05000272/LER-1981-053, Forwards LER 81-053/03L-0.Detailed Event Analysis Encl

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Forwards LER 81-053/03L-0.Detailed Event Analysis Encl
ML19350E800
Person / Time
Site: Salem PSEG icon.png
Issue date: 06/12/1981
From: Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19350E801 List:
References
NUDOCS 8106230535
Download: ML19350E800 (2)


LER-1981-053, Forwards LER 81-053/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2721981053R00 - NRC Website

text

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O PSIEG Putalic Service Electric and Gas Company 80 Park Plaza Newar k, N.J. 07101 Phone 201/430 7000 June 12, 1981 estim 5

Mr. Boyce H. Grier 8

f I' U N lj j' 1

Director of USNRC Office of Inspection and Enforcement [i

NN 2 3 ISSj m ~g Region 1

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u.s. m m, %

631 Park Avenue King of Prussia, Pennsylvania 19406 O

Dear Mr. Grier:

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LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-53/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-53/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

[

Uderity R. A.

General Manager -

Nuclear Production CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies) 8106:230636 3

mem ne w w. w e:

O PSEG l

Pubhc Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430 7000 June 12, 1981 Mr. Boyce H. Grier Director of USNRC Office of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 81-53/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 81-53/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

/

R. A.

Uderit General Manager -

Nuclear Production CC:

Lirector, Office of Inspection 4

and Enforcement (30 copies) b Director, Office of Management Information and Program Control (3 copies)

The Energy People 9s m :w,4 a:.

~.

.b E'

7

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ReporE Number: -

81-53/03L.

1

.i' Report Date:-

June 12, 1981-

^

OccurrencecDate:.5/20/.81' Facility:

Salem Generating Station, Unit 1.

Public Service' Electric-& Gas Company

.Hancocks Bridge, New Jersey 08038

. IDENTIFICATION--OF OCCURRENCE:

lB Diesel - Inoperable'- Water' Jacket Leak

~

CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 - Rx Power 0% - Unit Load OMW DESCRIPTION OF OCCURRENCE:-

' During routine' operation, an operator making rounds discovered the 1B Diesel Water Jacket was. leaking via a 1/4" pipe nipple.- Action ~

Statement'3.8.1.1 was entered at 05045 hours on May'20, 1981..

This occurrence' constituted operation in a degraded mode in accordance-

'with Technical Specification 6.9.1.9b.

DESIGNATION OF' APPARENT CAUSE OF OCCURRENCE:

- Personnel error.

This occurrence was caused by apparent use of the

' nipple-for-support'by an unknown person.

i ANALYSIS OF OCCURRENCE:.

. Technical Specification 3.8.1.la requires that with either an'offsite circuit or diesel generator inoperable demonstrate the operability of_the' remaining A.C. sources by performing Surveillance Requirements 4.8.l.1.la and 4.8.1.1.2.a.2 within one hour'and at least once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />; thereafter, restore at least two offsite circuits and three diesel generators to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least hot-standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown within-the'following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

b CORRECTIVE' ACTION:

}

The 1/4 inch nipple was replaced in kind, and 1B Diesel Generator was

. tested satisfactorily. -Action Statement 3.8.1.1 was terminated at 1650 hours0.0191 days <br />0.458 hours <br />0.00273 weeks <br />6.27825e-4 months <br /> on-May 20, 1981.

FAILURE DATA:

1/4Linch~ carbon steel nipple.

- Prepared By J.

J.

Espey

/

Manager - Salem Generating Station SORC Meeting No.

81-47'