05000311/LER-1981-073, Forwards LER 81-073/03L-0.Detailed Event Analysis Encl

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Forwards LER 81-073/03L-0.Detailed Event Analysis Encl
ML20030D309
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/21/1981
From: Midura H
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20030D310 List:
References
NUDOCS 8109010159
Download: ML20030D309 (3)


LER-1981-073, Forwards LER 81-073/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
3111981073R00 - NRC Website

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t.,6 A O PSEG Public Service Electric and Gas Company P.O. Box 168 Hancocks Bridge, New Jersey 08038 Salem Generating Station August 21, 1981

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Mr. Boyce H.

Grier g

Director of USNRC

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Office of Inspection and Enforcement

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Region 1 631 Park Avenue 0y King of Prussia, Pennsylvanir 19406 5

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Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-73/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 81-73/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours, l

QPwl Q

1 H.

J. Midura Manager -

Salem Generating Station CC:

R. A.

Uderitz General Manager - Nuclear Production Director, Office of Inspection and Entorcement (30 copies) gp Director, Office of Management I

Information and Program Control j

(3 copies)

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i The Energy Peorde 9sm9 tuwnico 8109010159 810821 l

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Report Number:

81-73/03L Report Date:

Occurrence Date:

7-24-81 Facility:

Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

125V DC Distribution System - 2Cl Battery Charger - Inoperable.

This report was initiated by Incident Report 81-277.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 1 - Rx Power 50% - Unit Load 460 MWe DESCRIPTION OF OCCURRENCE:

At approximately 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />, July 24, 1981, the control operator noticed No. 2Cl battery charger had tripped.

Upon resetting the breaker, it tripped again.

No.2C2 battery charger was put in service.

No. 2Cl battery charger was declared inoperable and action statement 3.8.2.3.c was entered at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />, July 24, 1981.

This occurrence constituted operation in a degraded mode in accord-ance with technical specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The cause of the first trip is unknown.

The battery charger was inspected and no problem was found.

The subsequent trips were caused by personnel error.

The battery voltage was several volts lower than the battery charger voltage setting.

That caused an immediate over-current situation, tripping the battery charaer breaker.

ANALYSIS OF OCCURRENCE:

Technical specification 3.8.2.3.c requires:

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With one 125 volt D.C. battery charger inoperable, restore the inoperable charger to operable status within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or connect the back-up charger for no more than 7 days or be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

LER 81-73/03L CORRECTIVE ACTION:

The battery charger voltage was reduced to match the battery voltage, and stepped up during the charge until full voltage was attained.

Personnel involved were instructed as to the problem.

At 0607 hours0.00703 days <br />0.169 hours <br />0.001 weeks <br />2.309635e-4 months <br />, July 25, 1981, No. 2Cl battery charger was back in service and action statement 3.8.2.3.c was terminated.

FAILURE DATA:

Not Applicable 6

e Prepared By F.

Dickey Manager - Salem Generating Station SORC Meeting No.

81-79 D

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