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Category:Letter
MONTHYEARIR 05000336/20240032024-11-0707 November 2024 Integrated Inspection Report 05000336/2024003 and 05000423/2024003 and Apparent Violation and Independent Spent Fuel Storage Installation Inspection Report 07200008/2024001 ML24289A0152024-10-21021 October 2024 Review of the Fall 2023 Steam Generator Tube Inspection Report 05000423/LER-2024-001, Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary2024-10-14014 October 2024 Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary IR 05000336/20244022024-10-0808 October 2024 Security Baseline Inspection Report 05000336/2024402 and 05000423/2024402 (Cover Letter Only) ML24281A1102024-10-0707 October 2024 Requalification Program Inspection 05000423/LER-2023-006-02, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-09-26026 September 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24260A2192024-09-16016 September 2024 Decommissioning Trust Fund Disbursement - Revision to Previous Thirty-Day Written Notification ML24260A1952024-09-16016 September 2024 Response to Request for Additional Information Regarding Proposed Amendment to Support Implementation of Framatome Gaia Fuel ML24248A2272024-09-0404 September 2024 Operator Licensing Examination Approval ML24240A1532024-09-0303 September 2024 Summary of Regulatory Audit Supporting the Review of License Amendment Request for Implementation of Framatome Gaia Fuel IR 05000336/20240052024-08-29029 August 2024 Updated Inspection Plan for Millstone Power Station, Units 2 and 3 (Reports 05000336/2024005 and 05000423/2024005 IR 05000336/20240022024-08-13013 August 2024 Integrated Inspection Report 05000336/2024002 and 05000423/2024002 ML24221A2872024-08-0808 August 2024 Independent Spent Fuel Storage Installation (ISFSI) - Submittal of Cask Registration for Spent Fuel Storage IR 05000336/20244412024-08-0606 August 2024 Supplemental Inspection Report 05000336/2024441 and 05000423/2024441 and Follow-Up Assessment Letter (Cover Letter Only) ML24212A0742024-08-0505 August 2024 Request for Withholding Information from Public Disclosure - Millstone Power Station, Unit No. 3, Proposed Alternative Request IR-4-13 to Support Steam Generator Channel Head Drain Modification ML24211A1712024-07-25025 July 2024 Associated Independent Spent Fuels Storage Installation, Revision to Emergency Plan - Report of Change IR 05000336/20244032024-07-22022 July 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000336/2024403 and 05000423/2024403 IR 05000336/20245012024-07-0101 July 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000336/2024501 and 05000423/2024501 ML24180A0932024-06-28028 June 2024 Readiness for Additional Inspection: EA-23-144 IR 05000336/20240102024-06-26026 June 2024 Biennial Problem Identification and Resolution Inspection Report 05000336/2024010 and 05000423/2024010 ML24178A2422024-06-25025 June 2024 2023 Annual Report of Emergency Core Cooling System (ECCS) Model, Changes Pursuant to the Requirements of 10 CFR 50.46 IR 05000336/20244402024-06-24024 June 2024 Final Significance Determination for Security-Related Greater than Green Finding(S) with Assessment Follow-up; IR 05000336/2024440 and 05000423/2024440 and Notice of Violation(S), NRC Investigation Rpt 1-2024-001 (Cvr Ltr Only) ML24176A1782024-06-20020 June 2024 Update to the Final Safety Analysis Report ML24176A2622024-06-20020 June 2024 Update to the Final Safety Analysis Report, Revision 37 ML24177A2792024-06-20020 June 2024 Preparation and Scheduling of Operator Licensing Examinations ML24280A0012024-06-20020 June 2024 Update to the Final Safety Analysis Report (Redacted Version) ML24281A2072024-06-20020 June 2024 Update to the Final Safety Analysis Report, Revision 37 (Redacted Version) 05000336/LER-2024-001, Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications2024-06-10010 June 2024 Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications ML24170B0532024-06-10010 June 2024 DOM-NAF-2-P/NP-A, Revision 0.5, Reactor Core Thermal-Hydraulics Using the VIPRE-D Computer Code ML24165A1292024-06-0505 June 2024 ISFSI, 10 CFR 50.59 Annual Change Report for 2023 Annual Regulatory Commitment Change Report for 2023 ML24128A2772024-06-0404 June 2024 Issuance of Amendment No. 290 to Revise TSs for Reactor Core Safety Limits, Fuel Assemblies, and Core Operating Limits Report for Use of Framatome Gaia Fuel (EPID L-2023-LLA-0074) (Non-Proprietary) ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24110A0562024-05-21021 May 2024 Exemption from the Requirements of 10 CFR Part 50, Section 50.46, and Appendix K Regarding Use of M5 Cladding Material (EPID L-2023-LLE-0013) (Letter) ML24109A0032024-05-21021 May 2024 Issuance of Amendment No. 289 to Revise Technical Specifications to Use Framatome Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limit (EPID L-2023-LLA-0065) (Non-Proprietary) ML24142A0952024-05-20020 May 2024 End of Cycle 22 Steam Generator Tube Inspection Report 05000423/LER-2023-006-01, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-20020 May 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications ML24141A2432024-05-20020 May 2024 Response to Request for Additional Information Regarding Alloy 600 Aging Management Program Submittal Related to License Renewal Commitment No. 15 IR 05000336/20240012024-05-14014 May 2024 Integrated Inspection Report 05000336/2024001 and 05000423/2024001 and Apparent Violation ML24123A2042024-05-0202 May 2024 Pre-Decisional Replay to EA-23-144 05000423/LER-2023-006, Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-0202 May 2024 Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications IR 05000336/20244012024-04-30030 April 2024 Security Baseline Inspection Report 05000336/2024401 and 05000423/2024401 (Cover Letter Only) ML24123A1222024-04-30030 April 2024 Inservice Inspection Program - Owners Activity Report, Refueling Outage 22 ML24116A0452024-04-25025 April 2024 Special Inspection Follow-Up Report 05000336/2024440 and 05000423/2024440 and Preliminary Finding(S) of Greater than Very Low Significance and NRC Investigation Report No. 1-2024-001 (Cover Letter Only) ML24116A1742024-04-24024 April 2024 Annual Radiological Environmental Operating Report ML24114A2662024-04-24024 April 2024 Submittal of 2023 Annual Radioactive Effluent Release Report ML24103A0202024-04-22022 April 2024 Summary of Regulatory Audit in Support of License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits ML24106A2032024-04-15015 April 2024 2023 Annual Environmental Operating Report ML24088A3302024-04-0404 April 2024 Regulatory Audit Plan in Support of License Amendment Request to Implement Framatome Gaia Fuel ML24093A2162024-04-0101 April 2024 Response to Request for Additional Information Regarding License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000423/LER-2024-001, Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary2024-10-14014 October 2024 Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary 05000423/LER-2023-006-02, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-09-26026 September 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications 05000336/LER-2024-001, Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications2024-06-10010 June 2024 Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-006-01, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-20020 May 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-006, Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-0202 May 2024 Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-005, Oil Leakage from C RSS Pump Motor Challenged Meeting Its Mission Time Resulting in a Condition Prohibited by Technical Specifications2024-02-0808 February 2024 Oil Leakage from C RSS Pump Motor Challenged Meeting Its Mission Time Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-004, For Millstone Power Station, Unit 3 Regarding Reactor Coolant System Pressure Isolation Valves Operational Leakage Exceeded the Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications2023-12-19019 December 2023 For Millstone Power Station, Unit 3 Regarding Reactor Coolant System Pressure Isolation Valves Operational Leakage Exceeded the Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-003, RCS Temperature Detector Exceeded Time Response Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications2023-12-0808 December 2023 RCS Temperature Detector Exceeded Time Response Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-002, Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications2023-11-30030 November 2023 Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications ML23334A1522023-11-30030 November 2023 Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications 05000336/LER-2023-002, Failed Check Valve Resulted in an Unanalyzed Condition2023-08-31031 August 2023 Failed Check Valve Resulted in an Unanalyzed Condition 05000423/LER-2023-001, Automatic Reactor Trip Due to Main Generator Output Breaker Ground Fault2023-07-27027 July 2023 Automatic Reactor Trip Due to Main Generator Output Breaker Ground Fault 05000336/LER-2023-001, For Millstone, Unit 2, Structural Integrity of a Train Service Water Header Piping Could Not Be Demonstrated Causing the Unit to Operate in a Condition Prohibited by Technical Specifications2023-07-0707 July 2023 For Millstone, Unit 2, Structural Integrity of a Train Service Water Header Piping Could Not Be Demonstrated Causing the Unit to Operate in a Condition Prohibited by Technical Specifications 05000423/LER-2022-002, Two Main Steam Safety Valves Installed in Wring Location Resulting in Failure to Lift within the Technical Specification Acceptance Criteria2022-05-31031 May 2022 Two Main Steam Safety Valves Installed in Wring Location Resulting in Failure to Lift within the Technical Specification Acceptance Criteria 05000423/LER-2022-001, Emergency Core Cooling and Reactor Plant Component Cooling Water Systems Inoperable for Time Greater than Allowed by Technical Specifications2022-03-24024 March 2022 Emergency Core Cooling and Reactor Plant Component Cooling Water Systems Inoperable for Time Greater than Allowed by Technical Specifications 05000336/LER-2022-001, Structural Integrity of Reactor Building Component Cooling Water Cracked Threaded Fitting Could Not Be Established Resulting in System Inoperable Longer than Allowed by Technical Specifications2022-03-18018 March 2022 Structural Integrity of Reactor Building Component Cooling Water Cracked Threaded Fitting Could Not Be Established Resulting in System Inoperable Longer than Allowed by Technical Specifications 05000336/LER-2021-002, Failed Check Valve Resulting in Unnalyzed and Operation Prohibited by Technical Specifications2022-01-0505 January 2022 Failed Check Valve Resulting in Unnalyzed and Operation Prohibited by Technical Specifications 05000336/LER-2021-001, Incorrectly Placed Spent Fuel Assemblies in Unit 2 Spent Fuel Pool2021-09-23023 September 2021 Incorrectly Placed Spent Fuel Assemblies in Unit 2 Spent Fuel Pool 05000423/LER-2019-0012020-02-13013 February 2020 LER 2019-001-00 for Millstone Power Station Unit 3 Regarding Plant Shutdown Required by Technical Specifications, Emergency Diesel Generator Exceeded Allowed Outage Time 05000423/LER-2017-0012017-03-20020 March 2017 Loss of Safety Function - Secondary Containment, LER 17-001-00 for Millstone, Unit 3 Regarding Loss of Safety Function - Secondary Containment 05000336/LER-2016-0022016-09-20020 September 2016 Manual Reactor Trip Due to Loss of Two Circulating Water Pumps, LER 16-002-00 for Millstone Power Station Unit 2 Regarding Manual Reactor Trip Due Loss Of Two Circulating Water Pumps 05000423/LER-2016-0052016-08-0909 August 2016 Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation, LER 16-005-00 for Millstone Power Station Unit 3 RE: Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation 05000423/LER-2016-0042016-07-13013 July 2016 Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator, LER 16-004-00 for Millstone Power Station Unit 3 RE: Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator 05000336/LER-2016-0012016-06-27027 June 2016 Turbine Driven Auxiliary Feedwater Putnp Room HELB Door Left Open, LER 16-001-00 for Millstone Power Station Unit 2 RE: Turbine Driven Auxiliary Feedwater Pump Room HELB Door Left Open 05000423/LER-2016-0032016-06-0808 June 2016 Loss of Safety Function- Supplementary Leak Collection and Release System, LER 16-003-00 for Millstone Power Station, Unit 3, Regarding Loss of Safety Function-Supplementary Leak Collection and Release System 05000423/LER-2016-0022016-03-23023 March 2016 Feedwater Isolation Signal Defeated Due to Wiring Error, LER 16-002-00 for Millstone Power Station Unit 3 Regarding Feedwater Isolation Signal Defeated Due to Wiring Error 05000423/LER-2016-0012016-03-16016 March 2016 Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump, LER 16-001-00 for Millstone Power Station Unit 3, Regarding Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump 05000336/LER-2015-0032016-01-0707 January 2016 Valid Actuation of the Reactor Protection System, LER 15-003-00 for Millstone, Unit 2, Regarding Valid Actuation of the Reactor Protection System ML0925900552009-09-0808 September 2009 Special Report for Seismic Instrumentation ML0719302812007-04-11011 April 2007 Final ASP Analysis- Millstone (LER 336/06-002) ML0622802402006-08-0808 August 2006 Special Report for Inoperable Radiation Monitor 2024-09-26
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Serial No. 2 3-209 Docket No. 50 -336 Licensee Event Report 2023-002 -00 Page 2 of 2
cc: U.S. Nuclear Regulat ory Commission Region I 475 Allendale Road, Suite 102, King of Prussia, PA 19406-1415.
R. V. Guzman NRC Project Manager Millstone Units 2 and 3 U.S. Nuclear Regulatory Commission One White Flint North, Mail Stop 08 C2 11555 Rockville Pike Rockville, MD 20852-2738
NRC Senior Resident Inspector Millstone Power Station Serial No.23-209 Docket No. 50- 336 Licensee Event Repor t 2023-002-00
ATTACHMENT
LICENSEE EVENT REPORT 2023- 002- 00 FAILED CHECK VALVE RESULTED IN AN UNANALYZED CONDITION.
MILLSTONE POWER STATION UNIT 2 DOMINION ENERGY NUCLEAR CONNECTICU T, INC.
Abstract
On July 6, 2023, at 0938, Millstone Power Station Unit 2 was in Mode 1 at 100 perc ent reactor power, when it was identified that the turbine driven auxiliary feedwater (TDAFW) pump supply check valve from #2 steam generator, 2-MS-4B, may not be able to prevent reverse flow in the event of a main steam line break in the #2 steam generator main steam line upstream of the main steam isolation valves. To verify its operability, the 2-MS-4B closure test was performed on July 6, 2023, at 1202, with unsatisfactory results. 2-MS-4B was disassembled and the bolt that holds the disc to swing arm was found to have failed.
The direct cause of the mechanical damage to the disc bolt was check valve chatter. 2-MS-4B internals were replaced and reactor power was reduced to 86% to reduce the valve chatter as an interim action. 2-MS-4B was replaced with a normally open nozzle check valve and reactor power was returned to 100%. The inability of 2-MS-4B to prevent reverse flow, constituted an unanalyzed condition that could result in exceeding the containment design pressure in response to a main steam line break. This report is being submitted as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety pursuant to 10 CFR 50.73(a)(2)(ii)(B).
On July 6, 2023, at 0938, Millstone Power Station Unit 2 was in Mode 1 at 100 percent reactor power, when it was identified that the turbine driven auxiliary feedwater (TDAFW) pump supply check valve from #2 steam generator, 2-MS-4B, may not be able to perform its safety function to prevent reverse flow in the event of a m ain steam line break (MSLB) in the #2 steam generator main steam line upstream of the main steam isolation valves. To verify its operability, the 2-MS-4B closure test was performed on July 6, 2023, at 1202, with unsatisfactory results. The TDAFW pump steam supply line containing 2-MS-4B was isolated by closing steam supply stop valve, 2-MS-202, from #2 steam generator on July 6, 2023, at 1206. 2-MS-4B was disassembled and the disc bolt holding the dis c to the swing arm was found to have failed with the disc sitting ins ide the valve body.
On July 3, 2023, at 2005, in Mode 1 during power ascension from a refueling outage, chattering was noted on 2-MS-4B.
Station personnel performed troubleshooting in an effort to eliminate or reduce the valve chatter by reconfiguring plant alignment and isolating steam traps on the Unit 2 main steam piping. Operations performed 2-MS-4B closure test on July 4, 2023, at 0359, which was satisfactory, demonstrating that the valve was capable to perform its safety function.
Continued valve chattering was observed on July 6, 2023, at 0250, providing a reasonable assurance that the valve disc was still attached to the swing arm and valve 2-MS-4B would be able to per form its isolation function at that time.
On July 6, 2023, upon no longer hearing valve chattering, the 2-MS-4B closure test was performed which required isolating one path of steam to the TDAFW Pump and entry into Technical Specification Action Statement (TSAS) 3.7.1.2.a at 1202. Results of the surveillance were unsatisfactory and the main steam line was maintained isolated. To support internal inspection of 2-MS-4B, both steam supply lines to the TDAFW Pum p were required to be isolated and TSAS 3.7.1.2.c was entered on July 6 at 1727 hours0.02 days <br />0.48 hours <br />0.00286 weeks <br />6.571235e-4 months <br />. The 2-MS-4B internals were replaced and post maintenance tests were completed including a satisfactory valve closure test on July 8, 2023. At 1729 on July 8, 2023, TSAS 3.7.1.2.c was exited. Troubleshooting was perfor med and an alternate plant configuration that involved lowering reactor power to 86%
that reduced valve chatter as an interim measure on July 11, 2023. 2-MS-4B closure test was performed with satisfactory results
The plant was maintained at 86% power awaiting an Engineering Change to replace the 2-MS-4B swing check valve with a normally open nozzle check valve. The 2-MS-4B nozzle check valve installation and post maintenance tes ting at 100% reactor power was completed on July 27, 2023, at 1307.
Evaluation determined that this condition, inability of 2-MS-4B to prevent reverse flow, constituted an unanalyzed condition that could result in exceeding the containment design pressure in response to a main steam line break. This failure would have resulted in the blowdown of both steam generators during a main steam line break in #2 steam generator main steam line upstream of the main steam isolation valves until the operators could manually isolate the faulted steam generator.
NRC resident inspectors were notified and an 8-hour non-emergency notification that the plant had been in an unanalyzed condition for the failure of 2-MS-4B was made on July 6, 2023, at 1648.
This 60-day report is being submitted to report that on July 6, 2023, from the time of discovery at 0938 until 1206, when the TDAFW pump steam supply line containing 2-MS-4B was isolated by closing steam supply stop valve, 2-MS-202, a condition existed that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety pursuant to 10 CFR 50.73(a)(2)(ii) (B).
CAUSE
The direct cause of the valve failure was mechanical damage to the disc bolt caus ed by check valve chatter.
ASSESSMENT OF SAFETY CONSEQUENCE S
The as found condition of 2-MS-4B resulted in the inability of the check valve to prevent reverse flow from the #1 steam generator main steam line in the event of a MSLB in the #2 steam generator main steam line upstream of the main steam isolation valves. Additionally, the potential for the 2-MS-4B separated disc to block steam flow from the #2 steam generator main steam line through 2-MS-4B to the TDAFW pump has not been conclusiv ely ruled out.
In the event of a MSLB in the #2 steam generator main steam line upstream of the main steam isolation valves with 2-MS-4B failing to prevent reverse flow, then the FSAR Section 14.8.2 MSLB analyses for the containment response would no longer be bounding. In this scenario, additional mass and energy releases fr om the intact #1 steam generator main steam line would continue until the operators isolate this steam flow path in accordance with the existing Emergency Operating Procedure guidance. This would result in an increase in mass and energy releases to containment with the predicted containment pressure exceeding the c ontainment design pressure of 54 psig. While the containment design pressure would have been exceeded, the predicted peak containment pressure would be less than the containment lower bound failure pressure of 102 psig established in the Millstone 2 Individual Plant Examination.
In the event the 2-MS-4B separated disc blocked all steam flow fr om the #2 steam generator main steam line through 2-MS-4B to the TDAFW pump, the other flow path from the #1 steam generator main steam line through 2-MS-4A to the TDAFW pump was available. The steam flow path through 2-MS-4A to the TDAFW pump is adequate for the pump to perform its design function of delivering auxiliary feedwater to the steam generators in the event of a loss of all AC power (station black out) and for all FSAR Chapter 14 Safety Analysis scenarios, except for MSLB in either main steam line upstream of the main steam isolation valves. In this MSLB scenario, the two remaining motor driven auxiliary feedwater pumps would be adequate to satisfy the reactor coolant system (RCS) decay heat removal safety function.
CORRECTIVE ACTION
The TDAFW pump steam supply swing disk check valve, 2-MS-4B, was replaced with a normally open nozzle check valve. Additional corrective actions will be taken in accordanc e with the stations corrective action program.
PREVIOUS OCCURRENCES
LER 2021-002-00
On Oct 23, 2021, during valve overhaul of 2-MS-4B, the valve disc was found separated from the disc arm. The direct cause of the event was mechanical damage due to valve disk chattering. Two interim corrective actions were implemented. An alternate system alignment was established which significantly reduced 2-MS-4B chatter. Also, 2-MS-4B was redesigned to have a more robust valve disc retention mechanism to reduce likelihood of its failure.
Following troubleshooting and discussions with third party vendors, an Engineering Change was implemented in May 2023 during the Unit 2 refueling outage to impr ove the piping configuration design to prevent the most probable cause, turbulent flow, from initiating check valve chatter. The piping configuration change was not successful in stopping the chatter. An Engineering Change to change the check valve was not pursued due to previous successes in preventing check valve chattering and indus try OE.
ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES
SB Main Steam V Valve
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05000423/LER-2023-001, Automatic Reactor Trip Due to Main Generator Output Breaker Ground Fault | Automatic Reactor Trip Due to Main Generator Output Breaker Ground Fault | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2023-001, For Millstone, Unit 2, Structural Integrity of a Train Service Water Header Piping Could Not Be Demonstrated Causing the Unit to Operate in a Condition Prohibited by Technical Specifications | For Millstone, Unit 2, Structural Integrity of a Train Service Water Header Piping Could Not Be Demonstrated Causing the Unit to Operate in a Condition Prohibited by Technical Specifications | | 05000423/LER-2023-002, Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications | Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2023-002, Failed Check Valve Resulted in an Unanalyzed Condition | Failed Check Valve Resulted in an Unanalyzed Condition | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000423/LER-2023-003, RCS Temperature Detector Exceeded Time Response Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications | RCS Temperature Detector Exceeded Time Response Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2023-004, For Millstone Power Station, Unit 3 Regarding Reactor Coolant System Pressure Isolation Valves Operational Leakage Exceeded the Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications | For Millstone Power Station, Unit 3 Regarding Reactor Coolant System Pressure Isolation Valves Operational Leakage Exceeded the Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2023-005, Oil Leakage from C RSS Pump Motor Challenged Meeting Its Mission Time Resulting in a Condition Prohibited by Technical Specifications | Oil Leakage from C RSS Pump Motor Challenged Meeting Its Mission Time Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2023-006-02, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications | Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(viii)(A) | 05000423/LER-2023-006-01, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications | Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2023-006, Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications | Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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