heat Flux Hot Channel Factor Limit Violations for LOCA Analysis | /01T-0:on 830601,Westinghouse Notified Util That Extended Operation at Low Power & Subsequent Escalation to Power in Same Fuel Cycle Would Result in Heat Flux Hot Channel Factor Limit Violations for LOCA Analysis | | | 05000369/LER-1983-030-01, /01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules Recalibr | /01T-0:on 830526,discovered Monthly Test of Containment Pressure Control Sys Failed to Satisfy Surveillance Requirements to Check Permissive/Termination Setpoint Accuracy.Alarm Modules Recalibr | | | 05000369/LER-1983-031-03, /03L-0:on 830512,reactor Coolant Pump Taken Out of Svc Following Sporadic Low Oil Level Alarms from Pump Motor 1D Upper Reservoir.Level Found Slightly Low.Cause Not Determined.Oil Added.Pump Restarted | /03L-0:on 830512,reactor Coolant Pump Taken Out of Svc Following Sporadic Low Oil Level Alarms from Pump Motor 1D Upper Reservoir.Level Found Slightly Low.Cause Not Determined.Oil Added.Pump Restarted | | | 05000369/LER-1983-032-03, /03L-0:on 830513,control Area Ventilation Sys Train a Failed to Meet Pressurization Criteria.Caused by Degradation of Door Seals & Lack of Trip Interlocks.Door Seals Taped & Later Replaced.Test Rerun | /03L-0:on 830513,control Area Ventilation Sys Train a Failed to Meet Pressurization Criteria.Caused by Degradation of Door Seals & Lack of Trip Interlocks.Door Seals Taped & Later Replaced.Test Rerun | | | 05000369/LER-1983-033-03, /03L-0:on 830701,two Programmed Setpoint Circuit Cards of Each Steam Generator Water Level low-low Channel Not Tested During Required Monthly Surveillance.Cause Not Known.Monthly Surveillance Procedure Revised | /03L-0:on 830701,two Programmed Setpoint Circuit Cards of Each Steam Generator Water Level low-low Channel Not Tested During Required Monthly Surveillance.Cause Not Known.Monthly Surveillance Procedure Revised | |
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