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LER-1982-060, Forwards LER 82-060/03L-0.Detailed Event Analysis Encl |
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'O PSEG i
Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 03038 i
Salem Generating Station August 18, 1982 1
Mr.
R.
C.
Haynes i
Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406 I
Dear Mr. Haynes:
LICENSE NO. DPR-75 3
DOCKET NO. 50-311 REPORTABLE OCCURRENCE 82-060/03L Pursuant to the requirements of Salem Generating Station j
Unit No.
2, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable a
Occurrence 82-060/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours, l
l<
r H.
J.
Midura j
General Manager -
Salem Operations RH:ksfj[ff CC:
Distribution I
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l 8200310395 820818 PDR ADDCK 05000311 S
PDR The Energy People gfW u m aa.o o et
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Report Number:
82-060/03L Report Date:
08-18-82 l
)
Occurrence Date:
07-22-82 Facility:
Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Emergency Core Cooling System-Accumulator - Inoperable.
This report was initiated by Incident Reports82-189 and 82-190.
l CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 - Rx Power 83% - Unit Load 890 MWe.
DESCRIPTION OF OCCURRENCE:
At 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />, on July 22, 1982, during normal operation, the Control Room Operator determined the contained volume of i
borated water in No. 24 Accumulator, as indicated by the temporary sightglass, was less than the minimum volume required by Technical Specification Limiting Condition for Operation 3.5.lb.
The accumulator was immediately declared inoperable j
and Action Statement 3.5.la was entered at 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />.
The l
control room operator commenced filling the accumulator, however, by 1440 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.4792e-4 months <br />, the level still was not within specified limits.
A unit load reduction was commenced in compliance with the Action Statement.
The accumulator level was increased to within specified limits.
At 1444 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.49442e-4 months <br />, l
July 22, 1982, No. 24 Accumulator was declared operable, Action l
Statement 3.5.la was terminated, and normal power operation l
was resumed.
Later that day, at 1743 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.632115e-4 months <br />, a temporary sight-glass was also installed on No. 23 Accumulator.
The control room operator determined, by sightolass indication, that the contained volume of borated water in No. 23 Accumulator, was less than the minimum required by Technical Specification Limiting Condition for Operation 3.5.1.
The accumulator was immediately declared inoperable and at 1743 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.632115e-4 months <br />, Action Statement 3.5.la was entered.
The control room operator commenced filling the accumulator, however, by 1843 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.012615e-4 months <br /> the accumulator level was j
not within the specified limits.
Preparation for a unit load reduction was commenced in compliance with the Action Statement.
i l
The accumulator level was raised to within specified limits.
At i
1844 hours0.0213 days <br />0.512 hours <br />0.00305 weeks <br />7.01642e-4 months <br />, July 22, 1982, No. 23 Accumulator was declared operable and Action Statement 3.5.la was terminated.
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LER 82-060/03L -
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
The cause of both occurrences was drift of level indications.
Each accumulator has two remote level indications.
An increasing difference between the indicated levels for No. 24 Accumulator had been noted.
Because the level transmitter isolation valves had some leakage, the transmitters could not be calibrated while the unit was operating.
Therefore, No. 24 Accumulator level was maintained to keep both indications within the specified limits.
When the difference in level indications for No. 24 Accumulator became excessive, a sight-glass was installed.
The sightglass indication revealed that the actual level was below specified limits.
The Action State-ment was immediately entered and the accumulator level was restored to normal operating band.
A similar problem of level indication drift for No. 23 Accumulator was also experienced.
In this case, the lower indication had been declared inoperable because it seemed to be inaccurate.
No. 23 Accumulator level had been maintained to keep the higher indication within the operating band.
The isolation valves for the level transmitters had some leakage, therefore, No. 23 Accumulator level transmitters could not be calibrated while operating.
Because of the problem discovered with No. 24 Accumulator level indication, a sightglass was also installed on No. 23 Accumulator.
The sightglass indication revealed that the accumulator actual level was below specified limits.
The Action Statement was immediately entered, and the accumulator level was restored to normal operating band.
ANALYSIS OF OCCURRENCE:
The operability of each Reactor Coolant System (RCS) accumulator ensures that a sufficient volume of borated water will be immediately forced into the reactor core through each of the cold legs in the event the RCS pressure falls below the pressure of the accumulators.
This initial surge of water into the core i
provides the initial cooling mechanism during large RCS pipe ruptures.
Action Statement 3.5.la requires:
With one accumulator inoperable, except as a result of a closed isolation valve, restore the inoperable accumulator to operable status within one hour or be in hot standby within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
LER 82-060/03L
- ANALYSIS OF OCCURRENCE:Inoperability of one accumulator constitutes operation in a degraded mode permitted by a Limiting Condition for Operation and is reportable in accordance with Technical Specification 6.9.1.9.b.
CORRECTIVE ACTION
As noted, sightglass level indicators have been installed and accumulator levels were raised to comply with the Technical Specifications.
An operator will check the sightglass indi-cations on No. 23 and 24 Accumulators every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
The level transmitters will be calibrated at the next scheduled outage.
A Design Change Request, 2EC-1424, has been submitted to replace the level transmitters and install additional valves at the next refueling outage.
FAILURE DATA:
Barton Instrument Co.
Level Transmitter Model 384-352 Prepared By R.
Heller
/
MM Gen 6raf Manager -
Salem Operations SORC Meeting No.
82-77
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| 05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed | | | 05000272/LER-1982-001-03, Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | Pressurizer Overprotection Sys Valve 1PR1 Was Isolated Due to Leakage. on 820107,while Draining Rcs,Valve 1RP2 Would Not Open. Caused by Generic Problem.Reactor Vessel Head Removed | | | 05000311/LER-1982-001-03, /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | /03L-0:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Sticking Open,Freezing Pressure Sensing Line.Damper Freed & Closed. Line Thawed | | | 05000272/LER-1982-001, Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | Forwards Revised LER 82-001/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-002-01, /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | /01T-0:on 820119,indications of Tube Thinning Were Detected by Eddy Current Exam.Steam Generators 12 & 14 Required Two & Three Sample Insp,Respectively.All Defective Tubes & Tubes Degraded Above 30& Plugged | | | 05000311/LER-1982-002-03, /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | /03L-0:on 820111,2A1 Battery Charger Tripped, Was Reset & Tripped Again.No Problem Found.Subsequent Trip Caused by Difference Between Battery Voltage & Battery Charger Voltage Setting.Personnel Instructed | | | 05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing | | | 05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo | Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage | | | 05000311/LER-1982-003, Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | Forwards LER 82-003/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-003-03, /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | /03L-0:on 820106,1B & 1C Diesels Locked Out, Rendering Diesels Inoperable at Same Time.On 820106,diesel Generator 1C Declared Inoperable While Diesel 1B Out of Svc for Maint.Caused by Misinterpretation of Lockout Switch Tag | | | 05000311/LER-1982-003-03, /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | /03L-0:on 820112,during Routine Calibr Testing, Radiation Monitor 2R11A Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Tested Satisfactorily | | | 05000272/LER-1982-004-03, /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | /03L-0:on 820109,primary Coolant Water Sample Results Indicated Excessive Boron Concentration,Constituting Positive Reactivity Change.Caused by Water Draining Out of Steam Generator Tubes.Rcs Rapid Boration Initiated | | | 05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration | | | 05000311/LER-1982-004, Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | Forwards LER 82-004/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-005-01, /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | /01X-1:on 820131,degradation of Fuel Cladding on Fuel Assembly C-04 Discovered.Caused by Fuel Lockup Due to Wedged Fuel Pellet.Fuel Assembly Placed in Spent Fuel Pit. All C Assemblies Scheduled for Reuse in Core | | | 05000272/LER-1982-005, Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | Forwards LER 82-005/01X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-005, Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | Forwards LER 82-005/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-005-03, /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | /03L-0:on 820121,during Performance of M3T Maint Surveillance Test Undervoltage Relay on 2C Vital Bus Actuated at 5.5 Volts Instead of 77.3 Volt Trip Setpoint Value.No Defects Found.Relay Recalibr | | | 05000272/LER-1982-006-03, /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | /03L-0:on 820113,air Particulate Detector Failed. Cause Not Stated.All Required Containment Purge & Pressure Vacuum Relief Penetrations Isolated.High & Low Speed Filter Paper Drives Replaced | | | 05000272/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006, Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | Forwards LER 82-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-006-03, /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | /03L-0:on 820128,svc Water Flow Indicator Indicated No Flow Condition.Caused by Svc Water Discharge Valve 22SW223 Being Stuck Shut.Valve Opened,Locally Tested & Returned to Svc | | | 05000272/LER-1982-007-01, /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | /01X-2:on 820211,during Design Review,Discovered That Check Valves 1AF71 & 1AF72 & Associated Piping Not Seismically Analyzed & Protected.Protective Steel Structures Provided Off Seismic Wall | | | 05000272/LER-1982-007, Forwards LER 82-007/01X-2 | Forwards LER 82-007/01X-2 | | | 05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added | | | 05000272/LER-1982-008-03, /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | /03L-0:on 820126,sample Results from Boric Acid Tanks Indicated Boric Acid Concentration Below Tech Specs. Refueling Water Storage Tank Low.Core Alterations & Positive Reactivity Changes Suspended.Level Adjusted | | | 05000311/LER-1982-008, Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | Forwards LER 82-008/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-008-03, /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | /03L-0:on 820128,overpower Delta T Indication for Channel 21 Failed High.Caused by Signal Summator 2T-M412E Having No Output Due to Failed Capacitors. Five Capacitors Replaced | | | 05000311/LER-1982-009, Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | Forwards LER 82-009/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage | | | 05000272/LER-1982-009-03, /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | /03L-0:on 820118 & 25,switches for Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Tank Area 12 Had Been in Manual Position for Greater than 14 Days Due to Maint Outage | | | 05000311/LER-1982-009-03, /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | /03L-0:on 820129,air Particulate Detector Pump Low Flow Alarm Annuniciated.Caused by Incorrect Normal Flow Valve Lineup to Pump.Pump Removed from Normal Flow & Placed in Backup Flow Lineup | | | 05000311/LER-1982-010-03, /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | /03L-0:on 820201,discrepancy Between Individual Rod Position Indicator (Irpi) & Control Rod Bank Demand Indicator for Rod 2C2 Exceeded 12 Steps in Either Direction. Caused by Incorrect Calibr of Irpi.Irpi Calibr | | | 05000272/LER-1982-010-03, /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | /03X-1:on 820201,temporary Hose Connection from Unit 1 Spent Fuel Pool to Unit 2 Exchanger Found Leaking on Auxiliary Bldg 84-ft Elevation.Caused by Improper Clamp Installation.Hose Disconnected | | | 05000311/LER-1982-010, Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | Forwards LER 82-010/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1982-010, Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | Forwards LER 82-010/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-011, Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | Forwards LER 82-011/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-011-03, /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | /03L-0:on 820205,during Radiological Survey of Hot Laundry Trailer Area,Technician Discovered Lint from Dryer Exhaust of Trailer B Revealing Traces of Cs-137,Co-60 & Co-58.New Trailer & Lint Collector Installed | | | 05000272/LER-1982-011, Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | Forwards LER 82-011/03X-1.Detailed Event Analysis Encl | | | 05000272/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | Forwards LER 82-012/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-012, Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | Forwards LER 82-012/03X-1.Detailed Event Analysis Encl | | | 05000311/LER-1982-012-03, /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | /03X-1:on 820209,steam Generator Level Channel 2 Displayed Erratic Behavior,Indicating Drift.Apparently Caused by Intermittent Ground on Signal Lead.Ground Eliminated by Lifting Leads While Troubleshooting Problem | | | 05000272/LER-1982-012-03, /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | /03L-0:on 820223,operator Found Significant Amount of Chromated Water on Floor in Diesel Generator 1B Cubicle. Caused by Leakage on Right Side Jacket Water Heater.Jacket Water Heaters Replaced | | | 05000272/LER-1982-013-03, /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | /03L-0:on 820301,control Room Operator Closed Pressurizer Relief Valve 1PR1 When Valve 1PR2 Was Still Closed.Caused by Operator Error.Operator Counseled by Senior Shift Supervisor | | | 05000311/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-013-03, L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | L-0:on 820215,shift Supervisor Informed That Two 4-inch Core Bores Opened on 78-ft Elevation Between Mechanical & Electrical Penetration Areas.No Fire Watch Posted.Caused by Inadvertently Posting Watch on Wrong Unit | | | 05000272/LER-1982-013, Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | Forwards LER 82-013/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1982-014-03, /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | /03L-0:on 820219,steam Generator 21 Level Channel 2 Read 20% Higher than Channels 3 & 4.Channel 2 Declared Inoperable.Cause Unknown.Transmitter Tested & Found Satisfactory.Sensing Lines Blown Down to Remove Solids | | | 05000272/LER-1982-014-03, /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | /03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable | | | 05000311/LER-1982-014, Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | Forwards LER 82-014/03L-0.Detailed Event Analysis Encl | |
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