Similar Documents at Cook |
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LER-2077-024, Electrical Failure of Valve QMO-201, Charging Header Isolation |
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| 3162077024R00 - NRC Website |
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NRC FORM 195 (2-76 I U.S. NUCLEAR REGULATORY COM
~ION DOCKE~UMBER~ )
wD-9 FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL Mr. J.G.
Keppler FROM:
Indiana G Michigan Power Company Bridgman, Michigan D.V. Shaller DATE OF DOCUMENT
/19/77 DATE RECEIVED 8/1/77 Q LETTER Q OR IG INAL QCPP Y
DESCRIPTION
0 NOTOR IZE 0 Q UN C LASS IF I E D PROP INPUT FORM ENCLOSURE NUMBER OF COPIES RECEIVED Si'd Licensee Event Report PRO 50-315/7?-24 on 6/24/77 concerning~:valve QM0-201, Oharging Header Isolation, which would not close electrically during testing.
PLANT NAME:
Donald C. Cook Nuclear Plant VT 8/2/77 (1-P)
DO ROT RED~
ZCKZOWLED<<D (1-P)
NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J.
COLLINS Rem. 4 FOR ACTION/INFORMATION a
5 INTERNAL0 ISTR I BUTION EXTERNAL DISTR IBUTION CONTROL NUMBER ACRS 16 SENT AS AT
/
1
'.772140219 NRC FORM 195 (2 78)
D NA & MICHIGANPOf/VER COMP NY DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Bridgman, Michigan 49106 July 19, 1977 Mr. J.G.
- Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen El lyn, IL 60137
Dear Mr. Keppler:
, rg AUG'ging yQ "satec~~~~
gr Ataff~~~
I lr Og Operating License DPR-58 Docket No. 50-315 Pursuant to the requirements of Appendix A Technical Specifications and the United States Nuclear Regulatory Commission Regulatory Guide
- 1. 16, Revision 4, Section 2.b, the following report 'is'ubmitted:
RO 50-315/77-24.
Sincerely, D.V. Shaller Plant Manager
/bab cc:
J.E.
Dolan R.W. Jurgensen G.E. Lien R. Kilburn R.J.
Vollen BPI ROC. Callen MPSC K.R. Baker RO:III P.W. Steketee, Esq.
R. Walsh, Esq.
G. Charnoff, Esq.
G. Olson J.M. Hennigan PNSRC J.F. Stietzel Dir., (30 copies)
Dir., (3 copies) 7721402l9 JUL 21 1977
~~~
h;i I'
I" t
Form No. 4484 CONTROL BLOCK:
Q ICENSEE EVENT REPORT
~AC/(f8'20jij,)'~t-Qttf~t (PLEASE PRINT ALcI. REOUIREOAIIICdRIVIATION)
LCENSEE NAME LICENSE NUMBER LICENSE TYPE EVENT rYPF.
Qojs Ii I
OC C
I OO O
O O
O O
7 89 14 15 0
0 30 31 32 25 28 4
1 1
1 1
0 3
REPORT REI ORT CATEGORY TYPE SOURCE
~a~caus~
~L L
OS 7
8 57 58 59 80 81
~ ~ 4I OOCKE('PLUMBER 4 I 0 0 3
1 4
~
It 5'
88 69
" FVENI OATE RI I'ORT OATr.
6 24 7
7 0
7 I 97 7
74 75 EVENT OESCRIPTION Qo 2 Durin surveillance testin
, valve h10-201, Char in Header Isolation, would not close 7
8 9 80 [0D3] electricall A small amount of boric acid cr stal s from a sli ht ackin leak were 7
89 80 [oai] Ifcund cn the stem causin bindin Cleaned stem b
c clin valve b
hand.
Subse uent 7
8 9 80 [oOs]
tests of the valve were satisfactor The valve packing was properly adjusted which 7
8 9 Qog shoul d revent recurrence.
80 R 5-3 80 COMPONENT MANUFACTURER L
2 0
0 48 7
8 9 FAME SYSTEM
CAUSE
COMPONENT COBE COBE COMPONENT CODE SUPPLER VOLATION
~PC
~E V
A t V
0 P
N N
7 8 8 10 11 12 17 43 44 47 CAUSE OESCRIPTION toOI A ver sli ht ackin leak resulted in a boric acid cr stal buildu on the stem.
Thus 7
8 9 [iso]
7 89 FACIEITY STATUS
'L POWER I?~~ l LEJ ~
NA 7
8 9
10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY f11/
~Z Z
NA 7
8 9
10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION IttsI ~00 0
z I"lA 7
89 11,12 13 PERSONNEL INJURIES NUMBER
DESCRIPTION
~)4 ~00 0
NA 7
89 11 12 OTHER, STATUS OFFSITE CONSEQUENCES
~15 NA 7
8 9 LOSS OR OAMAGE TO FACILITY TYPE OESCRIPTION [116]
7 89 10 PUBLICITY NA
~
7 89 AOOITIONAL FACTORS
~18 NA 7
89 METHOO OF OISCOVERY 44 45 48 44 45 NA 7
8 9
~09 excessive tor ue was re uired to operate the valve remotely.
DISCOVERY OESCRIPTION LOCATION OF RELEASE 80 80 80 80 80 BO 80 80 80 80 80 7
89 NAME David G. Hizner 616-465-5901 80 CPO Ibt 4 667
REc<IVED 00cUHE>lp PHOCEss~yg g'~;-;
)9lf AU8 f
pg
~p pp
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